HL incident on 2022-07-14 — TX

Operator
Enterprise Crude Pipeline Llc
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2022-07-14 03:07
Report number
Location
TX
Narrative
On 7/14/22 at approximately 03:04 cdst an enterprise operator was making rounds at echo station and observed crude oil pooling in the vicinity of meter skid 350. Control center was then notified to shut down the movement across the meter skid and the affected area was isolated. An estimated 2.7 barrels of crude oil were released. Remediation of the soil is complete. The portion of line that leaked has been permanently deactivated. Apparent cause of the leak has been determined as internal corrosion. Nrc: #1341590 on 7/15/2022 at 12:41 cdst due to cleanup costs exceeding $50k. 48 hr nrc: #1341721 on 7/16 at 20:42 cdst.
Detailed record list
Report Received Date
2022-08-12 00:00:00
Iyear
2022
Report Number
20220181
Supplemental Number
37467
Report Type
Supplemental Final
Operator Id
Name
Enterprise Crude Pipeline Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2022-07-14 03:12:00
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
2.7
Recovered Bbls
2.7
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Ground Patrol By Operator Or Its Contractor
Operator Type
Operator Employee
Incident Identified Datetime
2022-07-14 03:07:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2022-07-14 03:12:00
Restart Datetime
2022-07-26 08:00:00
Communication State Fed Ind
No
On Site Datetime
2022-07-14 03:50:00
Confirmed Discovery Datetime
2022-07-14 03:07:00
Nrc Rpt Datetime
2022-07-14 12:41:00
Nrc Rpt Num
Additional Nrc Report Numbers
1341721
Ignite Ind
No
Notify Qualified Indiv Ind
Yes
Qualified Indiv Notif Datetime
2022-07-14 03:12:00
Oil Spill Removal Org Ind
Yes
Osro Activated Datetime
2022-07-14 03:15:00
Osro Arrived On Site Dt
7/14/2022 3:50
Num Pub Evacuated
0
Pipe Fac Name
Echo Station
Segment Name
Meter Skid 350
Onshore State Abbreviation
Tx
Onshore Postal Code
77034
Onshore City Name
Houston
Onshore County Name
Harris
Designated Location
Milepost
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Exposed Due To Excavation
Depth Of Cover
48
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Puddle Weld Ind
No
Pipe Diameter
24
Pipe Wall Thickness
0.375
Pipe Smys
42000
Pipe Specification
Unknown
Pipe Seam Type
Other
Pipe Seam Details
Unknown
Pipe Manufacturer
United States Steel
Pipe Coating Type
Fusion Bonded Epoxy(Fbe)
Coating Applied Ind
No
Installation Year
2011
Manufactured Year
2011
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
200
Est Cost Prop Damage
0
Est Cost Emergency
283000
Est Cost Environmental
0
Est Cost Other
0
Prpty
283200
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
106
Mop Psig
1440
Mop Cfr Section
Component Design Pressure �195.406(A)(2)
Maop Established Date
2011-08-31 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Controller did not contribute to accident.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Not Cut Open
Int Corrosive Commodity Ind
Yes
Int Field Exam Basis Ind
Yes
Int Dead Leg Loc Ind
Yes
Corrosion Inhibitors
Yes
Corrosion Lining
No
Cleaning Dewatering
Not Applicable - Not Mainline Pipe
Corrosion Coupons
Yes
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
R*** T********
Preparer Title
Senior Pipeline Compliance Engineer
Preparer Email
R*********@e****.com
Preparer Telephone
713-381-4659
Prepared Date
2022-12-15 00:00:00
Authorizer Name
R*** T********
Authorizer Telephone
713-381-4659
Authorizer Title
Senior Pipeline Compliance Engineer
Authorizer Email
R*********@e****.com
Narrative
On 7/14/22 at approximately 03:04 cdst an enterprise operator was making rounds at echo station and observed crude oil pooling in the vicinity of meter skid 350. Control center was then notified to shut down the movement across the meter skid and the affected area was isolated. An estimated 2.7 barrels of crude oil were released. Remediation of the soil is complete. The portion of line that leaked has been permanently deactivated. Apparent cause of the leak has been determined as internal corrosion. Nrc: #1341590 on 7/15/2022 at 12:41 cdst due to cleanup costs exceeding $50k. 48 hr nrc: #1341721 on 7/16 at 20:42 cdst.
Report Received Date 2022-08-12 00:00:00
Iyear 2022
Report Number 20220181
Supplemental Number 37467
Report Type Supplemental Final
Operator Id 30829 PHMSA Enforcement
Name Enterprise Crude Pipeline Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2022-07-14 03:12:00
Time Zone Central
Daylight Savings Ind Yes
Location Latitude 29.61103 Google Maps OpenStreetMap
Location Longitude -95.1846 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 2.7
Recovered Bbls 2.7
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Ground Patrol By Operator Or Its Contractor
Operator Type Operator Employee
Incident Identified Datetime 2022-07-14 03:07:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Status When Identified Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind Yes
Shutdown Datetime 2022-07-14 03:12:00
Restart Datetime 2022-07-26 08:00:00
Communication State Fed Ind No
On Site Datetime 2022-07-14 03:50:00
Confirmed Discovery Datetime 2022-07-14 03:07:00
Nrc Rpt Datetime 2022-07-14 12:41:00
Nrc Rpt Num 1341590 NRC Report How to search
Additional Nrc Report Numbers 1341721
Ignite Ind No
Notify Qualified Indiv Ind Yes
Qualified Indiv Notif Datetime 2022-07-14 03:12:00
Oil Spill Removal Org Ind Yes
Osro Activated Datetime 2022-07-14 03:15:00
Osro Arrived On Site Dt 7/14/2022 3:50
Num Pub Evacuated 0
Pipe Fac Name Echo Station
Segment Name Meter Skid 350
Onshore State Abbreviation Tx
Onshore Postal Code 77034
Onshore City Name Houston
Onshore County Name Harris
Designated Location Milepost
Designated Name 0
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Exposed Due To Excavation
Depth Of Cover 48
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Puddle Weld Ind No
Pipe Diameter 24
Pipe Wall Thickness 0.375
Pipe Smys 42000
Pipe Specification Unknown
Pipe Seam Type Other
Pipe Seam Details Unknown
Pipe Manufacturer United States Steel
Pipe Coating Type Fusion Bonded Epoxy(Fbe)
Coating Applied Ind No
Installation Year 2011
Manufactured Year 2011
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 200
Est Cost Prop Damage 0
Est Cost Emergency 283000
Est Cost Environmental 0
Est Cost Other 0
Prpty 283200
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 106
Mop Psig 1440
Mop Cfr Section Component Design Pressure �195.406(A)(2) View CFR 49 §192
Maop Established Date 2011-08-31 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Controller did not contribute to accident.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results Not Cut Open
Int Corrosive Commodity Ind Yes
Int Field Exam Basis Ind Yes
Int Dead Leg Loc Ind Yes
Corrosion Inhibitors Yes
Corrosion Lining No
Cleaning Dewatering Not Applicable - Not Mainline Pipe
Corrosion Coupons Yes
Collected Data Ind No
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name R*** T********
Preparer Title Senior Pipeline Compliance Engineer
Preparer Email R*********@e****.com
Preparer Telephone 713-381-4659
Prepared Date 2022-12-15 00:00:00
Authorizer Name R*** T********
Authorizer Telephone 713-381-4659
Authorizer Title Senior Pipeline Compliance Engineer
Authorizer Email R*********@e****.com
Narrative On 7/14/22 at approximately 03:04 cdst an enterprise operator was making rounds at echo station and observed crude oil pooling in the vicinity of meter skid 350. Control center was then notified to shut down the movement across the meter skid and the affected area was isolated. An estimated 2.7 barrels of crude oil were released. Remediation of the soil is complete. The portion of line that leaked has been permanently deactivated. Apparent cause of the leak has been determined as internal corrosion. Nrc: #1341590 on 7/15/2022 at 12:41 cdst due to cleanup costs exceeding $50k. 48 hr nrc: #1341721 on 7/16 at 20:42 cdst.

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