HL incident on 2022-06-23 — TX

Operator
Enbridge Energy, Limited Partnership
Cause
Incorrect Operation
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2022-06-23 14:20
Report number
Location
TX
Narrative
On june 23, 2022 at approximately 2:20 pm cdt, while performing open system maintenance work, crews experienced a release of 7 barrels of crude oil within manifold 201 at flanagan terminal due to a passing isolation valve. Incoming and outgoing lines at flanagan terminal were already shut down for scheduled maintenance activities. Plm crews were on-site with vac trucks to recover impacted soil. A contractor was also mobilized with additional clean up and recovery equipment. The nrc was notified on june 23, 2022 at 3:05 pm cdt (report #1339619). A 48-hour nrc notification was made on june 25, 2022 at 12:11 pm cdt (report #1339763). The cause of the release was due to incorrectly disassembling a flange connection on valve 201-v-2023. The valve was repaired, and all lines were returned to service. Approximately 12 yards of contaminated soil was removed from the release site.
Detailed record list
Report Received Date
2022-07-21 00:00:00
Iyear
2022
Report Number
20220156
Supplemental Number
36886
Report Type
Original Final
Operator Id
Name
Enbridge Energy, Limited Partnership
Operator Street Address
915 N Eldridge Parkway, Suite 1100
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77079
Local Datetime
2022-06-23 14:20:00
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
7
Recovered Bbls
7
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2022-06-23 14:20:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
No
Shutdown Explain
Scheduled Shut Down For Maintenance Activity
Communication State Fed Ind
No
On Site Datetime
2022-06-23 14:20:00
Confirmed Discovery Datetime
2022-06-23 14:20:00
Nrc Rpt Datetime
2022-06-23 15:03:00
Nrc Rpt Num
Additional Nrc Report Numbers
1339763
Ignite Ind
No
Notify Qualified Indiv Ind
Yes
Qualified Indiv Notif Datetime
2022-06-23 14:30:00
Oil Spill Removal Org Ind
Yes
Osro Activated Datetime
2022-06-23 14:30:00
Osro Arrived On Site Dt
6/23/2022 14:30
Num Pub Evacuated
0
Pipe Fac Name
Flanagan Terminal
Segment Name
Valve 201-V-2023
Onshore State Abbreviation
Il
Onshore Postal Code
61740
Onshore City Name
Livingston
Onshore County Name
Pontiac
Designated Location
Milepost
Designated Name
Fn
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Installation Year
2022
Manufactured Year
2022
Material Involved
Carbon Steel
Release Type
Other
Release Type Details
Disassembling Flange
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
735
Est Cost Prop Damage
0
Est Cost Emergency
21640
Est Cost Environmental
209400
Est Cost Other
0
Prpty
231775
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
0
Mop Psig
275
Mop Cfr Section
Component Design Pressure �195.406(A)(2)
Maop Established Date
2021-09-20 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The release was due to incorrect disassembling of a flange connection during field work on an open system
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Other Incorrect Operation
Operation Type
Other Incorrect Operation
Operation Details
Incorrectly Disassembled Flange Connection
Related Failure Follow Ind
Yes
Category Type
Other Maintenance
Operator Qualification Ind
No
Preparer Name
S**** S****
Preparer Title
Sr Compliance Analyst
Preparer Email
S**********@e*******.com
Preparer Telephone
715-395-3620
Prepared Date
2022-07-21 00:00:00
Authorizer Name
S**** D*****
Authorizer Telephone
715-394-1405
Authorizer Title
Supervisor Us Pipeline Compliance
Authorizer Email
S************@e*******.com
Narrative
On june 23, 2022 at approximately 2:20 pm cdt, while performing open system maintenance work, crews experienced a release of 7 barrels of crude oil within manifold 201 at flanagan terminal due to a passing isolation valve. Incoming and outgoing lines at flanagan terminal were already shut down for scheduled maintenance activities. Plm crews were on-site with vac trucks to recover impacted soil. A contractor was also mobilized with additional clean up and recovery equipment. The nrc was notified on june 23, 2022 at 3:05 pm cdt (report #1339619). A 48-hour nrc notification was made on june 25, 2022 at 12:11 pm cdt (report #1339763). The cause of the release was due to incorrectly disassembling a flange connection on valve 201-v-2023. The valve was repaired, and all lines were returned to service. Approximately 12 yards of contaminated soil was removed from the release site.
Report Received Date 2022-07-21 00:00:00
Iyear 2022
Report Number 20220156
Supplemental Number 36886
Report Type Original Final
Operator Id 11169 PHMSA Enforcement
Name Enbridge Energy, Limited Partnership
Operator Street Address 915 N Eldridge Parkway, Suite 1100
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77079
Local Datetime 2022-06-23 14:20:00
Time Zone Central
Daylight Savings Ind Yes
Location Latitude 40.942956 Google Maps OpenStreetMap
Location Longitude -88.647229 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 7
Recovered Bbls 7
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2022-06-23 14:20:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Status When Identified Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind No
Shutdown Explain Scheduled Shut Down For Maintenance Activity
Communication State Fed Ind No
On Site Datetime 2022-06-23 14:20:00
Confirmed Discovery Datetime 2022-06-23 14:20:00
Nrc Rpt Datetime 2022-06-23 15:03:00
Nrc Rpt Num 1339619 NRC Report How to search
Additional Nrc Report Numbers 1339763
Ignite Ind No
Notify Qualified Indiv Ind Yes
Qualified Indiv Notif Datetime 2022-06-23 14:30:00
Oil Spill Removal Org Ind Yes
Osro Activated Datetime 2022-06-23 14:30:00
Osro Arrived On Site Dt 6/23/2022 14:30
Num Pub Evacuated 0
Pipe Fac Name Flanagan Terminal
Segment Name Valve 201-V-2023
Onshore State Abbreviation Il
Onshore Postal Code 61740
Onshore City Name Livingston
Onshore County Name Pontiac
Designated Location Milepost
Designated Name Fn
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Installation Year 2022
Manufactured Year 2022
Material Involved Carbon Steel
Release Type Other
Release Type Details Disassembling Flange
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 735
Est Cost Prop Damage 0
Est Cost Emergency 21640
Est Cost Environmental 209400
Est Cost Other 0
Prpty 231775
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 0
Mop Psig 275
Mop Cfr Section Component Design Pressure �195.406(A)(2) View CFR 49 §192
Maop Established Date 2021-09-20 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The release was due to incorrect disassembling of a flange connection during field work on an open system
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Other Incorrect Operation
Operation Type Other Incorrect Operation
Operation Details Incorrectly Disassembled Flange Connection
Related Failure Follow Ind Yes
Category Type Other Maintenance
Operator Qualification Ind No
Preparer Name S**** S****
Preparer Title Sr Compliance Analyst
Preparer Email S**********@e*******.com
Preparer Telephone 715-395-3620
Prepared Date 2022-07-21 00:00:00
Authorizer Name S**** D*****
Authorizer Telephone 715-394-1405
Authorizer Title Supervisor Us Pipeline Compliance
Authorizer Email S************@e*******.com
Narrative On june 23, 2022 at approximately 2:20 pm cdt, while performing open system maintenance work, crews experienced a release of 7 barrels of crude oil within manifold 201 at flanagan terminal due to a passing isolation valve. Incoming and outgoing lines at flanagan terminal were already shut down for scheduled maintenance activities. Plm crews were on-site with vac trucks to recover impacted soil. A contractor was also mobilized with additional clean up and recovery equipment. The nrc was notified on june 23, 2022 at 3:05 pm cdt (report #1339619). A 48-hour nrc notification was made on june 25, 2022 at 12:11 pm cdt (report #1339763). The cause of the release was due to incorrectly disassembling a flange connection on valve 201-v-2023. The valve was repaired, and all lines were returned to service. Approximately 12 yards of contaminated soil was removed from the release site.

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