Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2022-10-17 — TX
Operator
Kinder Morgan Liquid Terminals, Llc
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$2,050
Incident datetime
2022-10-17 01:35
Report number
Location
TX
Narrative
On 10/17/2022, at 0100 (central), kinder morgan liquids terminals operations personnel at galena park noticed a hydrocarbon alarm. The location of the alarm was at tank 80-21/22 pump manifold. Operations personnel were dispatched to investigate. When they arrived at the location of the alarm, they found a sample port (threaded fitting), near a pressure relief system had broken off and product was leaking into the concrete containment. An estimated 10 gallons of gasoline blend stock leaked into the concrete containment. Only the affected pump was shut down and the affected piping was isolated. The failed component was removed and sent out for metallurgical analysis. The metallurgical analysis determined that the threaded nipple (bleeder on thermal relief piping) failed due to high-cycle fatigue initiating at the thread root of the nipple connection. New piping was installed, and the pump was returned back into service the next day. 2/26/2024 - gps coordinates were updated.
Detailed record list
Report Received Date
2022-11-17 00:00:00
Iyear
2022
Report Number
20220255
Supplemental Number
39255
Report Type
Supplemental Final
Operator Id
26041
Name
Kinder Morgan Liquid Terminals, Llc
Operator Street Address
1001 Louisiana St, Suite 1000
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2022-10-17 01:30:00
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
29.728611
Location Longitude
-95.233889
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
0.25
Recovered Bbls
0.25
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Or Pack Calculations)
Incident Identified Datetime
2022-10-17 01:35:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
No
Shutdown Explain
Only The Affected Pump Was Shut Down And Isolated.
Communication State Fed Ind
No
On Site Datetime
2022-10-17 01:35:00
Confirmed Discovery Datetime
2022-10-17 01:35:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Notify Qualified Indiv Ind
No
Oil Spill Removal Org Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Kinder Morgan Galena Park Terminal
Segment Name
80-21/22 Pump Manifold
Onshore State Abbreviation
Tx
Onshore Postal Code
77547
Onshore City Name
Galena Park
Onshore County Name
Harris
Designated Location
Milepost
Designated Name
80-21/22 Man.
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Relief Line And Relief Equipment
Installation Year
1997
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Commercially Nav Ind
Yes
Commercially Nav Yes No
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Usa Ecological Ind
Yes
Usa Ecological Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
2050
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
2050
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
25
Mop Psig
150
Mop Cfr Section
Component Design Pressure �195.406(A)(2)
Maop Established Date
1997-01-01 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
< 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The cause of the leak was determined to be unrelated to controller action.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Threaded Connection/coupling Failure
Eq Failure Type
Threaded Connection/coupling Failure
Other Stripped Ind
Pipe Nipple
Eq Additional Other Ind
Yes
Eq Additional Other Details
High-Cycle Fatigue As Detailed In The Metallurgical Analysis Report.
Preparer Name
A**** R***** J*
Preparer Title
Compliance Manager
Preparer Email
A***********@k***********.com
Preparer Telephone
713.420.6325
Prepared Date
2024-02-26 00:00:00
Local Contact Name
A*** R*****
Local Contact Email
A**********@k***********.com
Local Contact Telephone
346.352.5923
Authorizer Name
A**** R***** J*
Authorizer Telephone
713.420.6325
Authorizer Title
Compliance Manager
Authorizer Email
A***********@k***********.com
Narrative
On 10/17/2022, at 0100 (central), kinder morgan liquids terminals operations personnel at galena park noticed a hydrocarbon alarm. The location of the alarm was at tank 80-21/22 pump manifold. Operations personnel were dispatched to investigate. When they arrived at the location of the alarm, they found a sample port (threaded fitting), near a pressure relief system had broken off and product was leaking into the concrete containment. An estimated 10 gallons of gasoline blend stock leaked into the concrete containment. Only the affected pump was shut down and the affected piping was isolated. The failed component was removed and sent out for metallurgical analysis. The metallurgical analysis determined that the threaded nipple (bleeder on thermal relief piping) failed due to high-cycle fatigue initiating at the thread root of the nipple connection. New piping was installed, and the pump was returned back into service the next day. 2/26/2024 - gps coordinates were updated.
| Report Received Date | 2022-11-17 00:00:00 |
|---|---|
| Iyear | 2022 |
| Report Number | 20220255 |
| Supplemental Number | 39255 |
| Report Type | Supplemental Final |
| Operator Id | 26041 PHMSA Enforcement |
| Name | Kinder Morgan Liquid Terminals, Llc |
| Operator Street Address | 1001 Louisiana St, Suite 1000 |
| Operator City Name | Houston |
| Operator State Abbreviation | TX |
| Operator Postal Code | 77002 |
| Local Datetime | 2022-10-17 01:30:00 |
| Time Zone | Central |
| Daylight Savings Ind | Yes |
| Location Latitude | 29.728611 Google Maps OpenStreetMap |
| Location Longitude | -95.233889 Google Maps OpenStreetMap |
| Commodity Released Type | Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions |
| Commodity Subtype | Gasoline (Non-Ethanol) |
| Unintentional Release Bbls | 0.25 |
| Recovered Bbls | 0.25 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Accident Identifier | Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Or Pack Calculations) |
| Incident Identified Datetime | 2022-10-17 01:35:00 |
| System Part Involved | Onshore Terminal/tank Farm Equipment And Piping |
| On Off Shore | Onshore |
| Status When Identified | Normal Operation, Includes Pauses Between Batches And During Maintenance |
| Shutdown Due Accident Ind | No |
| Shutdown Explain | Only The Affected Pump Was Shut Down And Isolated. |
| Communication State Fed Ind | No |
| On Site Datetime | 2022-10-17 01:35:00 |
| Confirmed Discovery Datetime | 2022-10-17 01:35:00 |
| Nrc Rpt Num | Nrc Notification Not Required NRC Report How to search |
| Ignite Ind | No |
| Notify Qualified Indiv Ind | No |
| Oil Spill Removal Org Ind | No |
| Num Pub Evacuated | 0 |
| Pipe Fac Name | Kinder Morgan Galena Park Terminal |
| Segment Name | 80-21/22 Pump Manifold |
| Onshore State Abbreviation | Tx |
| Onshore Postal Code | 77547 |
| Onshore City Name | Galena Park |
| Onshore County Name | Harris |
| Designated Location | Milepost |
| Designated Name | 80-21/22 Man. |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Aboveground |
| Incident Area Subtype | Typical Aboveground Facility Piping Or Appurtenance |
| Crossing | No |
| Pipe Facility Type | Interstate |
| Item Involved | Relief Line And Relief Equipment |
| Installation Year | 1997 |
| Manufactured Year | Unknown |
| Material Involved | Carbon Steel |
| Release Type | Leak |
| Leak Type | Connection Failure |
| Wildlife Impact Ind | No |
| Soil Contamination | No |
| Long Term Assessment | No |
| Remediation Ind | No |
| Water Contam Ind | No |
| Could Be Hca | Yes |
| Commodity Reached Hca | Yes |
| Commercially Nav Ind | Yes |
| Commercially Nav Yes No | Yes |
| High Pop Ind | Yes |
| High Pop Yes No | Yes |
| Other Pop Ind | Yes |
| Other Pop Yes No | Yes |
| Usa Drinking Ind | Yes |
| Usa Drinking Yes No | Yes |
| Usa Ecological Ind | Yes |
| Usa Ecological Yes No | Yes |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 0 |
| Est Cost Prop Damage | 2050 |
| Est Cost Emergency | 0 |
| Est Cost Environmental | 0 |
| Est Cost Other | 0 |
| Prpty | 2050 |
| Num Persons Hosp Not Ovnght | 0 |
| Num Injured Treated By Emt | 0 |
| Num Resident Building Affctd | 0 |
| Num Business Building Affctd | 0 |
| Accident Psig | 25 |
| Mop Psig | 150 |
| Mop Cfr Section | Component Design Pressure �195.406(A)(2) View CFR 49 §192 |
| Maop Established Date | 1997-01-01 00:00:00 |
| Maop Reversal Flow Ind | No |
| Accident Pressure | Pressure Did Not Exceed Mop |
| Pressure Restriction Ind | No |
| Pipeline Function | < 20% Smys Regulated Transmission |
| Scada In Place Ind | Yes |
| Scada Operating Ind | Yes |
| Scada Functional Ind | Yes |
| Scada Detection Ind | Yes |
| Scada Conf Ind | Yes |
| Cpm In Place Ind | No |
| Investigation Status | No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate) |
| Investigation Status Details | The cause of the leak was determined to be unrelated to controller action. |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Equipment Failure |
| Cause Details | Threaded Connection/coupling Failure |
| Eq Failure Type | Threaded Connection/coupling Failure |
| Other Stripped Ind | Pipe Nipple |
| Eq Additional Other Ind | Yes |
| Eq Additional Other Details | High-Cycle Fatigue As Detailed In The Metallurgical Analysis Report. |
| Preparer Name | A**** R***** J* |
| Preparer Title | Compliance Manager |
| Preparer Email | A***********@k***********.com |
| Preparer Telephone | 713.420.6325 |
| Prepared Date | 2024-02-26 00:00:00 |
| Local Contact Name | A*** R***** |
| Local Contact Email | A**********@k***********.com |
| Local Contact Telephone | 346.352.5923 |
| Authorizer Name | A**** R***** J* |
| Authorizer Telephone | 713.420.6325 |
| Authorizer Title | Compliance Manager |
| Authorizer Email | A***********@k***********.com |
| Narrative | On 10/17/2022, at 0100 (central), kinder morgan liquids terminals operations personnel at galena park noticed a hydrocarbon alarm. The location of the alarm was at tank 80-21/22 pump manifold. Operations personnel were dispatched to investigate. When they arrived at the location of the alarm, they found a sample port (threaded fitting), near a pressure relief system had broken off and product was leaking into the concrete containment. An estimated 10 gallons of gasoline blend stock leaked into the concrete containment. Only the affected pump was shut down and the affected piping was isolated. The failed component was removed and sent out for metallurgical analysis. The metallurgical analysis determined that the threaded nipple (bleeder on thermal relief piping) failed due to high-cycle fatigue initiating at the thread root of the nipple connection. New piping was installed, and the pump was returned back into service the next day. 2/26/2024 - gps coordinates were updated. |
External Resources
PHMSA pipeline safety insights.
Product
Features
Company
All rights reserved. Copyright © by ClearPHMSA