HL incident on 2022-08-05 — GA

Operator
Colonial Pipeline Co
Cause
Incorrect Operation
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$140,000
Incident datetime
2022-08-05 15:25
Report number
Location
GA
Narrative
On 8/3/2022 tank 837 at greensboro junction experienced a communication issue resulting in the loss of the saab (radar gauging system for the tank). A required reading was issued to local operations on august 2020, which made approval from leadership mandatory to receive product into a tank with a standing communication error. On 8/5/2022 the local operator on shift was preparing for a batch change during line 01 receiving and switched into tank 837 without leadership approval. The operator misread that tank had 9,000 bbls of product when in reality it had 9,000 bbls of available space to the safe fill level. At 15:10 gasoline reached the overflow ports and an estimate of 2.5 bbls was released down the side of the tank. The max fill alarm was never received. Local operations responded immediately in coordination with local first responders. The operator was removed from the desk, and his oq qualifications were revoked. Contractors remained on site to complete additional soil delineation. The max-fill alarm, as well as the saab head have been replaced.
Detailed record list
Report Received Date
2022-09-02 00:00:00
Iyear
2022
Report Number
20220202
Supplemental Number
37277
Report Type
Supplemental Final
Operator Id
Name
Colonial Pipeline Co
Operator Street Address
1000 Lake St.
Operator City Name
Alpharetta
Operator State Abbreviation
GA
Operator Postal Code
30009
Local Datetime
2022-08-05 15:10:00
Time Zone
Eastern
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
-79.93686505
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
2.5
Recovered Bbls
0.1
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2022-08-05 15:25:00
System Part Involved
Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
No
Shutdown Explain
Incident Isolated To Tank.
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Initial Responder Com Datetime
2022-08-05 15:49:00
On Site Datetime
2022-08-05 15:25:00
Confirmed Discovery Datetime
2022-08-05 15:25:00
Nrc Rpt Datetime
2022-08-05 16:36:00
Nrc Rpt Num
Additional Nrc Report Numbers
1343702
Ignite Ind
No
Notify Qualified Indiv Ind
No
Oil Spill Removal Org Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Greensboro Junction
Segment Name
Greensboro Junction
Onshore State Abbreviation
Nc
Onshore Postal Code
27409
Onshore City Name
Greensboro
Onshore County Name
Guilford
Designated Location
Survey Station No.
Designated Name
1012
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Tank, Including Attached Appurtenances
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Tank/vessel
Tank Vessel Subtype
Other
Tank Vessel Details
Overflow Vents.
Tank Type
Atmospheric
Safe Fill Level
41.1
Safe Fill Level Exceeded Ind
Yes
Api Std Out Of Service Year
2006
Api Std In Service Year
2019
Installation Year
1963
Manufactured Year
1963
Material Involved
Carbon Steel
Release Type
Overfill Or Overflow
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
317
Est Cost Prop Damage
140000
Est Cost Emergency
65300
Est Cost Environmental
325000
Est Cost Other
0
Prpty
530617
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
0
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind
Yes
Invest Incorrect Action Ind
Yes
Employee Drug Test Ind
Yes
Contractor Drug Test Ind
No
Num Employees Tested
1
Num Employees Failed
0
Cause
Incorrect Operation
Cause Details
Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Operation Type
Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Overflow Other Ind
Incorrect Reference Data/calculation
Related Failure Follow Ind
Yes
Category Type
Normal Operating Conditions
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Eqf Control Releaf Ind
Yes
Preparer Name
D***** L******
Preparer Title
Compliance Coordinator
Preparer Email
D*******@c******.com
Preparer Telephone
4438211456
Prepared Date
2022-10-25 00:00:00
Authorizer Name
Q****** F******
Authorizer Telephone
6787622270
Authorizer Title
Director Pipeline Compliance
Authorizer Email
Q*******@c******.com
Narrative
On 8/3/2022 tank 837 at greensboro junction experienced a communication issue resulting in the loss of the saab (radar gauging system for the tank). A required reading was issued to local operations on august 2020, which made approval from leadership mandatory to receive product into a tank with a standing communication error. On 8/5/2022 the local operator on shift was preparing for a batch change during line 01 receiving and switched into tank 837 without leadership approval. The operator misread that tank had 9,000 bbls of product when in reality it had 9,000 bbls of available space to the safe fill level. At 15:10 gasoline reached the overflow ports and an estimate of 2.5 bbls was released down the side of the tank. The max fill alarm was never received. Local operations responded immediately in coordination with local first responders. The operator was removed from the desk, and his oq qualifications were revoked. Contractors remained on site to complete additional soil delineation. The max-fill alarm, as well as the saab head have been replaced.
Report Received Date 2022-09-02 00:00:00
Iyear 2022
Report Number 20220202
Supplemental Number 37277
Report Type Supplemental Final
Operator Id 2552 PHMSA Enforcement
Name Colonial Pipeline Co
Operator Street Address 1000 Lake St.
Operator City Name Alpharetta
Operator State Abbreviation GA
Operator Postal Code 30009
Local Datetime 2022-08-05 15:10:00
Time Zone Eastern
Daylight Savings Ind Yes
Location Latitude 36.07123064 Google Maps OpenStreetMap
Location Longitude -79.93686505 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 2.5
Recovered Bbls 0.1
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2022-08-05 15:25:00
System Part Involved Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore Onshore
Status When Identified Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind No
Shutdown Explain Incident Isolated To Tank.
Communication State Fed Ind Yes
Party Initiated Communication Operator
Initial Responder Com Datetime 2022-08-05 15:49:00
On Site Datetime 2022-08-05 15:25:00
Confirmed Discovery Datetime 2022-08-05 15:25:00
Nrc Rpt Datetime 2022-08-05 16:36:00
Nrc Rpt Num 1343659 NRC Report How to search
Additional Nrc Report Numbers 1343702
Ignite Ind No
Notify Qualified Indiv Ind No
Oil Spill Removal Org Ind No
Num Pub Evacuated 0
Pipe Fac Name Greensboro Junction
Segment Name Greensboro Junction
Onshore State Abbreviation Nc
Onshore Postal Code 27409
Onshore City Name Greensboro
Onshore County Name Guilford
Designated Location Survey Station No.
Designated Name 1012
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Tank, Including Attached Appurtenances
Crossing No
Pipe Facility Type Interstate
Item Involved Tank/vessel
Tank Vessel Subtype Other
Tank Vessel Details Overflow Vents.
Tank Type Atmospheric
Safe Fill Level 41.1
Safe Fill Level Exceeded Ind Yes
Api Std Out Of Service Year 2006
Api Std In Service Year 2019
Installation Year 1963
Manufactured Year 1963
Material Involved Carbon Steel
Release Type Overfill Or Overflow
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 317
Est Cost Prop Damage 140000
Est Cost Emergency 65300
Est Cost Environmental 325000
Est Cost Other 0
Prpty 530617
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 0
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind Yes
Invest Incorrect Action Ind Yes
Employee Drug Test Ind Yes
Contractor Drug Test Ind No
Num Employees Tested 1
Num Employees Failed 0
Cause Incorrect Operation
Cause Details Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Operation Type Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Overflow Other Ind Incorrect Reference Data/calculation
Related Failure Follow Ind Yes
Category Type Normal Operating Conditions
Operator Qualification Ind Yes
Qualified Individuals Yes, They Were Qualified For The Task(S)
Eqf Control Releaf Ind Yes
Preparer Name D***** L******
Preparer Title Compliance Coordinator
Preparer Email D*******@c******.com
Preparer Telephone 4438211456
Prepared Date 2022-10-25 00:00:00
Authorizer Name Q****** F******
Authorizer Telephone 6787622270
Authorizer Title Director Pipeline Compliance
Authorizer Email Q*******@c******.com
Narrative On 8/3/2022 tank 837 at greensboro junction experienced a communication issue resulting in the loss of the saab (radar gauging system for the tank). A required reading was issued to local operations on august 2020, which made approval from leadership mandatory to receive product into a tank with a standing communication error. On 8/5/2022 the local operator on shift was preparing for a batch change during line 01 receiving and switched into tank 837 without leadership approval. The operator misread that tank had 9,000 bbls of product when in reality it had 9,000 bbls of available space to the safe fill level. At 15:10 gasoline reached the overflow ports and an estimate of 2.5 bbls was released down the side of the tank. The max fill alarm was never received. Local operations responded immediately in coordination with local first responders. The operator was removed from the desk, and his oq qualifications were revoked. Contractors remained on site to complete additional soil delineation. The max-fill alarm, as well as the saab head have been replaced.

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