HL incident on 2022-06-22 — TX

Operator
Kinder Morgan Crude And Condensate Llc
Cause
Incorrect Operation
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$488,470
Incident datetime
2022-06-22 12:15
Report number
Location
TX
Narrative
06/22/2022- an aerial patrol pilot notified kinder morgan crude and condensate operations personnel of a stain on the row on the intrastate 30 inch kmcc dewitt to oti line near the city of edna in jackson county, texas at approximately 11:30 cst. Operations dispatched personnel to the site and they confirmed a crude oil release at 12:15pm cst. The pipeline was already on a scheduled shutdown at the time of the reported staining. Based on initial estimate of a crude oil release greater than 5 gallons, a telephonic notification was made to the railroad commission of texas's emergency line. Additional calls to 911, kinder morgan contract osro's were also made and the kmcc emergency response plan was implemented. When local operations anticipated cost of repair to exceed $50k, a call was made to the national response center at 2130 on 6/22/2022 (nrc#1339540). The source of the release was identified as a crack on the pipeline. The failed section of pipe was cut out and replaced. The failed section was sent off for a metallurgical analysis to determine the root cause failure. The root cause and updated property damage costs will be provided in a future supplemental and final 7000.1 report. Update 09/2/2022 metallurgical analysis concluded the crack started at a location where the welder stopped and restarted during initial construction in 1952. The crack expanded from that spot over time due to cyclical stresses. . It is assumed that in 1952 no x-ray took place that potentially could have identified a crack that resulted in a failure 70 years after construction was completed. (g6 - incorrect operation; equipment not installed properly)(contributing factor - inadequate procedure)
Detailed record list
Report Received Date
2022-07-22 00:00:00
Iyear
2022
Report Number
20220157
Supplemental Number
37069
Report Type
Supplemental Final
Operator Id
Name
Kinder Morgan Crude And Condensate Llc
Operator Street Address
1001 Louisiana St., Suite 1000
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2022-06-22 11:30:00
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
13.92
Recovered Bbls
11.9
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Air Patrol
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2022-06-22 12:15:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Status When Identified
Routine Shutdown
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Initial Responder Com Datetime
2022-06-22 13:00:00
On Site Datetime
2022-06-22 12:15:00
Confirmed Discovery Datetime
2022-06-22 12:15:00
Nrc Rpt Datetime
2022-06-22 21:30:00
Nrc Rpt Num
Additional Nrc Report Numbers
1339696
Ignite Ind
No
Upstream Action Taken
Valve Closure
Upstream Valve Close Datetime
2022-06-22 11:37:00
Upstream Valve Type Ind
Remotely Controlled
Downstream Action Taken
Valve Closure
Downstream Vlv Close Datetime
2022-06-22 11:40:00
Downstream Valve Type Ind
Remotely Controlled
Notify Qualified Indiv Ind
Yes
Qualified Indiv Notif Datetime
2022-06-22 11:30:00
Oil Spill Removal Org Ind
Yes
Osro Activated Datetime
2022-06-22 12:30:00
Osro Arrived On Site Dt
6/22/2022 13:30
Num Pub Evacuated
0
Pipe Fac Name
Dewitt To Oil Tanking
Segment Name
30" Edna To Missouri City
Onshore State Abbreviation
Tx
Onshore Postal Code
77957
Onshore City Name
Edna
Onshore County Name
Jackson
Designated Location
Milepost
Designated Name
53.47
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
36
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Seam
Pipe Diameter
30
Pipe Wall Thickness
0.344
Pipe Smys
52000
Pipe Specification
X52
Pipe Seam Type
Dsaw
Pipe Manufacturer
Unknown
Pipe Coating Type
Coal Tar
Coating Applied Ind
Unknown
Installation Year
1952
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Crack
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
10000
Est Cost Gas Released
1482
Est Cost Prop Damage
488470
Est Cost Emergency
96135
Est Cost Environmental
225807
Est Cost Other
0
Prpty
821894
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
119
Mop Psig
858
Mop Cfr Section
Internal Design Pressure �195.406(A)(1)
Maop Established Date
2019-02-23 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
247616
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
Yes
Cpm In Place Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind
Yes
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Equipment Not Installed Properly
Operation Type
Equipment Not Installed Properly
Related Inadequate Proc Ind
Yes
Category Type
Construction
Operator Qualification Ind
No
Preparer Name
J**** P*******
Preparer Title
Specialist - Technical Compliance Code St Sr Ii
Preparer Email
J*************@k***********.com
Preparer Telephone
7134207004
Prepared Date
2022-09-02 00:00:00
Local Contact Name
J****** O**
Local Contact Email
J**********@k***********.com
Local Contact Telephone
9795318137
Authorizer Name
D******* S*******
Authorizer Telephone
7134206496
Authorizer Title
Manager - Compliance Code St
Authorizer Email
D****************@k***********.com
Narrative
06/22/2022- an aerial patrol pilot notified kinder morgan crude and condensate operations personnel of a stain on the row on the intrastate 30 inch kmcc dewitt to oti line near the city of edna in jackson county, texas at approximately 11:30 cst. Operations dispatched personnel to the site and they confirmed a crude oil release at 12:15pm cst. The pipeline was already on a scheduled shutdown at the time of the reported staining. Based on initial estimate of a crude oil release greater than 5 gallons, a telephonic notification was made to the railroad commission of texas's emergency line. Additional calls to 911, kinder morgan contract osro's were also made and the kmcc emergency response plan was implemented. When local operations anticipated cost of repair to exceed $50k, a call was made to the national response center at 2130 on 6/22/2022 (nrc#1339540). The source of the release was identified as a crack on the pipeline. The failed section of pipe was cut out and replaced. The failed section was sent off for a metallurgical analysis to determine the root cause failure. The root cause and updated property damage costs will be provided in a future supplemental and final 7000.1 report. Update 09/2/2022 metallurgical analysis concluded the crack started at a location where the welder stopped and restarted during initial construction in 1952. The crack expanded from that spot over time due to cyclical stresses. . It is assumed that in 1952 no x-ray took place that potentially could have identified a crack that resulted in a failure 70 years after construction was completed. (g6 - incorrect operation; equipment not installed properly)(contributing factor - inadequate procedure)
Report Received Date 2022-07-22 00:00:00
Iyear 2022
Report Number 20220157
Supplemental Number 37069
Report Type Supplemental Final
Operator Id 32678 PHMSA Enforcement
Name Kinder Morgan Crude And Condensate Llc
Operator Street Address 1001 Louisiana St., Suite 1000
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2022-06-22 11:30:00
Time Zone Central
Daylight Savings Ind Yes
Location Latitude 28.93896 Google Maps OpenStreetMap
Location Longitude -96.584013 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 13.92
Recovered Bbls 11.9
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Air Patrol
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2022-06-22 12:15:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Status When Identified Routine Shutdown
Communication State Fed Ind Yes
Party Initiated Communication Operator
Initial Responder Com Datetime 2022-06-22 13:00:00
On Site Datetime 2022-06-22 12:15:00
Confirmed Discovery Datetime 2022-06-22 12:15:00
Nrc Rpt Datetime 2022-06-22 21:30:00
Nrc Rpt Num 1339540 NRC Report How to search
Additional Nrc Report Numbers 1339696
Ignite Ind No
Upstream Action Taken Valve Closure
Upstream Valve Close Datetime 2022-06-22 11:37:00
Upstream Valve Type Ind Remotely Controlled
Downstream Action Taken Valve Closure
Downstream Vlv Close Datetime 2022-06-22 11:40:00
Downstream Valve Type Ind Remotely Controlled
Notify Qualified Indiv Ind Yes
Qualified Indiv Notif Datetime 2022-06-22 11:30:00
Oil Spill Removal Org Ind Yes
Osro Activated Datetime 2022-06-22 12:30:00
Osro Arrived On Site Dt 6/22/2022 13:30
Num Pub Evacuated 0
Pipe Fac Name Dewitt To Oil Tanking
Segment Name 30" Edna To Missouri City
Onshore State Abbreviation Tx
Onshore Postal Code 77957
Onshore City Name Edna
Onshore County Name Jackson
Designated Location Milepost
Designated Name 53.47
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 36
Crossing No
Pipe Facility Type Intrastate
Item Involved Pipe
Pipe Type Pipe Seam
Pipe Diameter 30
Pipe Wall Thickness 0.344
Pipe Smys 52000
Pipe Specification X52
Pipe Seam Type Dsaw
Pipe Manufacturer Unknown
Pipe Coating Type Coal Tar
Coating Applied Ind Unknown
Installation Year 1952
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Crack
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 10000
Est Cost Gas Released 1482
Est Cost Prop Damage 488470
Est Cost Emergency 96135
Est Cost Environmental 225807
Est Cost Other 0
Prpty 821894
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 119
Mop Psig 858
Mop Cfr Section Internal Design Pressure �195.406(A)(1) View CFR 49 §192
Maop Established Date 2019-02-23 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 247616
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind Yes
Cpm In Place Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind Yes
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Equipment Not Installed Properly
Operation Type Equipment Not Installed Properly
Related Inadequate Proc Ind Yes
Category Type Construction
Operator Qualification Ind No
Preparer Name J**** P*******
Preparer Title Specialist - Technical Compliance Code St Sr Ii
Preparer Email J*************@k***********.com
Preparer Telephone 7134207004
Prepared Date 2022-09-02 00:00:00
Local Contact Name J****** O**
Local Contact Email J**********@k***********.com
Local Contact Telephone 9795318137
Authorizer Name D******* S*******
Authorizer Telephone 7134206496
Authorizer Title Manager - Compliance Code St
Authorizer Email D****************@k***********.com
Narrative 06/22/2022- an aerial patrol pilot notified kinder morgan crude and condensate operations personnel of a stain on the row on the intrastate 30 inch kmcc dewitt to oti line near the city of edna in jackson county, texas at approximately 11:30 cst. Operations dispatched personnel to the site and they confirmed a crude oil release at 12:15pm cst. The pipeline was already on a scheduled shutdown at the time of the reported staining. Based on initial estimate of a crude oil release greater than 5 gallons, a telephonic notification was made to the railroad commission of texas's emergency line. Additional calls to 911, kinder morgan contract osro's were also made and the kmcc emergency response plan was implemented. When local operations anticipated cost of repair to exceed $50k, a call was made to the national response center at 2130 on 6/22/2022 (nrc#1339540). The source of the release was identified as a crack on the pipeline. The failed section of pipe was cut out and replaced. The failed section was sent off for a metallurgical analysis to determine the root cause failure. The root cause and updated property damage costs will be provided in a future supplemental and final 7000.1 report. Update 09/2/2022 metallurgical analysis concluded the crack started at a location where the welder stopped and restarted during initial construction in 1952. The crack expanded from that spot over time due to cyclical stresses. . It is assumed that in 1952 no x-ray took place that potentially could have identified a crack that resulted in a failure 70 years after construction was completed. (g6 - incorrect operation; equipment not installed properly)(contributing factor - inadequate procedure)

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