GTG incident on 2022-11-11 — OK

Operator
Enlink Processing Services, Llc
Cause
Other Outside Force Damage
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$36,898
Incident datetime
2022-11-11 23:30
Report number
Location
OK
Narrative
A landowner was burning his field when the fire spread to the wooden pipeline support structure. When the support structure was destroyed, the above ground piping collapsed. This caused the piping to separate at an insulating flange, which then released and ignited the gas in the pipeline.
Detailed record list
Report Received Date
2022-12-09 00:00:00
Iyear
2022
Report Number
20220129
Supplemental Number
37713
Report Type
Supplemental Final
Operator Id
Name
Enlink Processing Services, Llc
Operator Street Address
100 West 5th St.
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2022-11-11 23:30:00
Time Zone
Central
Daylight Savings Ind
No
Location Latitude
Location Longitude
Nrc Rpt Num
Nrc Rpt Datetime
2022-11-12 02:23:00
Additional Nrc Report Numbers
1352481
Commodity Released Type
Natural Gas
Unintentional Release
20420
Intentional Release
34843
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Status When Identified
Idle
Ignite Ind
Yes
Ignite Datetime
2022-11-11 23:30:00
How Extinguished
Allowed To Burn Out
Gas Consumed By Fire In Mcf
20420
Explode Ind
No
Upstream Action Taken
Valve Closure
Upstream Valve Close Datetime
2022-11-12 01:37:00
Downstream Action Taken
Valve Closure
Downstream Vlv Close Datetime
2022-11-12 01:40:00
Num Pub Evacuated
0
Incident Identified Datetime
2022-11-11 23:30:00
On Site Datetime
2022-11-12 03:50:00
On Off Shore
Onshore
Onshore State Abbreviation
La
Onshore Postal Code
70548
Onshore City Name
Not Within A Municipality
Onshore County Name
Vermilion
Designated Location
Not Applicable
Pipe Fac Name
P1122 Florence 6" Lateral
Segment Name
P1122 Florence 6" Lateral
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
System Part Involved
Onshore Pipeline, Including Valve Sites
Item Involved
Scraper/pig Trap
Installation Year
1977
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Connection Failure
Class Location Type
Class 1 Location
Could Be Hca
No
Pir Radius
146
Heat Damage Ind
No
Non Heat Damage Ind
No
Did Occur In Mca Ind
No
Est Cost Oper Paid
0
Est Cost Unintentional Release
135589
Est Cost Intentional Release
231358
Est Cost Prop Damage
36898
Est Cost Emergency
0
Est Cost Other
0
Gas Cost In Mcf
6.64
Prpty
403845
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Wildlife Impact Ind
No
Accident Psig
885
Gas Flow In Pipe In Mcf
42.4
Mop Psig
1100
Mop Cfr Section
192.619(A)(2)
Maop Established Date
1977-11-01 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Gas Required Odorized Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Length Segment Isolated
204811
Internal Inspection Ind
No
Other Inspection Ind
Yes
Internal Inspection Details
Pipeline Is Now Shutdown. Was Not In Use At The Time Of The Incident.
Operation Complications Ind
Yes
Low Flow Ind
Yes
Pipeline Function
Transmission System
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Accident Identifier
Notification From Emergency Responder
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Control room personnel responded to the loss of pressure as expected. Incident was not caused by controller action.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Other Outside Force Damage
Cause Details
Nearby Industrial, Man-Made, Or Other Fire/explosion As Primary Cause Of Incident
Outside Force Type
Nearby Industrial, Man-Made, Or Other Fire/explosion As Primary Cause Of Incident
Preparer Name
C****** T******
Preparer Title
Sr. Dot Specialist
Preparer Email
C**************@e*****.com
Preparer Telephone
3373226682
Local Contact Name
C****** T******
Local Contact Email
C**************@e*****.com
Local Contact Telephone
3373226682
Authorizer Name
C****** T******
Authorizer Title
Sr. Dot Specialist
Authorizer Telephone
3373226682
Authorizer Email
C**************@e*****.com
Narrative
A landowner was burning his field when the fire spread to the wooden pipeline support structure. When the support structure was destroyed, the above ground piping collapsed. This caused the piping to separate at an insulating flange, which then released and ignited the gas in the pipeline.
Report Received Date 2022-12-09 00:00:00
Iyear 2022
Report Number 20220129
Supplemental Number 37713
Report Type Supplemental Final
Operator Id 32005 PHMSA Enforcement
Name Enlink Processing Services, Llc
Operator Street Address 100 West 5th St.
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74103
Local Datetime 2022-11-11 23:30:00
Time Zone Central
Daylight Savings Ind No
Location Latitude 29.86243 Google Maps OpenStreetMap
Location Longitude -92.447134 Google Maps OpenStreetMap
Nrc Rpt Num 1352375 NRC Report How to search
Nrc Rpt Datetime 2022-11-12 02:23:00
Additional Nrc Report Numbers 1352481
Commodity Released Type Natural Gas
Unintentional Release 20420
Intentional Release 34843
Accompanying Liquid 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Status When Identified Idle
Ignite Ind Yes
Ignite Datetime 2022-11-11 23:30:00
How Extinguished Allowed To Burn Out
Gas Consumed By Fire In Mcf 20420
Explode Ind No
Upstream Action Taken Valve Closure
Upstream Valve Close Datetime 2022-11-12 01:37:00
Downstream Action Taken Valve Closure
Downstream Vlv Close Datetime 2022-11-12 01:40:00
Num Pub Evacuated 0
Incident Identified Datetime 2022-11-11 23:30:00
On Site Datetime 2022-11-12 03:50:00
On Off Shore Onshore
Onshore State Abbreviation La
Onshore Postal Code 70548
Onshore City Name Not Within A Municipality
Onshore County Name Vermilion
Designated Location Not Applicable
Pipe Fac Name P1122 Florence 6" Lateral
Segment Name P1122 Florence 6" Lateral
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
System Part Involved Onshore Pipeline, Including Valve Sites
Item Involved Scraper/pig Trap
Installation Year 1977
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Connection Failure
Class Location Type Class 1 Location
Could Be Hca No
Pir Radius 146
Heat Damage Ind No
Non Heat Damage Ind No
Did Occur In Mca Ind No
Est Cost Oper Paid 0
Est Cost Unintentional Release 135589
Est Cost Intentional Release 231358
Est Cost Prop Damage 36898
Est Cost Emergency 0
Est Cost Other 0
Gas Cost In Mcf 6.64
Prpty 403845
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Wildlife Impact Ind No
Accident Psig 885
Gas Flow In Pipe In Mcf 42.4
Mop Psig 1100
Mop Cfr Section 192.619(A)(2) View CFR 49 §192
Maop Established Date 1977-11-01 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Gas Required Odorized Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Length Segment Isolated 204811
Internal Inspection Ind No
Other Inspection Ind Yes
Internal Inspection Details Pipeline Is Now Shutdown. Was Not In Use At The Time Of The Incident.
Operation Complications Ind Yes
Low Flow Ind Yes
Pipeline Function Transmission System
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Accident Identifier Notification From Emergency Responder
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Control room personnel responded to the loss of pressure as expected. Incident was not caused by controller action.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Other Outside Force Damage
Cause Details Nearby Industrial, Man-Made, Or Other Fire/explosion As Primary Cause Of Incident
Outside Force Type Nearby Industrial, Man-Made, Or Other Fire/explosion As Primary Cause Of Incident
Preparer Name C****** T******
Preparer Title Sr. Dot Specialist
Preparer Email C**************@e*****.com
Preparer Telephone 3373226682
Local Contact Name C****** T******
Local Contact Email C**************@e*****.com
Local Contact Telephone 3373226682
Authorizer Name C****** T******
Authorizer Title Sr. Dot Specialist
Authorizer Telephone 3373226682
Authorizer Email C**************@e*****.com
Narrative A landowner was burning his field when the fire spread to the wooden pipeline support structure. When the support structure was destroyed, the above ground piping collapsed. This caused the piping to separate at an insulating flange, which then released and ignited the gas in the pipeline.

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