HL incident on 2022-06-25 — TX

Operator
Products (Se) Pipe Line Corporation
Cause
Incorrect Operation
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2022-06-25 07:45
Report number
Location
TX
Narrative
On 6/25/2022 what was originally thought to be a 3 gallon release occurred at the austell tank farm from an above ground jet fuel filter vessel. At the time of the release there was heavy rain, but all product was thought to have been recovered. On 6/27/2022 additional heavy rains overfilled kinder morgan's ppl (se) austell tank farm water retention pond causing a water & jet fuel mix to be released off the facility grounds. The water & jet fuel mixture entered a nearby creek and migrated to a private pond located at 2773 trail creek circle, lithia springs, ga 30122 in douglas county (lat 33.755061, lon -84.665357) where the product was contained. Due to the water being released offsite into the nearby creek and pond, the national response center was notified (nrc#1339939) as well as georgia epd, usepa region 4, and ga fish and wildlife. The incoming and outgoing pipelines were shut down and kinder morgan ppl (se) contract osro's were notified and the ppl se oil spill response plan was implemented. Initial volume of jet fuel released was an estimated 43 barrels. An internal investigation later determined that the initial release on 6/25/2022 was the origination of the release that was found on 6/27/2022. The investigation is still ongoing to determine the specific component that failed. This information will be updated on a supplemental and final 7000.1 as well as updated costs of remediation. Update 12/20/2022 - an internal investigation concluded the failed component was an o-ring which was not installed properly into the groove of a filter vessel and was pinched by the vessel closure door. A new o-ring was installed. The total costs for remediation listed in part d includes an estimated $200k for future remediation costs, therefore the continuation of supplemental report filings in the future will not provide any essential information which will be critically different than that contained in this supplemental and final report.
Detailed record list
Report Received Date
2022-07-25 00:00:00
Iyear
2022
Report Number
20220159
Supplemental Number
37811
Report Type
Supplemental Final
Operator Id
Name
Products (Se) Pipe Line Corporation
Operator Street Address
1001 Louisiana St Suite 1000
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2022-06-25 05:05:00
Time Zone
Eastern
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
43
Recovered Bbls
30.95
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Or Pack Calculations)
Incident Identified Datetime
2022-06-25 07:45:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Status When Identified
Routine Start-Up
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2022-06-25 05:13:00
Restart Datetime
2022-06-25 11:05:00
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Initial Responder Com Datetime
2022-06-27 14:00:00
On Site Datetime
2022-06-27 06:45:00
Confirmed Discovery Datetime
2022-06-27 14:40:00
Nrc Rpt Datetime
2022-06-27 15:24:00
Nrc Rpt Num
Additional Nrc Report Numbers
1340123
Ignite Ind
No
Notify Qualified Indiv Ind
Yes
Qualified Indiv Notif Datetime
2022-06-27 11:30:00
Oil Spill Removal Org Ind
Yes
Osro Activated Datetime
2022-06-27 13:00:00
Osro Arrived On Site Dt
6/27/2022 15:30
Num Pub Evacuated
0
Pipe Fac Name
Austell Tank Farm
Segment Name
12" Maf Atl Airport
Onshore State Abbreviation
Ga
Onshore Postal Code
30122
Onshore City Name
Lithia Springs
Onshore County Name
Douglass
Designated Location
Milepost
Designated Name
0
Federal
No
Location Type
Originated On Operator-Controlled Property, But Then Flowed Or Migrated Off The Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Filter/strainer/separator
Installation Year
1969
Manufactured Year
1969
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
Yes
Fish Aquatic Impact Ind
Yes
Soil Contamination
Yes
Long Term Assessment
Yes
Remediation Ind
Yes
Groundwater Remed Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
Yes
Surface Contam Ind
Yes
Amount Released
25
Rel Water Name
Unnamed Stream
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Est Cost Oper Paid
12150
Est Cost Gas Released
7380
Est Cost Prop Damage
0
Est Cost Emergency
359720
Est Cost Environmental
322345
Est Cost Other
0
Prpty
701595
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
96
Mop Psig
150
Mop Cfr Section
Component Design Pressure �195.406(A)(2)
Maop Established Date
1969-01-01 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind
Yes
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Equipment Not Installed Properly
Operation Type
Equipment Not Installed Properly
Related Other Ind
Yes
Operation Related Details
The Failed Component Was An O-Ring Which Was Not Installed Properly Into The Groove Of A Filter Vessel And Was Pinched By The Vessel Closure Door.
Category Type
Routine Maintenance
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
J**** P*******
Preparer Title
Specialist - Technical Compliance Code St Sr Ii
Preparer Email
J*************@k***********.com
Preparer Telephone
7134207004
Prepared Date
2023-03-08 00:00:00
Local Contact Name
C*** G******
Local Contact Email
C***********@k***********.com
Local Contact Telephone
7708244418
Authorizer Name
D******* S*******
Authorizer Telephone
7137250147
Authorizer Title
Manager
Authorizer Email
D****************@k***********.com
Narrative
On 6/25/2022 what was originally thought to be a 3 gallon release occurred at the austell tank farm from an above ground jet fuel filter vessel. At the time of the release there was heavy rain, but all product was thought to have been recovered. On 6/27/2022 additional heavy rains overfilled kinder morgan's ppl (se) austell tank farm water retention pond causing a water & jet fuel mix to be released off the facility grounds. The water & jet fuel mixture entered a nearby creek and migrated to a private pond located at 2773 trail creek circle, lithia springs, ga 30122 in douglas county (lat 33.755061, lon -84.665357) where the product was contained. Due to the water being released offsite into the nearby creek and pond, the national response center was notified (nrc#1339939) as well as georgia epd, usepa region 4, and ga fish and wildlife. The incoming and outgoing pipelines were shut down and kinder morgan ppl (se) contract osro's were notified and the ppl se oil spill response plan was implemented. Initial volume of jet fuel released was an estimated 43 barrels. An internal investigation later determined that the initial release on 6/25/2022 was the origination of the release that was found on 6/27/2022. The investigation is still ongoing to determine the specific component that failed. This information will be updated on a supplemental and final 7000.1 as well as updated costs of remediation. Update 12/20/2022 - an internal investigation concluded the failed component was an o-ring which was not installed properly into the groove of a filter vessel and was pinched by the vessel closure door. A new o-ring was installed. The total costs for remediation listed in part d includes an estimated $200k for future remediation costs, therefore the continuation of supplemental report filings in the future will not provide any essential information which will be critically different than that contained in this supplemental and final report.
Report Received Date 2022-07-25 00:00:00
Iyear 2022
Report Number 20220159
Supplemental Number 37811
Report Type Supplemental Final
Operator Id 15674 PHMSA Enforcement
Name Products (Se) Pipe Line Corporation
Operator Street Address 1001 Louisiana St Suite 1000
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2022-06-25 05:05:00
Time Zone Eastern
Daylight Savings Ind Yes
Location Latitude 33.755061 Google Maps OpenStreetMap
Location Longitude -84.665357 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls 43
Recovered Bbls 30.95
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Or Pack Calculations)
Incident Identified Datetime 2022-06-25 07:45:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Status When Identified Routine Start-Up
Shutdown Due Accident Ind Yes
Shutdown Datetime 2022-06-25 05:13:00
Restart Datetime 2022-06-25 11:05:00
Communication State Fed Ind Yes
Party Initiated Communication Operator
Initial Responder Com Datetime 2022-06-27 14:00:00
On Site Datetime 2022-06-27 06:45:00
Confirmed Discovery Datetime 2022-06-27 14:40:00
Nrc Rpt Datetime 2022-06-27 15:24:00
Nrc Rpt Num 1339939 NRC Report How to search
Additional Nrc Report Numbers 1340123
Ignite Ind No
Notify Qualified Indiv Ind Yes
Qualified Indiv Notif Datetime 2022-06-27 11:30:00
Oil Spill Removal Org Ind Yes
Osro Activated Datetime 2022-06-27 13:00:00
Osro Arrived On Site Dt 6/27/2022 15:30
Num Pub Evacuated 0
Pipe Fac Name Austell Tank Farm
Segment Name 12" Maf Atl Airport
Onshore State Abbreviation Ga
Onshore Postal Code 30122
Onshore City Name Lithia Springs
Onshore County Name Douglass
Designated Location Milepost
Designated Name 0
Federal No
Location Type Originated On Operator-Controlled Property, But Then Flowed Or Migrated Off The Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Filter/strainer/separator
Installation Year 1969
Manufactured Year 1969
Material Involved Carbon Steel
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind Yes
Fish Aquatic Impact Ind Yes
Soil Contamination Yes
Long Term Assessment Yes
Remediation Ind Yes
Groundwater Remed Ind Yes
Soil Remed Ind Yes
Water Contam Ind Yes
Surface Contam Ind Yes
Amount Released 25
Rel Water Name Unnamed Stream
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Usa Drinking Ind Yes
Usa Drinking Yes No Yes
Est Cost Oper Paid 12150
Est Cost Gas Released 7380
Est Cost Prop Damage 0
Est Cost Emergency 359720
Est Cost Environmental 322345
Est Cost Other 0
Prpty 701595
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 96
Mop Psig 150
Mop Cfr Section Component Design Pressure �195.406(A)(2) View CFR 49 §192
Maop Established Date 1969-01-01 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind Yes
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Equipment Not Installed Properly
Operation Type Equipment Not Installed Properly
Related Other Ind Yes
Operation Related Details The Failed Component Was An O-Ring Which Was Not Installed Properly Into The Groove Of A Filter Vessel And Was Pinched By The Vessel Closure Door.
Category Type Routine Maintenance
Operator Qualification Ind Yes
Qualified Individuals Yes, They Were Qualified For The Task(S)
Preparer Name J**** P*******
Preparer Title Specialist - Technical Compliance Code St Sr Ii
Preparer Email J*************@k***********.com
Preparer Telephone 7134207004
Prepared Date 2023-03-08 00:00:00
Local Contact Name C*** G******
Local Contact Email C***********@k***********.com
Local Contact Telephone 7708244418
Authorizer Name D******* S*******
Authorizer Telephone 7137250147
Authorizer Title Manager
Authorizer Email D****************@k***********.com
Narrative On 6/25/2022 what was originally thought to be a 3 gallon release occurred at the austell tank farm from an above ground jet fuel filter vessel. At the time of the release there was heavy rain, but all product was thought to have been recovered. On 6/27/2022 additional heavy rains overfilled kinder morgan's ppl (se) austell tank farm water retention pond causing a water & jet fuel mix to be released off the facility grounds. The water & jet fuel mixture entered a nearby creek and migrated to a private pond located at 2773 trail creek circle, lithia springs, ga 30122 in douglas county (lat 33.755061, lon -84.665357) where the product was contained. Due to the water being released offsite into the nearby creek and pond, the national response center was notified (nrc#1339939) as well as georgia epd, usepa region 4, and ga fish and wildlife. The incoming and outgoing pipelines were shut down and kinder morgan ppl (se) contract osro's were notified and the ppl se oil spill response plan was implemented. Initial volume of jet fuel released was an estimated 43 barrels. An internal investigation later determined that the initial release on 6/25/2022 was the origination of the release that was found on 6/27/2022. The investigation is still ongoing to determine the specific component that failed. This information will be updated on a supplemental and final 7000.1 as well as updated costs of remediation. Update 12/20/2022 - an internal investigation concluded the failed component was an o-ring which was not installed properly into the groove of a filter vessel and was pinched by the vessel closure door. A new o-ring was installed. The total costs for remediation listed in part d includes an estimated $200k for future remediation costs, therefore the continuation of supplemental report filings in the future will not provide any essential information which will be critically different than that contained in this supplemental and final report.

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