HL incident on 2022-07-19 — TX

Operator
Sunoco Pipeline L.p.
Cause
Miscellaneous Root Causes
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$200,000
Incident datetime
2022-07-19 18:08
Report number
Location
TX
Narrative
On 07/19/22 at 18:08, the control center received an initial line imbalance alarm. Controller made downstream adjustments to pumps believing that the alarm may be due to downstream suction. Controller then contacted alarm team which believed there could potentially be meter issues on the system. At 20:03, the controller shut down the line down and contacted field operations. At 20:40, the control center received a call from the landowner reporting a possible leak and the controller again contacted field operations to dispatch someone to the area to investigate. At 22:46, local operations personnel arrived onsite and confirmed a leak between alanreed and mcclellan pump stations and then proceeded to close valves to isolate the leak area. At 00:08 ct nrc was notified (report no. 1341998) due to anticipated total costs exceeding $50,000. Approximately 83 barrels of crude oil was released. Cleanup and repair crews were mobilized to begin remediation and repair efforts. It was determined that the landowner was cultivating the field earlier that day on 7/19/22 using a tractor with discs and struck the line causing the release. Measured depth at the strike was approximately 6-inches due to erosion. A plidco clamp was applied to control the release of crude oil while cleanup efforts continued. As a permanent repair and to address the shallow cover in this area to prevent a recurrence, approximately 120 feet of pipe was cut out and replaced and approximately 900 feet of the pipeline was lowered achieving approximately 36-40 inches of cover. The exposed pipeline is also being recoated. On 7/22/22 at approximately 12:30, the line was restarted. Supplemental report: part g accident cause updated to excavation damage by third party.
Detailed record list
Report Received Date
2022-08-18 00:00:00
Iyear
2022
Report Number
20220185
Supplemental Number
38301
Report Type
Supplemental Final
Operator Id
Name
Sunoco Pipeline L.p.
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2022-07-19 18:08:00
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
83
Recovered Bbls
83
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Cpm Leak Detection System
Incident Identified Datetime
2022-07-19 18:08:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2022-07-19 20:03:00
Restart Datetime
2022-07-22 12:30:00
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Initial Responder Com Datetime
2022-07-20 11:32:00
On Site Datetime
2022-07-19 22:46:00
Confirmed Discovery Datetime
2022-07-19 22:46:00
Nrc Rpt Datetime
2022-07-20 00:08:00
Nrc Rpt Num
Additional Nrc Report Numbers
1342167
Ignite Ind
No
Upstream Action Taken
Valve Closure
Upstream Valve Close Datetime
2022-07-19 22:30:00
Upstream Valve Type Ind
Manual
Downstream Action Taken
Valve Closure
Downstream Vlv Close Datetime
2022-07-19 23:13:00
Downstream Valve Type Ind
Manual
Notify Qualified Indiv Ind
Yes
Qualified Indiv Notif Datetime
2022-07-19 22:45:00
Oil Spill Removal Org Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Alanreed To Mcclellen
Segment Name
23002.08 - 8" Farm Rd 2477 Trap To Mcclellan
Onshore State Abbreviation
Tx
Onshore Postal Code
79002
Onshore City Name
Not Within Municipality
Onshore County Name
Gray
Designated Location
Survey Station No.
Designated Name
83172.2
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
6
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Body
Puddle Weld Ind
No
Pipe Diameter
8.625
Pipe Wall Thickness
0.322
Pipe Smys
30000
Pipe Specification
Api 5l Grade A
Pipe Seam Type
Lap Welded
Pipe Manufacturer
Unknown
Pipe Coating Type
None
Coating Applied Ind
No
Installation Year
1942
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Mechanical Puncture
Puncture Axial
3.9
Puncture Circum
3.6
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
7150
Est Cost Prop Damage
200000
Est Cost Emergency
100000
Est Cost Environmental
75000
Est Cost Other
0
Prpty
382150
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
295
Mop Psig
707
Mop Cfr Section
Subpart E Pressure Test �195.406(A)(3)
Maop Established Date
2016-03-15 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
44626
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
Yes
Cpm Conf Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind
Yes
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
Yes
Contractor Drug Test Ind
No
Num Employees Tested
1
Num Employees Failed
0
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
No
State Law Exempt Ind
Yes
State Law Exempt Type
Activity Is Exempt And Did Not Exceed The Limits Of The Exemption
State Law Exempt Authority
Texas Underground Facility Notification Corporation
State Law Exempt Criteria
Depth Exemption 16-Inch
Notify Cga Dirt
No
Private Row Ind
Yes
Private Subtype
Private Landowner
Joint Trench Ind
No
Cross Bore Ind
No
Depth Of Grade
< 18�
Excavator Type
Farmer
Excavator Equipment
Farm Equipment
Work Performed
Agriculture
One Call Notified Ind
No
Locator Type
Unknown/other
Visible Marks
No
Service Interruption
Yes
Service Interruption Hours
96
Root Cause Category
Miscellaneous Root Causes
Root Cause Type
Root Cause Not Listed (Comment Required)
Root Cause Type Other
Shallow Pipeline
Preparer Name
T*** N*******
Preparer Title
Director - Regulatory Compliance
Preparer Email
T************@e*************.com
Preparer Telephone
713-989-7126
Prepared Date
2023-07-21 00:00:00
Authorizer Name
T*** N*******
Authorizer Telephone
713-989-7126
Authorizer Title
Director - Regulatory Compliance
Authorizer Email
T************@e*************.com
Narrative
On 07/19/22 at 18:08, the control center received an initial line imbalance alarm. Controller made downstream adjustments to pumps believing that the alarm may be due to downstream suction. Controller then contacted alarm team which believed there could potentially be meter issues on the system. At 20:03, the controller shut down the line down and contacted field operations. At 20:40, the control center received a call from the landowner reporting a possible leak and the controller again contacted field operations to dispatch someone to the area to investigate. At 22:46, local operations personnel arrived onsite and confirmed a leak between alanreed and mcclellan pump stations and then proceeded to close valves to isolate the leak area. At 00:08 ct nrc was notified (report no. 1341998) due to anticipated total costs exceeding $50,000. Approximately 83 barrels of crude oil was released. Cleanup and repair crews were mobilized to begin remediation and repair efforts. It was determined that the landowner was cultivating the field earlier that day on 7/19/22 using a tractor with discs and struck the line causing the release. Measured depth at the strike was approximately 6-inches due to erosion. A plidco clamp was applied to control the release of crude oil while cleanup efforts continued. As a permanent repair and to address the shallow cover in this area to prevent a recurrence, approximately 120 feet of pipe was cut out and replaced and approximately 900 feet of the pipeline was lowered achieving approximately 36-40 inches of cover. The exposed pipeline is also being recoated. On 7/22/22 at approximately 12:30, the line was restarted. Supplemental report: part g accident cause updated to excavation damage by third party.
Report Received Date 2022-08-18 00:00:00
Iyear 2022
Report Number 20220185
Supplemental Number 38301
Report Type Supplemental Final
Operator Id 18718 PHMSA Enforcement
Name Sunoco Pipeline L.p.
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2022-07-19 18:08:00
Time Zone Central
Daylight Savings Ind Yes
Location Latitude 35.259413 Google Maps OpenStreetMap
Location Longitude -100.938225 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 83
Recovered Bbls 83
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Cpm Leak Detection System
Incident Identified Datetime 2022-07-19 18:08:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Status When Identified Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind Yes
Shutdown Datetime 2022-07-19 20:03:00
Restart Datetime 2022-07-22 12:30:00
Communication State Fed Ind Yes
Party Initiated Communication Operator
Initial Responder Com Datetime 2022-07-20 11:32:00
On Site Datetime 2022-07-19 22:46:00
Confirmed Discovery Datetime 2022-07-19 22:46:00
Nrc Rpt Datetime 2022-07-20 00:08:00
Nrc Rpt Num 1341998 NRC Report How to search
Additional Nrc Report Numbers 1342167
Ignite Ind No
Upstream Action Taken Valve Closure
Upstream Valve Close Datetime 2022-07-19 22:30:00
Upstream Valve Type Ind Manual
Downstream Action Taken Valve Closure
Downstream Vlv Close Datetime 2022-07-19 23:13:00
Downstream Valve Type Ind Manual
Notify Qualified Indiv Ind Yes
Qualified Indiv Notif Datetime 2022-07-19 22:45:00
Oil Spill Removal Org Ind No
Num Pub Evacuated 0
Pipe Fac Name Alanreed To Mcclellen
Segment Name 23002.08 - 8" Farm Rd 2477 Trap To Mcclellan
Onshore State Abbreviation Tx
Onshore Postal Code 79002
Onshore City Name Not Within Municipality
Onshore County Name Gray
Designated Location Survey Station No.
Designated Name 83172.2
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 6
Crossing No
Pipe Facility Type Intrastate
Item Involved Pipe
Pipe Type Pipe Body
Puddle Weld Ind No
Pipe Diameter 8.625
Pipe Wall Thickness 0.322
Pipe Smys 30000
Pipe Specification Api 5l Grade A
Pipe Seam Type Lap Welded
Pipe Manufacturer Unknown
Pipe Coating Type None
Coating Applied Ind No
Installation Year 1942
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Mechanical Puncture
Puncture Axial 3.9
Puncture Circum 3.6
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 7150
Est Cost Prop Damage 200000
Est Cost Emergency 100000
Est Cost Environmental 75000
Est Cost Other 0
Prpty 382150
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 295
Mop Psig 707
Mop Cfr Section Subpart E Pressure Test �195.406(A)(3) View CFR 49 §192
Maop Established Date 2016-03-15 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 44626
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind Yes
Cpm Conf Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind Yes
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind Yes
Contractor Drug Test Ind No
Num Employees Tested 1
Num Employees Failed 0
Cause Excavation Damage
Cause Details Excavation Damage By Third Party
Ex Party Type Excavation Damage By Third Party
Prior Notification Ind No
State Law Exempt Ind Yes
State Law Exempt Type Activity Is Exempt And Did Not Exceed The Limits Of The Exemption
State Law Exempt Authority Texas Underground Facility Notification Corporation
State Law Exempt Criteria Depth Exemption 16-Inch
Notify Cga Dirt No
Private Row Ind Yes
Private Subtype Private Landowner
Joint Trench Ind No
Cross Bore Ind No
Depth Of Grade < 18�
Excavator Type Farmer
Excavator Equipment Farm Equipment
Work Performed Agriculture
One Call Notified Ind No
Locator Type Unknown/other
Visible Marks No
Service Interruption Yes
Service Interruption Hours 96
Root Cause Category Miscellaneous Root Causes
Root Cause Type Root Cause Not Listed (Comment Required)
Root Cause Type Other Shallow Pipeline
Preparer Name T*** N*******
Preparer Title Director - Regulatory Compliance
Preparer Email T************@e*************.com
Preparer Telephone 713-989-7126
Prepared Date 2023-07-21 00:00:00
Authorizer Name T*** N*******
Authorizer Telephone 713-989-7126
Authorizer Title Director - Regulatory Compliance
Authorizer Email T************@e*************.com
Narrative On 07/19/22 at 18:08, the control center received an initial line imbalance alarm. Controller made downstream adjustments to pumps believing that the alarm may be due to downstream suction. Controller then contacted alarm team which believed there could potentially be meter issues on the system. At 20:03, the controller shut down the line down and contacted field operations. At 20:40, the control center received a call from the landowner reporting a possible leak and the controller again contacted field operations to dispatch someone to the area to investigate. At 22:46, local operations personnel arrived onsite and confirmed a leak between alanreed and mcclellan pump stations and then proceeded to close valves to isolate the leak area. At 00:08 ct nrc was notified (report no. 1341998) due to anticipated total costs exceeding $50,000. Approximately 83 barrels of crude oil was released. Cleanup and repair crews were mobilized to begin remediation and repair efforts. It was determined that the landowner was cultivating the field earlier that day on 7/19/22 using a tractor with discs and struck the line causing the release. Measured depth at the strike was approximately 6-inches due to erosion. A plidco clamp was applied to control the release of crude oil while cleanup efforts continued. As a permanent repair and to address the shallow cover in this area to prevent a recurrence, approximately 120 feet of pipe was cut out and replaced and approximately 900 feet of the pipeline was lowered achieving approximately 36-40 inches of cover. The exposed pipeline is also being recoated. On 7/22/22 at approximately 12:30, the line was restarted. Supplemental report: part g accident cause updated to excavation damage by third party.

All rights reserved. Copyright © by ClearPHMSA