HL incident on 2022-08-11 — TX

Operator
Shell Pipeline Co., L.p.
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$25,000
Incident datetime
2022-08-11 09:50
Report number
Location
TX
Narrative
An operator was making a routine round and checking the station, he noticed a leak coming from a gasket on some above-ground piping. After further investigation, it was determined to that the line needed to be shut down, and orsos called for clean-up. The crude was cleaned up and the line was put back into service. The source of the leak was a failed gasket.
Detailed record list
Report Received Date
2022-09-06 00:00:00
Iyear
2022
Report Number
20220204
Supplemental Number
37081
Report Type
Original Final
Operator Id
Name
Shell Pipeline Co., L.p.
Operator Street Address
150 North Dairy Ashford Road Wck Bldg. A
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77079
Local Datetime
2022-08-11 09:50:00
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
2
Recovered Bbls
2
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Ground Patrol By Operator Or Its Contractor
Operator Type
Operator Employee
Incident Identified Datetime
2022-08-11 09:50:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2022-08-11 10:00:00
Restart Datetime
2022-08-12 21:00:00
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Initial Responder Com Datetime
2022-08-11 10:38:00
On Site Datetime
2022-08-11 09:45:00
Confirmed Discovery Datetime
2022-08-11 09:48:00
Nrc Rpt Datetime
2022-08-11 11:49:00
Nrc Rpt Num
Ignite Ind
No
Notify Qualified Indiv Ind
Yes
Qualified Indiv Notif Datetime
2022-08-11 10:00:00
Oil Spill Removal Org Ind
Yes
Osro Activated Datetime
2022-08-11 10:10:00
Osro Arrived On Site Dt
8/11/2022 11:30
Num Pub Evacuated
0
Pipe Fac Name
Fourchon Booster Station
Segment Name
Fourchon Booster Station
Onshore State Abbreviation
La
Onshore Postal Code
70357
Onshore City Name
Golden Meadow
Onshore County Name
Lafourche
Designated Location
Milepost
Designated Name
Booster
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Flange Assembly
Installation Year
1998
Manufactured Year
1998
Material Involved
Material Other Than Carbon Steel
Material Details
Insulating Laminate
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
200
Est Cost Prop Damage
25000
Est Cost Emergency
75600
Est Cost Environmental
45000
Est Cost Other
0
Prpty
145800
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
375
Mop Psig
1800
Mop Cfr Section
Subpart E Pressure Test �195.406(A)(3)
Maop Established Date
1999-04-01 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The leak detection system functioned per design. The leak was not large enough to set off the setpoints of the leak detection system. Controllers responded appropriately to depressurize and isolate the system after being notified by a local technician.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
Gasket
Additional Erosion Wear Ind
Yes
Preparer Name
J***** H*****
Preparer Title
Operations Support Coordinator
Preparer Email
J************@s****.com
Preparer Telephone
4095402781
Prepared Date
2022-08-15 00:00:00
Local Contact Name
J***** H*****
Local Contact Email
J************@s****.com
Local Contact Telephone
4095402781
Authorizer Name
D****** P****
Authorizer Telephone
832-762-2553
Authorizer Title
Integrity And Regulatory Services Manager
Authorizer Email
D************@s****.com
Narrative
An operator was making a routine round and checking the station, he noticed a leak coming from a gasket on some above-ground piping. After further investigation, it was determined to that the line needed to be shut down, and orsos called for clean-up. The crude was cleaned up and the line was put back into service. The source of the leak was a failed gasket.
Report Received Date 2022-09-06 00:00:00
Iyear 2022
Report Number 20220204
Supplemental Number 37081
Report Type Original Final
Operator Id 31174 PHMSA Enforcement
Name Shell Pipeline Co., L.p.
Operator Street Address 150 North Dairy Ashford Road Wck Bldg. A
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77079
Local Datetime 2022-08-11 09:50:00
Time Zone Central
Daylight Savings Ind Yes
Location Latitude 29.157002 Google Maps OpenStreetMap
Location Longitude -90.174509 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 2
Recovered Bbls 2
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Ground Patrol By Operator Or Its Contractor
Operator Type Operator Employee
Incident Identified Datetime 2022-08-11 09:50:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Status When Identified Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind Yes
Shutdown Datetime 2022-08-11 10:00:00
Restart Datetime 2022-08-12 21:00:00
Communication State Fed Ind Yes
Party Initiated Communication Operator
Initial Responder Com Datetime 2022-08-11 10:38:00
On Site Datetime 2022-08-11 09:45:00
Confirmed Discovery Datetime 2022-08-11 09:48:00
Nrc Rpt Datetime 2022-08-11 11:49:00
Nrc Rpt Num 1344182 NRC Report How to search
Ignite Ind No
Notify Qualified Indiv Ind Yes
Qualified Indiv Notif Datetime 2022-08-11 10:00:00
Oil Spill Removal Org Ind Yes
Osro Activated Datetime 2022-08-11 10:10:00
Osro Arrived On Site Dt 8/11/2022 11:30
Num Pub Evacuated 0
Pipe Fac Name Fourchon Booster Station
Segment Name Fourchon Booster Station
Onshore State Abbreviation La
Onshore Postal Code 70357
Onshore City Name Golden Meadow
Onshore County Name Lafourche
Designated Location Milepost
Designated Name Booster
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Flange Assembly
Installation Year 1998
Manufactured Year 1998
Material Involved Material Other Than Carbon Steel
Material Details Insulating Laminate
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 200
Est Cost Prop Damage 25000
Est Cost Emergency 75600
Est Cost Environmental 45000
Est Cost Other 0
Prpty 145800
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 375
Mop Psig 1800
Mop Cfr Section Subpart E Pressure Test �195.406(A)(3) View CFR 49 §192
Maop Established Date 1999-04-01 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The leak detection system functioned per design. The leak was not large enough to set off the setpoints of the leak detection system. Controllers responded appropriately to depressurize and isolate the system after being notified by a local technician.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind Gasket
Additional Erosion Wear Ind Yes
Preparer Name J***** H*****
Preparer Title Operations Support Coordinator
Preparer Email J************@s****.com
Preparer Telephone 4095402781
Prepared Date 2022-08-15 00:00:00
Local Contact Name J***** H*****
Local Contact Email J************@s****.com
Local Contact Telephone 4095402781
Authorizer Name D****** P****
Authorizer Telephone 832-762-2553
Authorizer Title Integrity And Regulatory Services Manager
Authorizer Email D************@s****.com
Narrative An operator was making a routine round and checking the station, he noticed a leak coming from a gasket on some above-ground piping. After further investigation, it was determined to that the line needed to be shut down, and orsos called for clean-up. The crude was cleaned up and the line was put back into service. The source of the leak was a failed gasket.

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