HL incident on 2022-10-25 — TX

Operator
Chevron Midstream Services Llc
Cause
Miscellaneous Root Causes
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$810,000
Incident datetime
2022-10-25 08:30
Report number
Location
TX
Narrative
On oct 25th 2022, a third party as part of developement activities in area was provided clearance via 811 system to excavate 18" of topsoil in the pipeline area. Third party excavated outside of approved 18" depth zone and struck pipeline releasing crude oil into excavated hole.
Detailed record list
Report Received Date
2022-11-15 00:00:00
Iyear
2022
Report Number
20220252
Supplemental Number
41545
Report Type
Supplemental
Operator Id
Name
Chevron Midstream Services Llc
Operator Street Address
1400 Smith St Floor 37
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2022-10-25 08:30:00
Time Zone
Mountain
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
350
Recovered Bbls
90
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Third Party That Caused The Accident
Incident Identified Datetime
2022-10-25 08:30:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2022-10-25 09:45:00
Restart Datetime
2022-11-09 08:00:00
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Initial Responder Com Datetime
2022-10-25 08:30:00
On Site Datetime
2022-10-25 08:10:00
Confirmed Discovery Datetime
2022-10-25 09:44:00
Nrc Rpt Datetime
2022-10-25 12:41:00
Nrc Rpt Num
Additional Nrc Report Numbers
1350819, 1350892
Ignite Ind
No
Upstream Action Taken
Operational Control
Upstream Oprtnl Cntrl Detail
Shutdown Of Production Site Pump
Downstream Action Taken
Operational Control
Downstream Oprtnl Cntrl Detail
Pump Shutdown
Notify Qualified Indiv Ind
Yes
Qualified Indiv Notif Datetime
2022-10-25 10:00:00
Oil Spill Removal Org Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Evans Lateral
Segment Name
Bdo-06-Rvg-100-L2
Onshore State Abbreviation
Co
Onshore Postal Code
80631
Onshore City Name
Evans
Onshore County Name
Weld
Designated Location
Milepost
Designated Name
1.2
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Exposed Due To Excavation
Depth Of Cover
72
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Body
Puddle Weld Ind
No
Pipe Diameter
6.625
Pipe Wall Thickness
0.219
Pipe Smys
52000
Pipe Specification
Unknown
Pipe Seam Type
Erw - High Frequency
Pipe Manufacturer
Unknown
Pipe Coating Type
Fusion Bonded Epoxy(Fbe)
Coating Applied Ind
No
Installation Year
2016
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Mechanical Puncture
Puncture Axial
4
Puncture Circum
6
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
Yes
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
810000
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Est Cost Other Details
Not Known At This Time
Prpty
810000
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
250
Mop Psig
1440
Mop Cfr Section
Subpart E Pressure Test �195.406(A)(3)
Maop Established Date
2016-12-18 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Gathering
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
It was readily evident that controller or control room were not contributing factors to accident.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
Yes
One Call System Ind
Yes
State Law Exempt Ind
No
Notify Cga Dirt
No
Pipeline Easement Row Ind
Yes
Joint Trench Ind
No
Cross Bore Ind
No
Depth Of Grade
> 36�
Excavator Type
Contractor
Excavator Equipment
Backhoe/trackhoe
Work Performed
Site Development
One Call Notified Ind
Yes
One Call Ticket Num
B22830127800b
White Lined Ind
No
Locator Type
Facility Owner
Visible Marks
No
Service Interruption
Yes
Service Interruption Hours
384
Root Cause Category
Miscellaneous Root Causes
Root Cause Type
Root Cause Not Listed (Comment Required)
Root Cause Type Other
Excavated In Wrong Area, And Wrong Property
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
Other
Other Non Threaded Details
Block Valve Sealing Body O-Ring Failed Due To Liquid Buildup In Pig Receiver Barrel
Eq Additional Other Ind
Yes
Eq Additional Other Details
No
Preparer Name
C**** G****
Preparer Title
Regulatory Specialist
Preparer Email
C**********@c******.com
Preparer Telephone
9703818443
Prepared Date
2025-11-04 00:00:00
Local Contact Name
C**** G****
Local Contact Email
C**********@c******.com
Local Contact Telephone
9703818443
Authorizer Name
C**** G****
Authorizer Telephone
9703818443
Authorizer Email
C**********@c******.com
Narrative
On oct 25th 2022, a third party as part of developement activities in area was provided clearance via 811 system to excavate 18" of topsoil in the pipeline area. Third party excavated outside of approved 18" depth zone and struck pipeline releasing crude oil into excavated hole.
Report Received Date 2022-11-15 00:00:00
Iyear 2022
Report Number 20220252
Supplemental Number 41545
Report Type Supplemental
Operator Id 40419 PHMSA Enforcement
Name Chevron Midstream Services Llc
Operator Street Address 1400 Smith St Floor 37
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2022-10-25 08:30:00
Time Zone Mountain
Daylight Savings Ind Yes
Location Latitude 40.37301 Google Maps OpenStreetMap
Location Longitude -104.75821 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 350
Recovered Bbls 90
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Notification From Third Party That Caused The Accident
Incident Identified Datetime 2022-10-25 08:30:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Status When Identified Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind Yes
Shutdown Datetime 2022-10-25 09:45:00
Restart Datetime 2022-11-09 08:00:00
Communication State Fed Ind Yes
Party Initiated Communication Operator
Initial Responder Com Datetime 2022-10-25 08:30:00
On Site Datetime 2022-10-25 08:10:00
Confirmed Discovery Datetime 2022-10-25 09:44:00
Nrc Rpt Datetime 2022-10-25 12:41:00
Nrc Rpt Num 1350806 NRC Report How to search
Additional Nrc Report Numbers 1350819, 1350892
Ignite Ind No
Upstream Action Taken Operational Control
Upstream Oprtnl Cntrl Detail Shutdown Of Production Site Pump
Downstream Action Taken Operational Control
Downstream Oprtnl Cntrl Detail Pump Shutdown
Notify Qualified Indiv Ind Yes
Qualified Indiv Notif Datetime 2022-10-25 10:00:00
Oil Spill Removal Org Ind No
Num Pub Evacuated 0
Pipe Fac Name Evans Lateral
Segment Name Bdo-06-Rvg-100-L2
Onshore State Abbreviation Co
Onshore Postal Code 80631
Onshore City Name Evans
Onshore County Name Weld
Designated Location Milepost
Designated Name 1.2
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Exposed Due To Excavation
Depth Of Cover 72
Crossing No
Pipe Facility Type Intrastate
Item Involved Pipe
Pipe Type Pipe Body
Puddle Weld Ind No
Pipe Diameter 6.625
Pipe Wall Thickness 0.219
Pipe Smys 52000
Pipe Specification Unknown
Pipe Seam Type Erw - High Frequency
Pipe Manufacturer Unknown
Pipe Coating Type Fusion Bonded Epoxy(Fbe)
Coating Applied Ind No
Installation Year 2016
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Mechanical Puncture
Puncture Axial 4
Puncture Circum 6
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment Yes
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 810000
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Est Cost Other Details Not Known At This Time
Prpty 810000
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 250
Mop Psig 1440
Mop Cfr Section Subpart E Pressure Test �195.406(A)(3) View CFR 49 §192
Maop Established Date 2016-12-18 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Gathering
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details It was readily evident that controller or control room were not contributing factors to accident.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Ex Party Type Excavation Damage By Third Party
Prior Notification Ind Yes
One Call System Ind Yes
State Law Exempt Ind No
Notify Cga Dirt No
Pipeline Easement Row Ind Yes
Joint Trench Ind No
Cross Bore Ind No
Depth Of Grade > 36�
Excavator Type Contractor
Excavator Equipment Backhoe/trackhoe
Work Performed Site Development
One Call Notified Ind Yes
One Call Ticket Num B22830127800b
White Lined Ind No
Locator Type Facility Owner
Visible Marks No
Service Interruption Yes
Service Interruption Hours 384
Root Cause Category Miscellaneous Root Causes
Root Cause Type Root Cause Not Listed (Comment Required)
Root Cause Type Other Excavated In Wrong Area, And Wrong Property
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind Other
Other Non Threaded Details Block Valve Sealing Body O-Ring Failed Due To Liquid Buildup In Pig Receiver Barrel
Eq Additional Other Ind Yes
Eq Additional Other Details No
Preparer Name C**** G****
Preparer Title Regulatory Specialist
Preparer Email C**********@c******.com
Preparer Telephone 9703818443
Prepared Date 2025-11-04 00:00:00
Local Contact Name C**** G****
Local Contact Email C**********@c******.com
Local Contact Telephone 9703818443
Authorizer Name C**** G****
Authorizer Telephone 9703818443
Authorizer Email C**********@c******.com
Narrative On oct 25th 2022, a third party as part of developement activities in area was provided clearance via 811 system to excavate 18" of topsoil in the pipeline area. Third party excavated outside of approved 18" depth zone and struck pipeline releasing crude oil into excavated hole.

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