HL incident on 2022-08-17 — TX

Operator
Enterprise Products Operating Llc
Cause
Incorrect Operation
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2022-08-17 07:05
Report number
Location
TX
Narrative
On 8/17/22, at 7:05 am, contractors notified enterprise of a leak inside the channel meter station. At 07:15 am, enterprise personnel arrived on site and confirmed the leak was on the channel 8" line. At 08:05 am, the emergency response team arrived with the required personal protective equipment needed to enter the site. At 08:15 am, the leak source was identified to be a pressure gauge on piping installed for the ili assessment. A valve upstream was closed, ending the release. The pressure gauge was removed and replaced with a plug. At 07:50 am, enterprise determined the leak volume exceeded 5 gallons and notified the trrc at 08:29 am, incident report number 2685. Nrc reporting criteria was not met. Investigation of the failure concluded that the pressure gauge had a lower pressure scale range than the pipeline's operating pressure. The pressure gauge failed upon exceedance of its top range of 600 psig. The contractor did not conduct a drug or alcohol test as the pressure gauge was installed 38 hours prior to the accident.
Detailed record list
Report Received Date
2022-09-16 00:00:00
Iyear
2022
Report Number
20220214
Supplemental Number
37232
Report Type
Supplemental Final
Operator Id
Name
Enterprise Products Operating Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2022-08-17 07:05:00
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Other Hvl
Commodity Details
Propylene
Unintentional Release Bbls
3.54
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2022-08-17 07:05:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
No
Shutdown Explain
Leak Was Isolated Without Shutting Down The Pipeline.
Communication State Fed Ind
No
On Site Datetime
2022-08-17 07:15:00
Confirmed Discovery Datetime
2022-08-17 07:15:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Channel 8"
Segment Name
32694
Onshore State Abbreviation
Tx
Onshore Postal Code
77571
Onshore City Name
La Porte
Onshore County Name
Harris
Designated Location
Milepost
Designated Name
5.1
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Other
Item Involved Details
Pressure Gauge
Installation Year
Unknown
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Other
Leak Type Other
Pressure Gauge Failed
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
160
Est Cost Prop Damage
0
Est Cost Emergency
4200
Est Cost Environmental
0
Est Cost Other
0
Prpty
4360
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
605
Mop Psig
1440
Mop Cfr Section
Component Design Pressure �195.406(A)(2)
Maop Established Date
1982-12-30 00:00:00
Maop Reversal Flow Ind
Bi-Directional
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The leak occurred on a pressure gauge.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Wrong Equipment Specified Or Installed
Operation Type
Wrong Equipment Specified Or Installed
Related Failure Follow Ind
Yes
Category Type
Routine Maintenance
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Io Equipment Overpressure Ind
Yes
Preparer Name
M****** G*****
Preparer Title
Pipeline Compliance Engineer
Preparer Email
M******@e****.com
Preparer Telephone
713-381-4637
Prepared Date
2022-10-17 00:00:00
Authorizer Name
N*** T*****
Authorizer Telephone
713-381-2493
Authorizer Title
Compliance Senior Manager
Authorizer Email
N*******@e****.com
Narrative
On 8/17/22, at 7:05 am, contractors notified enterprise of a leak inside the channel meter station. At 07:15 am, enterprise personnel arrived on site and confirmed the leak was on the channel 8" line. At 08:05 am, the emergency response team arrived with the required personal protective equipment needed to enter the site. At 08:15 am, the leak source was identified to be a pressure gauge on piping installed for the ili assessment. A valve upstream was closed, ending the release. The pressure gauge was removed and replaced with a plug. At 07:50 am, enterprise determined the leak volume exceeded 5 gallons and notified the trrc at 08:29 am, incident report number 2685. Nrc reporting criteria was not met. Investigation of the failure concluded that the pressure gauge had a lower pressure scale range than the pipeline's operating pressure. The pressure gauge failed upon exceedance of its top range of 600 psig. The contractor did not conduct a drug or alcohol test as the pressure gauge was installed 38 hours prior to the accident.
Report Received Date 2022-09-16 00:00:00
Iyear 2022
Report Number 20220214
Supplemental Number 37232
Report Type Supplemental Final
Operator Id 31618 PHMSA Enforcement
Name Enterprise Products Operating Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2022-08-17 07:05:00
Time Zone Central
Daylight Savings Ind Yes
Location Latitude 29.689564 Google Maps OpenStreetMap
Location Longitude -95.057092 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Other Hvl
Commodity Details Propylene
Unintentional Release Bbls 3.54
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2022-08-17 07:05:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Status When Identified Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind No
Shutdown Explain Leak Was Isolated Without Shutting Down The Pipeline.
Communication State Fed Ind No
On Site Datetime 2022-08-17 07:15:00
Confirmed Discovery Datetime 2022-08-17 07:15:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Num Pub Evacuated 0
Pipe Fac Name Channel 8"
Segment Name 32694
Onshore State Abbreviation Tx
Onshore Postal Code 77571
Onshore City Name La Porte
Onshore County Name Harris
Designated Location Milepost
Designated Name 5.1
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Other
Item Involved Details Pressure Gauge
Installation Year Unknown
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Other
Leak Type Other Pressure Gauge Failed
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 160
Est Cost Prop Damage 0
Est Cost Emergency 4200
Est Cost Environmental 0
Est Cost Other 0
Prpty 4360
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 605
Mop Psig 1440
Mop Cfr Section Component Design Pressure �195.406(A)(2) View CFR 49 §192
Maop Established Date 1982-12-30 00:00:00
Maop Reversal Flow Ind Bi-Directional
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The leak occurred on a pressure gauge.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Wrong Equipment Specified Or Installed
Operation Type Wrong Equipment Specified Or Installed
Related Failure Follow Ind Yes
Category Type Routine Maintenance
Operator Qualification Ind Yes
Qualified Individuals Yes, They Were Qualified For The Task(S)
Io Equipment Overpressure Ind Yes
Preparer Name M****** G*****
Preparer Title Pipeline Compliance Engineer
Preparer Email M******@e****.com
Preparer Telephone 713-381-4637
Prepared Date 2022-10-17 00:00:00
Authorizer Name N*** T*****
Authorizer Telephone 713-381-2493
Authorizer Title Compliance Senior Manager
Authorizer Email N*******@e****.com
Narrative On 8/17/22, at 7:05 am, contractors notified enterprise of a leak inside the channel meter station. At 07:15 am, enterprise personnel arrived on site and confirmed the leak was on the channel 8" line. At 08:05 am, the emergency response team arrived with the required personal protective equipment needed to enter the site. At 08:15 am, the leak source was identified to be a pressure gauge on piping installed for the ili assessment. A valve upstream was closed, ending the release. The pressure gauge was removed and replaced with a plug. At 07:50 am, enterprise determined the leak volume exceeded 5 gallons and notified the trrc at 08:29 am, incident report number 2685. Nrc reporting criteria was not met. Investigation of the failure concluded that the pressure gauge had a lower pressure scale range than the pipeline's operating pressure. The pressure gauge failed upon exceedance of its top range of 600 psig. The contractor did not conduct a drug or alcohol test as the pressure gauge was installed 38 hours prior to the accident.

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