HL incident on 2022-06-25 — TX

Operator
Enterprise Products Operating Llc
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$15
Incident datetime
2022-06-25 03:00
Report number
Location
TX
Narrative
On 6/25/22 at approximately 03:00 cdst lowell booster pump went down on high gas detect and pipeline control dispatched local technician to investigate. Upon arrival the technician found that a pressure gauge's crossover tubing had broken off at the feral. It is estimated that 10 gallons of product were released. Product has been cleaned up and the line was restarted at 06:25 cdst the same day. Tubing has been reinstalled with supports to prevent recurrence.
Detailed record list
Report Received Date
2022-07-25 00:00:00
Iyear
2022
Report Number
20220158
Supplemental Number
37495
Report Type
Supplemental Final
Operator Id
Name
Enterprise Products Operating Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2022-06-25 03:00:00
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
0.3
Recovered Bbls
0.3
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Or Pack Calculations)
Incident Identified Datetime
2022-06-25 03:00:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2022-06-25 03:00:00
Restart Datetime
2022-06-25 06:25:00
Communication State Fed Ind
No
On Site Datetime
2022-06-25 04:00:00
Confirmed Discovery Datetime
2022-06-25 06:30:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Notify Qualified Indiv Ind
Yes
Qualified Indiv Notif Datetime
2022-06-25 03:05:00
Oil Spill Removal Org Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Lowell Station
Segment Name
Inxx0429
Onshore State Abbreviation
In
Onshore Postal Code
46356
Onshore City Name
Lowell
Onshore County Name
Lake County
Designated Location
Milepost
Designated Name
186.58
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Tubing
Tubing Material
Stainless Steel
Tubing Type
Rigid
Installation Year
2022
Manufactured Year
2022
Material Involved
Material Other Than Carbon Steel
Material Details
Rigid Stainless Steel Tubing
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
10
Est Cost Prop Damage
15
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
25
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
477
Mop Psig
1337
Mop Cfr Section
Subpart E Pressure Test �195.406(A)(3)
Maop Established Date
2009-11-04 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Leak cause was not attributed to controller's actions.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Threaded Connection/coupling Failure
Eq Failure Type
Threaded Connection/coupling Failure
Other Stripped Ind
Threaded Fitting
Additional Support Ind
Yes
Preparer Name
R*** T********
Preparer Title
Senior Pipeline Compliance Engineer
Preparer Email
R*********@e****.com
Preparer Telephone
713-381-4659
Prepared Date
2022-12-20 00:00:00
Authorizer Name
R*** T********
Authorizer Telephone
713-381-4659
Authorizer Title
Senior Pipeline Compliance Engineer
Authorizer Email
R*********@e****.com
Narrative
On 6/25/22 at approximately 03:00 cdst lowell booster pump went down on high gas detect and pipeline control dispatched local technician to investigate. Upon arrival the technician found that a pressure gauge's crossover tubing had broken off at the feral. It is estimated that 10 gallons of product were released. Product has been cleaned up and the line was restarted at 06:25 cdst the same day. Tubing has been reinstalled with supports to prevent recurrence.
Report Received Date 2022-07-25 00:00:00
Iyear 2022
Report Number 20220158
Supplemental Number 37495
Report Type Supplemental Final
Operator Id 31618 PHMSA Enforcement
Name Enterprise Products Operating Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2022-06-25 03:00:00
Time Zone Central
Daylight Savings Ind Yes
Location Latitude 41.26173 Google Maps OpenStreetMap
Location Longitude -87.48634 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 0.3
Recovered Bbls 0.3
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Or Pack Calculations)
Incident Identified Datetime 2022-06-25 03:00:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Status When Identified Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind Yes
Shutdown Datetime 2022-06-25 03:00:00
Restart Datetime 2022-06-25 06:25:00
Communication State Fed Ind No
On Site Datetime 2022-06-25 04:00:00
Confirmed Discovery Datetime 2022-06-25 06:30:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Notify Qualified Indiv Ind Yes
Qualified Indiv Notif Datetime 2022-06-25 03:05:00
Oil Spill Removal Org Ind No
Num Pub Evacuated 0
Pipe Fac Name Lowell Station
Segment Name Inxx0429
Onshore State Abbreviation In
Onshore Postal Code 46356
Onshore City Name Lowell
Onshore County Name Lake County
Designated Location Milepost
Designated Name 186.58
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Tubing
Tubing Material Stainless Steel
Tubing Type Rigid
Installation Year 2022
Manufactured Year 2022
Material Involved Material Other Than Carbon Steel
Material Details Rigid Stainless Steel Tubing
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 10
Est Cost Prop Damage 15
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 25
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 477
Mop Psig 1337
Mop Cfr Section Subpart E Pressure Test �195.406(A)(3) View CFR 49 §192
Maop Established Date 2009-11-04 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Leak cause was not attributed to controller's actions.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Threaded Connection/coupling Failure
Eq Failure Type Threaded Connection/coupling Failure
Other Stripped Ind Threaded Fitting
Additional Support Ind Yes
Preparer Name R*** T********
Preparer Title Senior Pipeline Compliance Engineer
Preparer Email R*********@e****.com
Preparer Telephone 713-381-4659
Prepared Date 2022-12-20 00:00:00
Authorizer Name R*** T********
Authorizer Telephone 713-381-4659
Authorizer Title Senior Pipeline Compliance Engineer
Authorizer Email R*********@e****.com
Narrative On 6/25/22 at approximately 03:00 cdst lowell booster pump went down on high gas detect and pipeline control dispatched local technician to investigate. Upon arrival the technician found that a pressure gauge's crossover tubing had broken off at the feral. It is estimated that 10 gallons of product were released. Product has been cleaned up and the line was restarted at 06:25 cdst the same day. Tubing has been reinstalled with supports to prevent recurrence.

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