HL incident on 2022-08-23 — KS

Operator
Flint Hills Resources, Lc
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$21,850
Incident datetime
2022-08-23 10:30
Report number
Location
KS
Narrative
Update to section g. Results of the third party analysis indicate trap closure door o-ring seal failure due to rapid gas decompression . 08-23-22 - 10:30 - third party mowers in the area contact fhr operations to report a small ice ball at an fhr trap site. 08-23-22 - 12:28 - fhr operations personnel arrive on site and observe an ice ball formation on the trap door. 08-23-22 - 12:35 - fhr operations personnel verified the trap was isolated from the pipeline. 08-23-22 - 13:25 - trrc notification is made; incident report number 2691. 08-23-22 - 13:41 - pipeline isolated to prepare for replacement of the kicker valve on the trap. 08-23-22 - 16:00 - field repairs begin. 08-23-22 - 18:39 - trap door was replaced with blind flange and kicker valve on trap was also replaced. 08-23-22 - 20:30 - pipeline is placed back in service.
Detailed record list
Report Received Date
2022-09-21 00:00:00
Iyear
2022
Report Number
20220217
Supplemental Number
37346
Report Type
Supplemental Final
Operator Id
Name
Flint Hills Resources, Lc
Operator Street Address
4111 East 37th Street North
Operator City Name
Wichita
Operator State Abbreviation
KS
Operator Postal Code
67220
Local Datetime
2022-08-23 10:30:00
Time Zone
Central
Daylight Savings Ind
No
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Other Hvl
Commodity Details
Propylene
Unintentional Release Bbls
2.13
Intentional Release Bbls
0.87
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Public
Incident Identified Datetime
2022-08-23 10:30:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2022-08-23 13:41:00
Restart Datetime
2022-08-23 20:30:00
Communication State Fed Ind
No
On Site Datetime
2022-08-23 12:28:00
Confirmed Discovery Datetime
2022-08-23 12:28:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Upstream Action Taken
Valve Closure
Upstream Valve Close Datetime
2022-08-23 13:41:00
Upstream Valve Type Ind
Remotely Controlled
Downstream Action Taken
Valve Closure
Downstream Vlv Close Datetime
2022-08-23 13:41:00
Downstream Valve Type Ind
Remotely Controlled
Num Pub Evacuated
0
Pipe Fac Name
Longview 604 P/l
Segment Name
80160400
Onshore State Abbreviation
Tx
Onshore Postal Code
77612
Onshore City Name
Buna
Onshore County Name
Jasper
Designated Location
Survey Station No.
Designated Name
970+60
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Scraper/pig Trap
Installation Year
2020
Manufactured Year
2020
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
9500
Est Cost Gas Released
313
Est Cost Prop Damage
21850
Est Cost Emergency
4980
Est Cost Environmental
0
Est Cost Other
0
Prpty
36643
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
250
Mop Psig
1440
Mop Cfr Section
Subpart E Pressure Test �195.406(A)(3)
Maop Established Date
2020-11-22 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
25
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Other Equipment Failure
Eq Failure Type
Other Equipment Failure
Failure Details
Trap Closure Door O-Ring Seal Failure
Eq Additional Other Ind
Yes
Eq Additional Other Details
Analysis Indicated O-Ring Seal Failure Due To Rapid Gas Decompression
Preparer Name
M**** T*****
Preparer Title
Senior Compliance Specialist
Preparer Email
M***********@f**.com
Preparer Telephone
409-273-9482
Prepared Date
2022-11-10 00:00:00
Local Contact Name
M**** T*****
Local Contact Email
M***********@f**.com
Local Contact Telephone
409-273-9482
Authorizer Name
M**** T*****
Authorizer Telephone
409-273-9482
Authorizer Title
Senior Compliance Specialist
Authorizer Email
M***********@f**.com
Narrative
Update to section g. Results of the third party analysis indicate trap closure door o-ring seal failure due to rapid gas decompression . 08-23-22 - 10:30 - third party mowers in the area contact fhr operations to report a small ice ball at an fhr trap site. 08-23-22 - 12:28 - fhr operations personnel arrive on site and observe an ice ball formation on the trap door. 08-23-22 - 12:35 - fhr operations personnel verified the trap was isolated from the pipeline. 08-23-22 - 13:25 - trrc notification is made; incident report number 2691. 08-23-22 - 13:41 - pipeline isolated to prepare for replacement of the kicker valve on the trap. 08-23-22 - 16:00 - field repairs begin. 08-23-22 - 18:39 - trap door was replaced with blind flange and kicker valve on trap was also replaced. 08-23-22 - 20:30 - pipeline is placed back in service.
Report Received Date 2022-09-21 00:00:00
Iyear 2022
Report Number 20220217
Supplemental Number 37346
Report Type Supplemental Final
Operator Id 22855 PHMSA Enforcement
Name Flint Hills Resources, Lc
Operator Street Address 4111 East 37th Street North
Operator City Name Wichita
Operator State Abbreviation KS
Operator Postal Code 67220
Local Datetime 2022-08-23 10:30:00
Time Zone Central
Daylight Savings Ind No
Location Latitude 30.38834 Google Maps OpenStreetMap
Location Longitude -93.98541 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Other Hvl
Commodity Details Propylene
Unintentional Release Bbls 2.13
Intentional Release Bbls 0.87
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Notification From Public
Incident Identified Datetime 2022-08-23 10:30:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Status When Identified Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind Yes
Shutdown Datetime 2022-08-23 13:41:00
Restart Datetime 2022-08-23 20:30:00
Communication State Fed Ind No
On Site Datetime 2022-08-23 12:28:00
Confirmed Discovery Datetime 2022-08-23 12:28:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Upstream Action Taken Valve Closure
Upstream Valve Close Datetime 2022-08-23 13:41:00
Upstream Valve Type Ind Remotely Controlled
Downstream Action Taken Valve Closure
Downstream Vlv Close Datetime 2022-08-23 13:41:00
Downstream Valve Type Ind Remotely Controlled
Num Pub Evacuated 0
Pipe Fac Name Longview 604 P/l
Segment Name 80160400
Onshore State Abbreviation Tx
Onshore Postal Code 77612
Onshore City Name Buna
Onshore County Name Jasper
Designated Location Survey Station No.
Designated Name 970+60
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Scraper/pig Trap
Installation Year 2020
Manufactured Year 2020
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 9500
Est Cost Gas Released 313
Est Cost Prop Damage 21850
Est Cost Emergency 4980
Est Cost Environmental 0
Est Cost Other 0
Prpty 36643
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 250
Mop Psig 1440
Mop Cfr Section Subpart E Pressure Test �195.406(A)(3) View CFR 49 §192
Maop Established Date 2020-11-22 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 25
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Other Equipment Failure
Eq Failure Type Other Equipment Failure
Failure Details Trap Closure Door O-Ring Seal Failure
Eq Additional Other Ind Yes
Eq Additional Other Details Analysis Indicated O-Ring Seal Failure Due To Rapid Gas Decompression
Preparer Name M**** T*****
Preparer Title Senior Compliance Specialist
Preparer Email M***********@f**.com
Preparer Telephone 409-273-9482
Prepared Date 2022-11-10 00:00:00
Local Contact Name M**** T*****
Local Contact Email M***********@f**.com
Local Contact Telephone 409-273-9482
Authorizer Name M**** T*****
Authorizer Telephone 409-273-9482
Authorizer Title Senior Compliance Specialist
Authorizer Email M***********@f**.com
Narrative Update to section g. Results of the third party analysis indicate trap closure door o-ring seal failure due to rapid gas decompression . 08-23-22 - 10:30 - third party mowers in the area contact fhr operations to report a small ice ball at an fhr trap site. 08-23-22 - 12:28 - fhr operations personnel arrive on site and observe an ice ball formation on the trap door. 08-23-22 - 12:35 - fhr operations personnel verified the trap was isolated from the pipeline. 08-23-22 - 13:25 - trrc notification is made; incident report number 2691. 08-23-22 - 13:41 - pipeline isolated to prepare for replacement of the kicker valve on the trap. 08-23-22 - 16:00 - field repairs begin. 08-23-22 - 18:39 - trap door was replaced with blind flange and kicker valve on trap was also replaced. 08-23-22 - 20:30 - pipeline is placed back in service.

All rights reserved. Copyright © by ClearPHMSA