HL incident on 2022-10-05 — TX

Operator
Tc Oil Pipeline Operations Inc
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$24,149
Incident datetime
2022-10-05 05:50
Report number
Location
TX
Narrative
6.5 barrels of product was released onto the facility piping and gravel pad at the david city pump station through a pin that had completely backed out of the bleed plug on the upstream piping of a thermal relief pressure safety valve. Investigation into what caused the pin to back out is ongoing. There was no impact to water and the pump station was immediately shut down upon confirmed discovery of the release. 20230207 update: the root cause analysis concluded that the station discharge psv relieved below the setpoint while the pump station was still in operation. Product began to relieve to the sump via the relief line per design. This further caused the adjacent 1-inch psv branch piping to vibrate, forcing the bleed plug to back out of the needle valve.
Detailed record list
Report Received Date
2022-11-04 00:00:00
Iyear
2022
Report Number
20220249
Supplemental Number
37692
Report Type
Supplemental Final
Operator Id
Name
Tc Oil Pipeline Operations Inc
Operator Street Address
920 Memorial City Way Suite 800
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77024
Local Datetime
2022-10-05 05:50:00
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
6.5
Recovered Bbls
6.5
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Or Pack Calculations)
Incident Identified Datetime
2022-10-05 05:50:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2022-10-05 05:52:00
Restart Datetime
2022-10-07 18:20:00
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Initial Responder Com Datetime
2022-10-05 07:53:00
On Site Datetime
2022-10-05 05:28:00
Confirmed Discovery Datetime
2022-10-05 05:50:00
Nrc Rpt Datetime
2022-10-05 06:49:00
Nrc Rpt Num
Additional Nrc Report Numbers
1349232
Ignite Ind
No
Notify Qualified Indiv Ind
Yes
Qualified Indiv Notif Datetime
2022-10-05 06:02:00
Oil Spill Removal Org Ind
No
Num Pub Evacuated
0
Pipe Fac Name
David City Pump Station
Segment Name
Ks7
Onshore State Abbreviation
Ne
Onshore Postal Code
68632
Onshore City Name
Not Within A Municipality
Onshore County Name
Butler
Designated Location
Survey Station No.
Designated Name
David City Ps
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Relief Line And Relief Equipment
Installation Year
2022
Manufactured Year
2022
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Other
Leak Type Other
Bleed Plug Of The Needle Valve
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
642
Est Cost Prop Damage
24149
Est Cost Emergency
489133
Est Cost Environmental
0
Est Cost Other
0
Prpty
513924
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
1399
Mop Psig
1440
Mop Cfr Section
Internal Design Pressure �195.406(A)(1)
Maop Established Date
2009-12-13 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The controllers actions did not contribute to the release.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Malfunction Of Control/relief Equipment
Eq Failure Type
Malfunction Of Control/relief Equipment
Other Control Relief Ind
Yes
Other Control Relief Details
Bleed Plug Backed Out Of The Needle Valve On The Upstream Piping Of The Thermal Relief Psv Due To Vibration.
Additional Vibration Ind
Yes
Eqf Control Releaf Ind
Yes
Preparer Name
J*** B******
Preparer Title
Senior Compliance Specialist
Preparer Email
J***********@t*******.com
Preparer Telephone
5312137945
Preparer Fax
4024927491
Prepared Date
2023-02-10 00:00:00
Local Contact Name
J*** B******
Local Contact Email
J***********@t*******.com
Local Contact Telephone
5312137945
Authorizer Name
E*** H*****
Authorizer Telephone
4024907253
Authorizer Title
Senior Manager Regulatory Compliance
Authorizer Email
E**********@t*******.com
Narrative
6.5 barrels of product was released onto the facility piping and gravel pad at the david city pump station through a pin that had completely backed out of the bleed plug on the upstream piping of a thermal relief pressure safety valve. Investigation into what caused the pin to back out is ongoing. There was no impact to water and the pump station was immediately shut down upon confirmed discovery of the release. 20230207 update: the root cause analysis concluded that the station discharge psv relieved below the setpoint while the pump station was still in operation. Product began to relieve to the sump via the relief line per design. This further caused the adjacent 1-inch psv branch piping to vibrate, forcing the bleed plug to back out of the needle valve.
Report Received Date 2022-11-04 00:00:00
Iyear 2022
Report Number 20220249
Supplemental Number 37692
Report Type Supplemental Final
Operator Id 32334 PHMSA Enforcement
Name Tc Oil Pipeline Operations Inc
Operator Street Address 920 Memorial City Way Suite 800
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77024
Local Datetime 2022-10-05 05:50:00
Time Zone Central
Daylight Savings Ind Yes
Location Latitude 41.263886 Google Maps OpenStreetMap
Location Longitude -97.185326 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 6.5
Recovered Bbls 6.5
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Or Pack Calculations)
Incident Identified Datetime 2022-10-05 05:50:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Status When Identified Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind Yes
Shutdown Datetime 2022-10-05 05:52:00
Restart Datetime 2022-10-07 18:20:00
Communication State Fed Ind Yes
Party Initiated Communication Operator
Initial Responder Com Datetime 2022-10-05 07:53:00
On Site Datetime 2022-10-05 05:28:00
Confirmed Discovery Datetime 2022-10-05 05:50:00
Nrc Rpt Datetime 2022-10-05 06:49:00
Nrc Rpt Num 1349061 NRC Report How to search
Additional Nrc Report Numbers 1349232
Ignite Ind No
Notify Qualified Indiv Ind Yes
Qualified Indiv Notif Datetime 2022-10-05 06:02:00
Oil Spill Removal Org Ind No
Num Pub Evacuated 0
Pipe Fac Name David City Pump Station
Segment Name Ks7
Onshore State Abbreviation Ne
Onshore Postal Code 68632
Onshore City Name Not Within A Municipality
Onshore County Name Butler
Designated Location Survey Station No.
Designated Name David City Ps
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Relief Line And Relief Equipment
Installation Year 2022
Manufactured Year 2022
Material Involved Carbon Steel
Release Type Leak
Leak Type Other
Leak Type Other Bleed Plug Of The Needle Valve
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 642
Est Cost Prop Damage 24149
Est Cost Emergency 489133
Est Cost Environmental 0
Est Cost Other 0
Prpty 513924
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 1399
Mop Psig 1440
Mop Cfr Section Internal Design Pressure �195.406(A)(1) View CFR 49 §192
Maop Established Date 2009-12-13 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The controllers actions did not contribute to the release.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Malfunction Of Control/relief Equipment
Eq Failure Type Malfunction Of Control/relief Equipment
Other Control Relief Ind Yes
Other Control Relief Details Bleed Plug Backed Out Of The Needle Valve On The Upstream Piping Of The Thermal Relief Psv Due To Vibration.
Additional Vibration Ind Yes
Eqf Control Releaf Ind Yes
Preparer Name J*** B******
Preparer Title Senior Compliance Specialist
Preparer Email J***********@t*******.com
Preparer Telephone 5312137945
Preparer Fax 4024927491
Prepared Date 2023-02-10 00:00:00
Local Contact Name J*** B******
Local Contact Email J***********@t*******.com
Local Contact Telephone 5312137945
Authorizer Name E*** H*****
Authorizer Telephone 4024907253
Authorizer Title Senior Manager Regulatory Compliance
Authorizer Email E**********@t*******.com
Narrative 6.5 barrels of product was released onto the facility piping and gravel pad at the david city pump station through a pin that had completely backed out of the bleed plug on the upstream piping of a thermal relief pressure safety valve. Investigation into what caused the pin to back out is ongoing. There was no impact to water and the pump station was immediately shut down upon confirmed discovery of the release. 20230207 update: the root cause analysis concluded that the station discharge psv relieved below the setpoint while the pump station was still in operation. Product began to relieve to the sump via the relief line per design. This further caused the adjacent 1-inch psv branch piping to vibrate, forcing the bleed plug to back out of the needle valve.

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