HL incident on 2022-09-24 — TX

Operator
Denbury Gulf Coast Pipelines, Llc
Cause
Equipment Failure
Commodity
Co2 (Carbon Dioxide)
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$734
Incident datetime
2022-09-24 09:25
Report number
Location
TX
Narrative
On 9/24/2022 at 09:25, a denbury contractor arrived at mlv-02, observed a CO2 leak from the receiver facility and immediately notified denbury personnel of the leak. Danbury's district manager notified the denbury control center (dcc) of the leak at 09:47 and requested an emergency phone conference. The dcc did not receive an alarm or identify any loss of pressure or product from the location of the leak due to the small size of the leak. The dcc began closing upstream remote-control valves at 09:59. Downstream remote-control valves were left open to allow the downstream pump station to draw down line pressure. Denbury began conducting notifications to emergency response officials starting with louisiana state police (lasp) at 10:06, ascension parish emergency operations center (eoc) at 10:18, and iberville parish eoc at 10:22. The national response center (nrc) was notified at 10:33 (nrc #1348131). Denbury (non-contractor) personnel began arriving onsite at 11:50 and, upon verification that the location was safe, began closing the manual 24-inch isolation valve for the receiver at 12:13, which resulted in an immediate reduction in release volume. The valve was verified closed at 12:17 which isolated the receiver barrel. At 14:42 denbury began equalizing differential pressure across the system and at 16:35 on 9/24/2022 the system was returned to normal operation. On 9/28/2022 the receiver trap door o-ring was replaced, and the receiver was pressurized without incident.
Detailed record list
Report Received Date
2022-10-24 00:00:00
Iyear
2022
Report Number
20220241
Supplemental Number
37267
Report Type
Original
Operator Id
Name
Denbury Gulf Coast Pipelines, Llc
Operator Street Address
5851 Legacy Circle Suite 1200
Operator City Name
Plano
Operator State Abbreviation
TX
Operator Postal Code
75024
Local Datetime
2022-09-24 09:25:00
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Commodity Released Type
Co2 (Carbon Dioxide)
Unintentional Release Bbls
678
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2022-09-24 09:25:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2022-09-24 09:59:00
Restart Datetime
2022-09-24 16:35:00
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Initial Responder Com Datetime
2022-09-24 10:06:00
On Site Datetime
2022-09-24 11:50:00
Confirmed Discovery Datetime
2022-09-24 09:25:00
Nrc Rpt Datetime
2022-09-24 10:33:00
Nrc Rpt Num
Additional Nrc Report Numbers
1348291, 1348304
Ignite Ind
No
Upstream Action Taken
Valve Closure
Upstream Valve Close Datetime
2022-09-24 12:17:00
Upstream Valve Type Ind
Manual
Downstream Action Taken
Operational Control
Downstream Oprtnl Cntrl Detail
Downstream Mov Remained Open To Allow Downstream Pump Station To Drop Line Pressure
Num Pub Evacuated
0
Pipe Fac Name
Nejd Lateral
Segment Name
Nejd Lateral
Onshore State Abbreviation
La
Onshore Postal Code
70788
Onshore City Name
Not Within A Municipality
Onshore County Name
Iberville
Designated Location
Milepost
Designated Name
1.99
Federal
No
Location Type
Originated On Operator-Controlled Property, But Then Flowed Or Migrated Off The Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Scraper/pig Trap
Installation Year
2010
Manufactured Year
Unknown
Material Involved
Material Other Than Carbon Steel
Material Details
Trap Door O-Ring/seal
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
1324
Est Cost Prop Damage
734
Est Cost Emergency
2500
Est Cost Environmental
0
Est Cost Other
0
Prpty
4558
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
1400
Mop Psig
2220
Mop Cfr Section
Component Design Pressure �195.406(A)(2)
Maop Established Date
2009-06-07 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind
Yes
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
O-Ring
Eq Additional Other Ind
Yes
Eq Additional Other Details
Age - O-Ring Was In-Service With No Issues For Over 10-Years
Preparer Name
C*** D******
Preparer Title
Regulatory Compliance Specialist
Preparer Email
C***********@d******.com
Preparer Telephone
9722026691
Prepared Date
2022-10-24 00:00:00
Local Contact Name
J**** D****
Local Contact Email
J**********@d******.com
Local Contact Telephone
6015404808
Authorizer Name
D**** S*******
Authorizer Telephone
9726732038
Authorizer Title
Evp Chief Operating Officer
Authorizer Email
D*************@d******.com
Narrative
On 9/24/2022 at 09:25, a denbury contractor arrived at mlv-02, observed a CO2 leak from the receiver facility and immediately notified denbury personnel of the leak. Danbury's district manager notified the denbury control center (dcc) of the leak at 09:47 and requested an emergency phone conference. The dcc did not receive an alarm or identify any loss of pressure or product from the location of the leak due to the small size of the leak. The dcc began closing upstream remote-control valves at 09:59. Downstream remote-control valves were left open to allow the downstream pump station to draw down line pressure. Denbury began conducting notifications to emergency response officials starting with louisiana state police (lasp) at 10:06, ascension parish emergency operations center (eoc) at 10:18, and iberville parish eoc at 10:22. The national response center (nrc) was notified at 10:33 (nrc #1348131). Denbury (non-contractor) personnel began arriving onsite at 11:50 and, upon verification that the location was safe, began closing the manual 24-inch isolation valve for the receiver at 12:13, which resulted in an immediate reduction in release volume. The valve was verified closed at 12:17 which isolated the receiver barrel. At 14:42 denbury began equalizing differential pressure across the system and at 16:35 on 9/24/2022 the system was returned to normal operation. On 9/28/2022 the receiver trap door o-ring was replaced, and the receiver was pressurized without incident.
Report Received Date 2022-10-24 00:00:00
Iyear 2022
Report Number 20220241
Supplemental Number 37267
Report Type Original
Operator Id 32545 PHMSA Enforcement
Name Denbury Gulf Coast Pipelines, Llc
Operator Street Address 5851 Legacy Circle Suite 1200
Operator City Name Plano
Operator State Abbreviation TX
Operator Postal Code 75024
Local Datetime 2022-09-24 09:25:00
Time Zone Central
Daylight Savings Ind Yes
Location Latitude 30.113468 Google Maps OpenStreetMap
Location Longitude -91.098478 Google Maps OpenStreetMap
Commodity Released Type Co2 (Carbon Dioxide)
Unintentional Release Bbls 678
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2022-09-24 09:25:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Status When Identified Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind Yes
Shutdown Datetime 2022-09-24 09:59:00
Restart Datetime 2022-09-24 16:35:00
Communication State Fed Ind Yes
Party Initiated Communication Operator
Initial Responder Com Datetime 2022-09-24 10:06:00
On Site Datetime 2022-09-24 11:50:00
Confirmed Discovery Datetime 2022-09-24 09:25:00
Nrc Rpt Datetime 2022-09-24 10:33:00
Nrc Rpt Num 1348131 NRC Report How to search
Additional Nrc Report Numbers 1348291, 1348304
Ignite Ind No
Upstream Action Taken Valve Closure
Upstream Valve Close Datetime 2022-09-24 12:17:00
Upstream Valve Type Ind Manual
Downstream Action Taken Operational Control
Downstream Oprtnl Cntrl Detail Downstream Mov Remained Open To Allow Downstream Pump Station To Drop Line Pressure
Num Pub Evacuated 0
Pipe Fac Name Nejd Lateral
Segment Name Nejd Lateral
Onshore State Abbreviation La
Onshore Postal Code 70788
Onshore City Name Not Within A Municipality
Onshore County Name Iberville
Designated Location Milepost
Designated Name 1.99
Federal No
Location Type Originated On Operator-Controlled Property, But Then Flowed Or Migrated Off The Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Scraper/pig Trap
Installation Year 2010
Manufactured Year Unknown
Material Involved Material Other Than Carbon Steel
Material Details Trap Door O-Ring/seal
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 1324
Est Cost Prop Damage 734
Est Cost Emergency 2500
Est Cost Environmental 0
Est Cost Other 0
Prpty 4558
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 1400
Mop Psig 2220
Mop Cfr Section Component Design Pressure �195.406(A)(2) View CFR 49 §192
Maop Established Date 2009-06-07 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind Yes
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind O-Ring
Eq Additional Other Ind Yes
Eq Additional Other Details Age - O-Ring Was In-Service With No Issues For Over 10-Years
Preparer Name C*** D******
Preparer Title Regulatory Compliance Specialist
Preparer Email C***********@d******.com
Preparer Telephone 9722026691
Prepared Date 2022-10-24 00:00:00
Local Contact Name J**** D****
Local Contact Email J**********@d******.com
Local Contact Telephone 6015404808
Authorizer Name D**** S*******
Authorizer Telephone 9726732038
Authorizer Title Evp Chief Operating Officer
Authorizer Email D*************@d******.com
Narrative On 9/24/2022 at 09:25, a denbury contractor arrived at mlv-02, observed a CO2 leak from the receiver facility and immediately notified denbury personnel of the leak. Danbury's district manager notified the denbury control center (dcc) of the leak at 09:47 and requested an emergency phone conference. The dcc did not receive an alarm or identify any loss of pressure or product from the location of the leak due to the small size of the leak. The dcc began closing upstream remote-control valves at 09:59. Downstream remote-control valves were left open to allow the downstream pump station to draw down line pressure. Denbury began conducting notifications to emergency response officials starting with louisiana state police (lasp) at 10:06, ascension parish emergency operations center (eoc) at 10:18, and iberville parish eoc at 10:22. The national response center (nrc) was notified at 10:33 (nrc #1348131). Denbury (non-contractor) personnel began arriving onsite at 11:50 and, upon verification that the location was safe, began closing the manual 24-inch isolation valve for the receiver at 12:13, which resulted in an immediate reduction in release volume. The valve was verified closed at 12:17 which isolated the receiver barrel. At 14:42 denbury began equalizing differential pressure across the system and at 16:35 on 9/24/2022 the system was returned to normal operation. On 9/28/2022 the receiver trap door o-ring was replaced, and the receiver was pressurized without incident.

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