Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2022-06-25 — TX
Operator
Enterprise Products Operating Llc
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$15
Incident datetime
2022-06-25 03:00
Report number
Location
TX
Narrative
On 6/25/22 at approximately 03:00 cdst lowell booster pump went down on high gas detect and pipeline control dispatched local technician to investigate. Upon arrival the technician found that a pressure gauge's crossover tubing had broken off at the feral. It is estimated that 10 gallons of product were released. Product has been cleaned up and the line was restarted at 06:25 cdst the same day. Tubing has been reinstalled with supports to prevent recurrence.
Detailed record list
Report Received Date
2022-07-25 00:00:00
Iyear
2022
Report Number
20220158
Supplemental Number
37495
Report Type
Supplemental Final
Operator Id
31618
Name
Enterprise Products Operating Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2022-06-25 03:00:00
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
41.26173
Location Longitude
-87.48634
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
0.3
Recovered Bbls
0.3
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Or Pack Calculations)
Incident Identified Datetime
2022-06-25 03:00:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2022-06-25 03:00:00
Restart Datetime
2022-06-25 06:25:00
Communication State Fed Ind
No
On Site Datetime
2022-06-25 04:00:00
Confirmed Discovery Datetime
2022-06-25 06:30:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Notify Qualified Indiv Ind
Yes
Qualified Indiv Notif Datetime
2022-06-25 03:05:00
Oil Spill Removal Org Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Lowell Station
Segment Name
Inxx0429
Onshore State Abbreviation
In
Onshore Postal Code
46356
Onshore City Name
Lowell
Onshore County Name
Lake County
Designated Location
Milepost
Designated Name
186.58
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Tubing
Tubing Material
Stainless Steel
Tubing Type
Rigid
Installation Year
2022
Manufactured Year
2022
Material Involved
Material Other Than Carbon Steel
Material Details
Rigid Stainless Steel Tubing
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
10
Est Cost Prop Damage
15
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
25
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
477
Mop Psig
1337
Mop Cfr Section
Subpart E Pressure Test �195.406(A)(3)
Maop Established Date
2009-11-04 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Leak cause was not attributed to controller's actions.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Threaded Connection/coupling Failure
Eq Failure Type
Threaded Connection/coupling Failure
Other Stripped Ind
Threaded Fitting
Additional Support Ind
Yes
Preparer Name
R*** T********
Preparer Title
Senior Pipeline Compliance Engineer
Preparer Email
R*********@e****.com
Preparer Telephone
713-381-4659
Prepared Date
2022-12-20 00:00:00
Authorizer Name
R*** T********
Authorizer Telephone
713-381-4659
Authorizer Title
Senior Pipeline Compliance Engineer
Authorizer Email
R*********@e****.com
Narrative
On 6/25/22 at approximately 03:00 cdst lowell booster pump went down on high gas detect and pipeline control dispatched local technician to investigate. Upon arrival the technician found that a pressure gauge's crossover tubing had broken off at the feral. It is estimated that 10 gallons of product were released. Product has been cleaned up and the line was restarted at 06:25 cdst the same day. Tubing has been reinstalled with supports to prevent recurrence.
| Report Received Date | 2022-07-25 00:00:00 |
|---|---|
| Iyear | 2022 |
| Report Number | 20220158 |
| Supplemental Number | 37495 |
| Report Type | Supplemental Final |
| Operator Id | 31618 PHMSA Enforcement |
| Name | Enterprise Products Operating Llc |
| Operator Street Address | 1100 Louisiana Street |
| Operator City Name | Houston |
| Operator State Abbreviation | TX |
| Operator Postal Code | 77002 |
| Local Datetime | 2022-06-25 03:00:00 |
| Time Zone | Central |
| Daylight Savings Ind | Yes |
| Location Latitude | 41.26173 Google Maps OpenStreetMap |
| Location Longitude | -87.48634 Google Maps OpenStreetMap |
| Commodity Released Type | Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions |
| Commodity Subtype | Gasoline (Non-Ethanol) |
| Unintentional Release Bbls | 0.3 |
| Recovered Bbls | 0.3 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Accident Identifier | Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Or Pack Calculations) |
| Incident Identified Datetime | 2022-06-25 03:00:00 |
| System Part Involved | Onshore Pump/meter Station Equipment And Piping |
| On Off Shore | Onshore |
| Status When Identified | Normal Operation, Includes Pauses Between Batches And During Maintenance |
| Shutdown Due Accident Ind | Yes |
| Shutdown Datetime | 2022-06-25 03:00:00 |
| Restart Datetime | 2022-06-25 06:25:00 |
| Communication State Fed Ind | No |
| On Site Datetime | 2022-06-25 04:00:00 |
| Confirmed Discovery Datetime | 2022-06-25 06:30:00 |
| Nrc Rpt Num | Nrc Notification Not Required NRC Report How to search |
| Ignite Ind | No |
| Notify Qualified Indiv Ind | Yes |
| Qualified Indiv Notif Datetime | 2022-06-25 03:05:00 |
| Oil Spill Removal Org Ind | No |
| Num Pub Evacuated | 0 |
| Pipe Fac Name | Lowell Station |
| Segment Name | Inxx0429 |
| Onshore State Abbreviation | In |
| Onshore Postal Code | 46356 |
| Onshore City Name | Lowell |
| Onshore County Name | Lake County |
| Designated Location | Milepost |
| Designated Name | 186.58 |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Aboveground |
| Incident Area Subtype | Typical Aboveground Facility Piping Or Appurtenance |
| Crossing | No |
| Pipe Facility Type | Interstate |
| Item Involved | Tubing |
| Tubing Material | Stainless Steel |
| Tubing Type | Rigid |
| Installation Year | 2022 |
| Manufactured Year | 2022 |
| Material Involved | Material Other Than Carbon Steel |
| Material Details | Rigid Stainless Steel Tubing |
| Release Type | Leak |
| Leak Type | Connection Failure |
| Wildlife Impact Ind | No |
| Soil Contamination | No |
| Long Term Assessment | No |
| Remediation Ind | No |
| Water Contam Ind | No |
| Could Be Hca | No |
| Commodity Reached Hca | No |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 10 |
| Est Cost Prop Damage | 15 |
| Est Cost Emergency | 0 |
| Est Cost Environmental | 0 |
| Est Cost Other | 0 |
| Prpty | 25 |
| Num Persons Hosp Not Ovnght | 0 |
| Num Injured Treated By Emt | 0 |
| Num Resident Building Affctd | 0 |
| Num Business Building Affctd | 0 |
| Accident Psig | 477 |
| Mop Psig | 1337 |
| Mop Cfr Section | Subpart E Pressure Test �195.406(A)(3) View CFR 49 §192 |
| Maop Established Date | 2009-11-04 00:00:00 |
| Maop Reversal Flow Ind | No |
| Accident Pressure | Pressure Did Not Exceed Mop |
| Pressure Restriction Ind | No |
| Pipeline Function | > 20% Smys Regulated Transmission |
| Scada In Place Ind | Yes |
| Scada Operating Ind | Yes |
| Scada Functional Ind | Yes |
| Scada Detection Ind | No |
| Scada Conf Ind | No |
| Cpm In Place Ind | Yes |
| Cpm Operating Ind | Yes |
| Cpm Functional Ind | Yes |
| Cpm Detection Ind | No |
| Cpm Conf Ind | No |
| Investigation Status | No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate) |
| Investigation Status Details | Leak cause was not attributed to controller's actions. |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Equipment Failure |
| Cause Details | Threaded Connection/coupling Failure |
| Eq Failure Type | Threaded Connection/coupling Failure |
| Other Stripped Ind | Threaded Fitting |
| Additional Support Ind | Yes |
| Preparer Name | R*** T******** |
| Preparer Title | Senior Pipeline Compliance Engineer |
| Preparer Email | R*********@e****.com |
| Preparer Telephone | 713-381-4659 |
| Prepared Date | 2022-12-20 00:00:00 |
| Authorizer Name | R*** T******** |
| Authorizer Telephone | 713-381-4659 |
| Authorizer Title | Senior Pipeline Compliance Engineer |
| Authorizer Email | R*********@e****.com |
| Narrative | On 6/25/22 at approximately 03:00 cdst lowell booster pump went down on high gas detect and pipeline control dispatched local technician to investigate. Upon arrival the technician found that a pressure gauge's crossover tubing had broken off at the feral. It is estimated that 10 gallons of product were released. Product has been cleaned up and the line was restarted at 06:25 cdst the same day. Tubing has been reinstalled with supports to prevent recurrence. |
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