HL incident on 2022-07-31 — TX

Operator
Energy Transfer Nederland Terminal Llc
Cause
Incorrect Operation
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$50
Incident datetime
2022-07-31 08:00
Report number
Location
TX
Narrative
On 7/31/22 at approximately 07:45, during a tank switch involving a crude oil receipt local operator opened wrong valve causing a pressure spike (<110% of mop) at the texoma manifold, a-bank causing oil leakage from a bolted flange gasket. The pressure was relieved and controlled and the flange was checked and retorqued by a mechanic. The line was static pressure tested and checked for leaks. Subsequent to the successful static check the line was put back into service. A vacuum truck collected the oil/water mixture and disposed of it in the water recycling facility.
Detailed record list
Report Received Date
2022-08-26 00:00:00
Iyear
2022
Report Number
20220197
Supplemental Number
37038
Report Type
Original Final
Operator Id
Name
Energy Transfer Nederland Terminal Llc
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2022-07-31 07:45:00
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.64
Recovered Bbls
0.64
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2022-07-31 08:00:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
No
Shutdown Explain
Leak Area Was Isolated And Normal Operation Was Able To Continue
Communication State Fed Ind
No
On Site Datetime
2022-07-31 08:00:00
Confirmed Discovery Datetime
2022-07-31 08:00:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Notify Qualified Indiv Ind
No
Oil Spill Removal Org Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Nederland Terminal
Segment Name
Texoma Manifold
Onshore State Abbreviation
Tx
Onshore Postal Code
77627
Onshore City Name
Nederland
Onshore County Name
Jefferson
Designated Location
Survey Station No.
Designated Name
0+00
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Flange Assembly
Installation Year
Unknown
Manufactured Year
Unknown
Material Involved
Material Other Than Carbon Steel
Material Details
Gasket Material
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
70
Est Cost Prop Damage
50
Est Cost Emergency
1000
Est Cost Environmental
0
Est Cost Other
0
Prpty
1120
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
300
Mop Psig
285
Mop Cfr Section
Subpart E Pressure Test �195.406(A)(3)
Maop Established Date
2018-05-08 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Exceeded Mop, But Did Not Exceed 110% Of Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
A review of the accident determined that there were no control room actions that contributed to the event.
Employee Drug Test Ind
Yes
Contractor Drug Test Ind
No
Num Employees Tested
1
Num Employees Failed
0
Cause
Incorrect Operation
Cause Details
Pipeline Or Equipment Overpressured
Operation Type
Pipeline Or Equipment Overpressured
Related Failure Follow Ind
Yes
Category Type
Normal Operating Conditions
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
T*** N*******
Preparer Title
Director - Regulatory Compliance
Preparer Email
T************@e*************.com
Preparer Telephone
7139897126
Prepared Date
2022-08-26 00:00:00
Authorizer Name
T*** N*******
Authorizer Telephone
713-989-7126
Authorizer Title
Director - Regulatory Compliance
Authorizer Email
T************@e*************.com
Narrative
On 7/31/22 at approximately 07:45, during a tank switch involving a crude oil receipt local operator opened wrong valve causing a pressure spike (<110% of mop) at the texoma manifold, a-bank causing oil leakage from a bolted flange gasket. The pressure was relieved and controlled and the flange was checked and retorqued by a mechanic. The line was static pressure tested and checked for leaks. Subsequent to the successful static check the line was put back into service. A vacuum truck collected the oil/water mixture and disposed of it in the water recycling facility.
Report Received Date 2022-08-26 00:00:00
Iyear 2022
Report Number 20220197
Supplemental Number 37038
Report Type Original Final
Operator Id 39706 PHMSA Enforcement
Name Energy Transfer Nederland Terminal Llc
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2022-07-31 07:45:00
Time Zone Central
Daylight Savings Ind Yes
Location Latitude 29.99529 Google Maps OpenStreetMap
Location Longitude -93.99296 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.64
Recovered Bbls 0.64
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2022-07-31 08:00:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Status When Identified Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind No
Shutdown Explain Leak Area Was Isolated And Normal Operation Was Able To Continue
Communication State Fed Ind No
On Site Datetime 2022-07-31 08:00:00
Confirmed Discovery Datetime 2022-07-31 08:00:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Notify Qualified Indiv Ind No
Oil Spill Removal Org Ind No
Num Pub Evacuated 0
Pipe Fac Name Nederland Terminal
Segment Name Texoma Manifold
Onshore State Abbreviation Tx
Onshore Postal Code 77627
Onshore City Name Nederland
Onshore County Name Jefferson
Designated Location Survey Station No.
Designated Name 0+00
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Flange Assembly
Installation Year Unknown
Manufactured Year Unknown
Material Involved Material Other Than Carbon Steel
Material Details Gasket Material
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 70
Est Cost Prop Damage 50
Est Cost Emergency 1000
Est Cost Environmental 0
Est Cost Other 0
Prpty 1120
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 300
Mop Psig 285
Mop Cfr Section Subpart E Pressure Test �195.406(A)(3) View CFR 49 §192
Maop Established Date 2018-05-08 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Exceeded Mop, But Did Not Exceed 110% Of Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details A review of the accident determined that there were no control room actions that contributed to the event.
Employee Drug Test Ind Yes
Contractor Drug Test Ind No
Num Employees Tested 1
Num Employees Failed 0
Cause Incorrect Operation
Cause Details Pipeline Or Equipment Overpressured
Operation Type Pipeline Or Equipment Overpressured
Related Failure Follow Ind Yes
Category Type Normal Operating Conditions
Operator Qualification Ind Yes
Qualified Individuals Yes, They Were Qualified For The Task(S)
Preparer Name T*** N*******
Preparer Title Director - Regulatory Compliance
Preparer Email T************@e*************.com
Preparer Telephone 7139897126
Prepared Date 2022-08-26 00:00:00
Authorizer Name T*** N*******
Authorizer Telephone 713-989-7126
Authorizer Title Director - Regulatory Compliance
Authorizer Email T************@e*************.com
Narrative On 7/31/22 at approximately 07:45, during a tank switch involving a crude oil receipt local operator opened wrong valve causing a pressure spike (<110% of mop) at the texoma manifold, a-bank causing oil leakage from a bolted flange gasket. The pressure was relieved and controlled and the flange was checked and retorqued by a mechanic. The line was static pressure tested and checked for leaks. Subsequent to the successful static check the line was put back into service. A vacuum truck collected the oil/water mixture and disposed of it in the water recycling facility.

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