HL incident on 2022-07-21 — TX

Operator
Chevron Pipe Line Co
Cause
Other Outside Force Damage
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2022-07-21 14:20
Report number
Location
TX
Narrative
At approx. 1420 cdt on 21jul22, while conducting an overflight for the pipeline de-oiling operations of 12" south timbalier 130 pipeline, when a 75-ft by 150-ft, light silver sheen was discovered. It was estimated that less than 0.125 gallons of crude oil released to waters while flushing the pipeline before removal. The release was not recoverable naturally dissipated. At approx. 06:30 on 22jul22, divers began inspecting an area of the 12' south timbalier 130 pipeline near the location of the sheen observed on 21jul22 (nrc report #1342172). Divers discovered a buried section of the pipe approximately 150' south of where the pipe was wrapped around a former caisson. Divers hand jetted approximately 12' below natural bottom without finding the source. Decision was made to stop hand jetting for safety reasons and find round pipe upstream and downstream of the problem area to install slip on flanges to bypass the area. During this time, the divers noted the pipe was severed on the seafloor approximately 300' south of the former caisson (125' from the buried pipe). Before de-oiling operations resumed, slip on flanges were installed upstream (south of the sever) and downstream (north of the former caisson) of the area and the line was de-oiled in two separate operations. The pipeline has been inactive since hurricane ida and was de-oiled over the months of july and august 2022. This release is a continued effort to de-oil pipelines damaged in the gulf of mexico by hurricane ida. All pipelines have remained idle before ida to present activities. Chevron pipe line is continuing investigations into the cause of the severed pipeline.
Detailed record list
Report Received Date
2022-08-19 00:00:00
Iyear
2022
Report Number
20220186
Supplemental Number
37310
Report Type
Supplemental Final
Operator Id
Name
Chevron Pipe Line Co
Operator Street Address
1400 Smith Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2022-07-21 14:20:00
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.1
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Air Patrol
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2022-07-21 14:20:00
System Part Involved
Offshore Pipeline, Including Riser And Riser Bend
On Off Shore
Offshore
Status When Identified
Idle
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Initial Responder Com Datetime
2022-07-21 15:31:00
On Site Datetime
2022-07-21 14:20:00
Confirmed Discovery Datetime
2022-07-21 14:20:00
Nrc Rpt Datetime
2022-07-21 15:31:00
Nrc Rpt Num
Additional Nrc Report Numbers
1342324
Ignite Ind
No
Upstream Action Taken
Operational Control
Upstream Oprtnl Cntrl Detail
Pipeline Was Idle During Time Of Release And Was In The Process Of Being De-Oiled.
Downstream Action Taken
Operational Control
Downstream Oprtnl Cntrl Detail
Pipeline Was Idle During Time Of Release And Was In The Process Of Being De-Oiled.
Num Pub Evacuated
0
Pipe Fac Name
St130
Segment Name
Psc 3958
Off Water Depth
40
Off Accident Origin
In State Waters
Offshore State Abbreviation
La
Off Instate Area
Bm3
Off Instate Block
Bm3
Offshore County Name
Lafourche
Off Area Accident Type
Below Water, Pipe On Or Above Seabed
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Puddle Weld Ind
No
Pipe Diameter
12
Pipe Wall Thickness
0.5
Pipe Smys
35000
Pipe Specification
Unknown
Pipe Seam Type
Seamless
Pipe Manufacturer
Unknown
Pipe Coating Type
Other
Pipe Coating Details
Mastic
Coating Applied Ind
No
Installation Year
1971
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Other
Leak Type Other
Line Appears To Be Severed
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
Yes
Ocean Seawater Ind
Yes
Amount Released
0.1
Rel Water Name
Gulf Of Mexico
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
0
Est Cost Emergency
2000
Est Cost Environmental
0
Est Cost Other
0
Prpty
2000
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
0.5
Mop Psig
1400
Mop Cfr Section
Component Design Pressure �195.406(A)(2)
Maop Established Date
2017-03-23 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
No
Scada Functional Ind
No
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Line was idle for maintenance during time of release
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Other Outside Force Damage
Cause Details
Other Outside Force Damage
Outside Force Type
Other Outside Force Damage
Osf Other Details
Line's Integrity Was Compromised During Hurricane Ida. During Incident Response, A Diver From A Dsv Noted That The Line Was Flat In This Area And Wrapped Around The Caisson. Subsequent Survey Indicated That The Line Was Still Intact. It Is Chevron's Opinion That The Line Was Severed By An Unknown Source After The Survey Was Performed. Approximately 125' North Of The Sever There Are Indications That A Jackup Had Set Down On The Line.
Preparer Name
G****** S* P*****
Preparer Title
Senior Regulatory Coordinator
Preparer Email
P******@c******.com
Preparer Telephone
8328544596
Prepared Date
2022-11-03 00:00:00
Authorizer Name
G****** S* P*****
Authorizer Telephone
8328544596
Authorizer Title
Senior Regulatory Coordinator
Authorizer Email
P******@c******.com
Narrative
At approx. 1420 cdt on 21jul22, while conducting an overflight for the pipeline de-oiling operations of 12" south timbalier 130 pipeline, when a 75-ft by 150-ft, light silver sheen was discovered. It was estimated that less than 0.125 gallons of crude oil released to waters while flushing the pipeline before removal. The release was not recoverable naturally dissipated. At approx. 06:30 on 22jul22, divers began inspecting an area of the 12' south timbalier 130 pipeline near the location of the sheen observed on 21jul22 (nrc report #1342172). Divers discovered a buried section of the pipe approximately 150' south of where the pipe was wrapped around a former caisson. Divers hand jetted approximately 12' below natural bottom without finding the source. Decision was made to stop hand jetting for safety reasons and find round pipe upstream and downstream of the problem area to install slip on flanges to bypass the area. During this time, the divers noted the pipe was severed on the seafloor approximately 300' south of the former caisson (125' from the buried pipe). Before de-oiling operations resumed, slip on flanges were installed upstream (south of the sever) and downstream (north of the former caisson) of the area and the line was de-oiled in two separate operations. The pipeline has been inactive since hurricane ida and was de-oiled over the months of july and august 2022. This release is a continued effort to de-oil pipelines damaged in the gulf of mexico by hurricane ida. All pipelines have remained idle before ida to present activities. Chevron pipe line is continuing investigations into the cause of the severed pipeline.
Report Received Date 2022-08-19 00:00:00
Iyear 2022
Report Number 20220186
Supplemental Number 37310
Report Type Supplemental Final
Operator Id 2731 PHMSA Enforcement
Name Chevron Pipe Line Co
Operator Street Address 1400 Smith Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2022-07-21 14:20:00
Time Zone Central
Daylight Savings Ind Yes
Location Latitude 29.043667 Google Maps OpenStreetMap
Location Longitude -90.191667 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.1
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Air Patrol
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2022-07-21 14:20:00
System Part Involved Offshore Pipeline, Including Riser And Riser Bend
On Off Shore Offshore
Status When Identified Idle
Communication State Fed Ind Yes
Party Initiated Communication Operator
Initial Responder Com Datetime 2022-07-21 15:31:00
On Site Datetime 2022-07-21 14:20:00
Confirmed Discovery Datetime 2022-07-21 14:20:00
Nrc Rpt Datetime 2022-07-21 15:31:00
Nrc Rpt Num 1342172 NRC Report How to search
Additional Nrc Report Numbers 1342324
Ignite Ind No
Upstream Action Taken Operational Control
Upstream Oprtnl Cntrl Detail Pipeline Was Idle During Time Of Release And Was In The Process Of Being De-Oiled.
Downstream Action Taken Operational Control
Downstream Oprtnl Cntrl Detail Pipeline Was Idle During Time Of Release And Was In The Process Of Being De-Oiled.
Num Pub Evacuated 0
Pipe Fac Name St130
Segment Name Psc 3958
Off Water Depth 40
Off Accident Origin In State Waters
Offshore State Abbreviation La
Off Instate Area Bm3
Off Instate Block Bm3
Offshore County Name Lafourche
Off Area Accident Type Below Water, Pipe On Or Above Seabed
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Puddle Weld Ind No
Pipe Diameter 12
Pipe Wall Thickness 0.5
Pipe Smys 35000
Pipe Specification Unknown
Pipe Seam Type Seamless
Pipe Manufacturer Unknown
Pipe Coating Type Other
Pipe Coating Details Mastic
Coating Applied Ind No
Installation Year 1971
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Other
Leak Type Other Line Appears To Be Severed
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind Yes
Ocean Seawater Ind Yes
Amount Released 0.1
Rel Water Name Gulf Of Mexico
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 0
Est Cost Emergency 2000
Est Cost Environmental 0
Est Cost Other 0
Prpty 2000
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 0.5
Mop Psig 1400
Mop Cfr Section Component Design Pressure �195.406(A)(2) View CFR 49 §192
Maop Established Date 2017-03-23 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind No
Scada Functional Ind No
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Line was idle for maintenance during time of release
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Other Outside Force Damage
Cause Details Other Outside Force Damage
Outside Force Type Other Outside Force Damage
Osf Other Details Line's Integrity Was Compromised During Hurricane Ida. During Incident Response, A Diver From A Dsv Noted That The Line Was Flat In This Area And Wrapped Around The Caisson. Subsequent Survey Indicated That The Line Was Still Intact. It Is Chevron's Opinion That The Line Was Severed By An Unknown Source After The Survey Was Performed. Approximately 125' North Of The Sever There Are Indications That A Jackup Had Set Down On The Line.
Preparer Name G****** S* P*****
Preparer Title Senior Regulatory Coordinator
Preparer Email P******@c******.com
Preparer Telephone 8328544596
Prepared Date 2022-11-03 00:00:00
Authorizer Name G****** S* P*****
Authorizer Telephone 8328544596
Authorizer Title Senior Regulatory Coordinator
Authorizer Email P******@c******.com
Narrative At approx. 1420 cdt on 21jul22, while conducting an overflight for the pipeline de-oiling operations of 12" south timbalier 130 pipeline, when a 75-ft by 150-ft, light silver sheen was discovered. It was estimated that less than 0.125 gallons of crude oil released to waters while flushing the pipeline before removal. The release was not recoverable naturally dissipated. At approx. 06:30 on 22jul22, divers began inspecting an area of the 12' south timbalier 130 pipeline near the location of the sheen observed on 21jul22 (nrc report #1342172). Divers discovered a buried section of the pipe approximately 150' south of where the pipe was wrapped around a former caisson. Divers hand jetted approximately 12' below natural bottom without finding the source. Decision was made to stop hand jetting for safety reasons and find round pipe upstream and downstream of the problem area to install slip on flanges to bypass the area. During this time, the divers noted the pipe was severed on the seafloor approximately 300' south of the former caisson (125' from the buried pipe). Before de-oiling operations resumed, slip on flanges were installed upstream (south of the sever) and downstream (north of the former caisson) of the area and the line was de-oiled in two separate operations. The pipeline has been inactive since hurricane ida and was de-oiled over the months of july and august 2022. This release is a continued effort to de-oil pipelines damaged in the gulf of mexico by hurricane ida. All pipelines have remained idle before ida to present activities. Chevron pipe line is continuing investigations into the cause of the severed pipeline.

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