HL incident on 2022-06-09 — TX

Operator
Shell Pipeline Co., L.p.
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$336,524
Incident datetime
2022-06-09 00:30
Report number
Location
TX
Narrative
On 6/9/22, around 12:30 am, an operator was dispatched to check an excessive sump pump running alarm at colex east tank farm. After checking the sump pump, the operator made a round by the manifold and discovered a small puddle of gasoline collecting near the interface of some below-ground piping. The operator notified supervision and it was determined to keep an eye on the location until daylight for further evaluation. At 7:40 the same day, it was determined to dig up the area and locate the source of the leak, and this time it was identified the costs would exceed $50k, and then the call to the nrc was made. Concerning cpm, the leak occurred on facility piping near the manifold and that doesn't fall under the cpm installed. In saying that, there is terminal balance leak detection primarily based on the ehh on the tanks. This system is designed to pick up a much larger release. After the investigation, it was determined the gasket failed from improper alignment from the original installation date.
Detailed record list
Report Received Date
2022-07-07 00:00:00
Iyear
2022
Report Number
20220142
Supplemental Number
37005
Report Type
Supplemental Final
Operator Id
Name
Shell Pipeline Co., L.p.
Operator Street Address
150 North Dairy Ashford Road Wck Bldg. A
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77079
Local Datetime
2022-06-09 07:40:00
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
2.1
Recovered Bbls
2.1
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Or Pack Calculations)
Incident Identified Datetime
2022-06-09 00:30:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2022-06-09 00:45:00
Restart Datetime
2022-07-07 08:00:00
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Initial Responder Com Datetime
2022-06-09 08:05:00
On Site Datetime
2022-06-09 00:30:00
Confirmed Discovery Datetime
2022-06-09 00:40:00
Nrc Rpt Datetime
2022-06-09 08:40:00
Nrc Rpt Num
Additional Nrc Report Numbers
1338460
Ignite Ind
No
Notify Qualified Indiv Ind
Yes
Qualified Indiv Notif Datetime
2022-06-09 07:40:00
Oil Spill Removal Org Ind
Yes
Osro Activated Datetime
2022-06-09 08:10:00
Osro Arrived On Site Dt
6/9/2022 9:10
Num Pub Evacuated
0
Pipe Fac Name
Colex East Tank Farm
Segment Name
Colex East Tank Farm
Onshore State Abbreviation
Tx
Onshore Postal Code
77506
Onshore City Name
Pasadena
Onshore County Name
Harris
Designated Location
Survey Station No.
Designated Name
Colex East
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
144
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Flange Assembly
Installation Year
1973
Manufactured Year
1973
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
400
Est Cost Prop Damage
336524
Est Cost Emergency
91076
Est Cost Environmental
0
Est Cost Other
0
Prpty
428000
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
30
Mop Psig
275
Mop Cfr Section
Component Design Pressure �195.406(A)(2)
Maop Established Date
1973-01-01 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
Yes, but the investigation of the control room and/or controller actions has not yet been completed by the operator (supplemental report required)
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
Gasket
Ief Addl Misalignment Ind
Yes
Preparer Name
J***** H*****
Preparer Title
Operations Support Coordinator
Preparer Email
J************@s****.com
Preparer Telephone
4095402781
Prepared Date
2022-08-22 00:00:00
Local Contact Name
J***** H*****
Local Contact Email
J************@s****.com
Local Contact Telephone
4095402781
Authorizer Name
D****** P****
Authorizer Telephone
832-762-2553
Authorizer Title
Integrity And Regulatory Services Manager
Authorizer Email
D************@s****.com
Narrative
On 6/9/22, around 12:30 am, an operator was dispatched to check an excessive sump pump running alarm at colex east tank farm. After checking the sump pump, the operator made a round by the manifold and discovered a small puddle of gasoline collecting near the interface of some below-ground piping. The operator notified supervision and it was determined to keep an eye on the location until daylight for further evaluation. At 7:40 the same day, it was determined to dig up the area and locate the source of the leak, and this time it was identified the costs would exceed $50k, and then the call to the nrc was made. Concerning cpm, the leak occurred on facility piping near the manifold and that doesn't fall under the cpm installed. In saying that, there is terminal balance leak detection primarily based on the ehh on the tanks. This system is designed to pick up a much larger release. After the investigation, it was determined the gasket failed from improper alignment from the original installation date.
Report Received Date 2022-07-07 00:00:00
Iyear 2022
Report Number 20220142
Supplemental Number 37005
Report Type Supplemental Final
Operator Id 31174 PHMSA Enforcement
Name Shell Pipeline Co., L.p.
Operator Street Address 150 North Dairy Ashford Road Wck Bldg. A
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77079
Local Datetime 2022-06-09 07:40:00
Time Zone Central
Daylight Savings Ind Yes
Location Latitude 29.71722 Google Maps OpenStreetMap
Location Longitude -95.17361 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 2.1
Recovered Bbls 2.1
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Or Pack Calculations)
Incident Identified Datetime 2022-06-09 00:30:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Status When Identified Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind Yes
Shutdown Datetime 2022-06-09 00:45:00
Restart Datetime 2022-07-07 08:00:00
Communication State Fed Ind Yes
Party Initiated Communication Operator
Initial Responder Com Datetime 2022-06-09 08:05:00
On Site Datetime 2022-06-09 00:30:00
Confirmed Discovery Datetime 2022-06-09 00:40:00
Nrc Rpt Datetime 2022-06-09 08:40:00
Nrc Rpt Num 1338227 NRC Report How to search
Additional Nrc Report Numbers 1338460
Ignite Ind No
Notify Qualified Indiv Ind Yes
Qualified Indiv Notif Datetime 2022-06-09 07:40:00
Oil Spill Removal Org Ind Yes
Osro Activated Datetime 2022-06-09 08:10:00
Osro Arrived On Site Dt 6/9/2022 9:10
Num Pub Evacuated 0
Pipe Fac Name Colex East Tank Farm
Segment Name Colex East Tank Farm
Onshore State Abbreviation Tx
Onshore Postal Code 77506
Onshore City Name Pasadena
Onshore County Name Harris
Designated Location Survey Station No.
Designated Name Colex East
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 144
Crossing No
Pipe Facility Type Interstate
Item Involved Flange Assembly
Installation Year 1973
Manufactured Year 1973
Material Involved Carbon Steel
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Usa Drinking Ind Yes
Usa Drinking Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 400
Est Cost Prop Damage 336524
Est Cost Emergency 91076
Est Cost Environmental 0
Est Cost Other 0
Prpty 428000
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 30
Mop Psig 275
Mop Cfr Section Component Design Pressure �195.406(A)(2) View CFR 49 §192
Maop Established Date 1973-01-01 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status Yes, but the investigation of the control room and/or controller actions has not yet been completed by the operator (supplemental report required)
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind Gasket
Ief Addl Misalignment Ind Yes
Preparer Name J***** H*****
Preparer Title Operations Support Coordinator
Preparer Email J************@s****.com
Preparer Telephone 4095402781
Prepared Date 2022-08-22 00:00:00
Local Contact Name J***** H*****
Local Contact Email J************@s****.com
Local Contact Telephone 4095402781
Authorizer Name D****** P****
Authorizer Telephone 832-762-2553
Authorizer Title Integrity And Regulatory Services Manager
Authorizer Email D************@s****.com
Narrative On 6/9/22, around 12:30 am, an operator was dispatched to check an excessive sump pump running alarm at colex east tank farm. After checking the sump pump, the operator made a round by the manifold and discovered a small puddle of gasoline collecting near the interface of some below-ground piping. The operator notified supervision and it was determined to keep an eye on the location until daylight for further evaluation. At 7:40 the same day, it was determined to dig up the area and locate the source of the leak, and this time it was identified the costs would exceed $50k, and then the call to the nrc was made. Concerning cpm, the leak occurred on facility piping near the manifold and that doesn't fall under the cpm installed. In saying that, there is terminal balance leak detection primarily based on the ehh on the tanks. This system is designed to pick up a much larger release. After the investigation, it was determined the gasket failed from improper alignment from the original installation date.

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