GTG incident on 2022-09-29 — TX

Operator
Anr Pipeline Co
Cause
Incorrect Operation
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 1 injury
Property damage (nominal)
$1,300,000
Incident datetime
2022-09-29 15:40
Report number
Location
TX
Narrative
On 29 september 2022, tc energy technicians were performing a corrective work order to replace the hydraulic fluid in the 501-45a-34 valve. While performing the work, an incident occurred resulting in injuries and a release of gas. The incident was reported to the national response center, #1348627. The anr 2-501 pipeline mp582.6 to mp585.1 - 2-501 loop south end to mainline valve 46 (isolated segment), has been blown down and isolated. In addition, tc energy has suspended qualifications on covered tasks associated with the work being performed associated with the incident and conducted drug testing. The pipeline segment remained out of service until repair of the pipeline was completed. Repair to the pipeline included the replacement of the valve and valve operator. The pipeline was restarted and returned to full service on january 13, 2023 at 11:39 cst. The primary cause of the failure has been determined to be the result of the technician failing to confirm manufacturer's repair procedure and opening the valve during corrective maintenance to replace the hydraulic hand pump. Following the repair, when the valve was actuated using the hand pump, hydraulic oil began to move to the open side of the valve stem and the valve gate disengaged and moved in an uncontrolled manner. The result of this action caused a failure in the valve actuator connection and a release of pipeline fluids and hydraulic oil to the surrounding area.
Detailed record list
Report Received Date
2022-10-28 00:00:00
Iyear
2022
Report Number
20220113
Supplemental Number
37725
Report Type
Supplemental Final
Operator Id
Name
Anr Pipeline Co
Operator Street Address
700 Louisiana Street Suite 700
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2022-09-29 15:40:00
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Nrc Rpt Num
Nrc Rpt Datetime
2022-09-29 16:30:00
Additional Nrc Report Numbers
1348783
Commodity Released Type
Natural Gas
Unintentional Release
189
Intentional Release
3677
Accompanying Liquid
0.1
Fatality Ind
No
Fatal
0
Injury Ind
Yes
Num Emp Injuries
1
Num Contr Injuries
0
Num Er Injuries
0
Num Worker Injuries
0
Num Gp Injuries
0
Injure
1
Status When Identified
Normal Operation, Includes Pauses During Maintenance
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2022-09-29 18:39:00
Restart Datetime
2023-01-13 11:39:00
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Initial Responder Com Datetime
2022-09-29 16:30:00
Ignite Ind
No
Upstream Action Taken
Valve Closure
Upstream Valve Close Datetime
2022-09-29 16:46:00
Downstream Action Taken
Valve Closure
Downstream Vlv Close Datetime
2022-09-29 16:39:00
Num Pub Evacuated
1
Incident Identified Datetime
2022-09-29 15:40:00
On Site Datetime
2022-09-29 15:40:00
On Off Shore
Onshore
Onshore State Abbreviation
Ky
Onshore Postal Code
42327
Onshore City Name
Not Within A Municipality
Onshore County Name
Mclean
Designated Location
Milepost
Designated Name
582.6
Pipe Fac Name
Mainline Valve 45a
Segment Name
8245501-Anr Mainline Loop 2 2-501 Mlv 45
Federal
No
Location Type
Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
20
Other Underground Facilities
No
Crossing
No
Pipe Facility Type
Interstate
System Part Involved
Onshore Pipeline, Including Valve Sites
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Installation Year
1986
Manufactured Year
1986
Material Involved
Carbon Steel
Release Type
Other
Release Type Details
Valve Failure
Class Location Type
Class 1 Location
Could Be Hca
No
Pir Radius
830
Heat Damage Ind
No
Non Heat Damage Ind
No
Hca Fatalities Ind
No
Did Occur In Mca Ind
No
Est Cost Oper Paid
0
Est Cost Unintentional Release
1300
Est Cost Intentional Release
25298
Est Cost Prop Damage
1300000
Est Cost Emergency
10000
Est Cost Other
100000
Est Cost Other Details
Laboratory And Investigation Costs
Gas Cost In Mcf
6.88
Prpty
1436598
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
1
Num Business Building Affctd
0
Wildlife Impact Ind
No
Accident Psig
580
Gas Flow In Pipe In Mcf
385
Mop Psig
858
Mop Cfr Section
192.619(A)(1)
Maop Established Date
1972-10-12 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Gas Required Odorized Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Length Segment Isolated
12277
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
Transmission System
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The incident occurred during maintenance operations while technicians were at the facility.
Employee Drug Test Ind
Yes
Contractor Drug Test Ind
No
Num Employees Tested
2
Num Employees Failed
0
Cause
Incorrect Operation
Cause Details
Other Incorrect Operation
Operation Type
Other Incorrect Operation
Operation Details
Technician Believed That Valve Needed To Be Closed During The Corrective Maintenance Of Replacing The Dhv Hand Pump. Technician Did Not Become Aware Of The Shafer Dhv Hand Pump Installation Procedure That Included A Note To Have The Valve Open At The Start Of Maintenance.
Related Inadequate Proc Ind
Yes
Related Failure Follow Ind
Yes
Category Type
Other Maintenance
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
R**** R S*****
Preparer Title
Manager Us Regulatory Compliance West
Preparer Email
R***********@t*******.com
Preparer Telephone
16154655123
Local Contact Name
R**** R S*****
Local Contact Email
R***********@t*******.com
Local Contact Telephone
16154655123
Authorizer Name
P*** S******
Authorizer Title
Senior Manager Usgo Regulatory Compliance
Authorizer Telephone
304-357-2245
Authorizer Email
P***********@t*******.com
Narrative
On 29 september 2022, tc energy technicians were performing a corrective work order to replace the hydraulic fluid in the 501-45a-34 valve. While performing the work, an incident occurred resulting in injuries and a release of gas. The incident was reported to the national response center, #1348627. The anr 2-501 pipeline mp582.6 to mp585.1 - 2-501 loop south end to mainline valve 46 (isolated segment), has been blown down and isolated. In addition, tc energy has suspended qualifications on covered tasks associated with the work being performed associated with the incident and conducted drug testing. The pipeline segment remained out of service until repair of the pipeline was completed. Repair to the pipeline included the replacement of the valve and valve operator. The pipeline was restarted and returned to full service on january 13, 2023 at 11:39 cst. The primary cause of the failure has been determined to be the result of the technician failing to confirm manufacturer's repair procedure and opening the valve during corrective maintenance to replace the hydraulic hand pump. Following the repair, when the valve was actuated using the hand pump, hydraulic oil began to move to the open side of the valve stem and the valve gate disengaged and moved in an uncontrolled manner. The result of this action caused a failure in the valve actuator connection and a release of pipeline fluids and hydraulic oil to the surrounding area.
Report Received Date 2022-10-28 00:00:00
Iyear 2022
Report Number 20220113
Supplemental Number 37725
Report Type Supplemental Final
Operator Id 405 PHMSA Enforcement
Name Anr Pipeline Co
Operator Street Address 700 Louisiana Street Suite 700
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2022-09-29 15:40:00
Time Zone Central
Daylight Savings Ind Yes
Location Latitude 37.59644 Google Maps OpenStreetMap
Location Longitude -87.43407 Google Maps OpenStreetMap
Nrc Rpt Num 1348627 NRC Report How to search
Nrc Rpt Datetime 2022-09-29 16:30:00
Additional Nrc Report Numbers 1348783
Commodity Released Type Natural Gas
Unintentional Release 189
Intentional Release 3677
Accompanying Liquid 0.1
Fatality Ind No
Fatal 0
Injury Ind Yes
Num Emp Injuries 1
Num Contr Injuries 0
Num Er Injuries 0
Num Worker Injuries 0
Num Gp Injuries 0
Injure 1
Status When Identified Normal Operation, Includes Pauses During Maintenance
Shutdown Due Accident Ind Yes
Shutdown Datetime 2022-09-29 18:39:00
Restart Datetime 2023-01-13 11:39:00
Communication State Fed Ind Yes
Party Initiated Communication Operator
Initial Responder Com Datetime 2022-09-29 16:30:00
Ignite Ind No
Upstream Action Taken Valve Closure
Upstream Valve Close Datetime 2022-09-29 16:46:00
Downstream Action Taken Valve Closure
Downstream Vlv Close Datetime 2022-09-29 16:39:00
Num Pub Evacuated 1
Incident Identified Datetime 2022-09-29 15:40:00
On Site Datetime 2022-09-29 15:40:00
On Off Shore Onshore
Onshore State Abbreviation Ky
Onshore Postal Code 42327
Onshore City Name Not Within A Municipality
Onshore County Name Mclean
Designated Location Milepost
Designated Name 582.6
Pipe Fac Name Mainline Valve 45a
Segment Name 8245501-Anr Mainline Loop 2 2-501 Mlv 45
Federal No
Location Type Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 20
Other Underground Facilities No
Crossing No
Pipe Facility Type Interstate
System Part Involved Onshore Pipeline, Including Valve Sites
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Installation Year 1986
Manufactured Year 1986
Material Involved Carbon Steel
Release Type Other
Release Type Details Valve Failure
Class Location Type Class 1 Location
Could Be Hca No
Pir Radius 830
Heat Damage Ind No
Non Heat Damage Ind No
Hca Fatalities Ind No
Did Occur In Mca Ind No
Est Cost Oper Paid 0
Est Cost Unintentional Release 1300
Est Cost Intentional Release 25298
Est Cost Prop Damage 1300000
Est Cost Emergency 10000
Est Cost Other 100000
Est Cost Other Details Laboratory And Investigation Costs
Gas Cost In Mcf 6.88
Prpty 1436598
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 1
Num Business Building Affctd 0
Wildlife Impact Ind No
Accident Psig 580
Gas Flow In Pipe In Mcf 385
Mop Psig 858
Mop Cfr Section 192.619(A)(1) View CFR 49 §192
Maop Established Date 1972-10-12 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Gas Required Odorized Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Length Segment Isolated 12277
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function Transmission System
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The incident occurred during maintenance operations while technicians were at the facility.
Employee Drug Test Ind Yes
Contractor Drug Test Ind No
Num Employees Tested 2
Num Employees Failed 0
Cause Incorrect Operation
Cause Details Other Incorrect Operation
Operation Type Other Incorrect Operation
Operation Details Technician Believed That Valve Needed To Be Closed During The Corrective Maintenance Of Replacing The Dhv Hand Pump. Technician Did Not Become Aware Of The Shafer Dhv Hand Pump Installation Procedure That Included A Note To Have The Valve Open At The Start Of Maintenance.
Related Inadequate Proc Ind Yes
Related Failure Follow Ind Yes
Category Type Other Maintenance
Operator Qualification Ind Yes
Qualified Individuals Yes, They Were Qualified For The Task(S)
Preparer Name R**** R S*****
Preparer Title Manager Us Regulatory Compliance West
Preparer Email R***********@t*******.com
Preparer Telephone 16154655123
Local Contact Name R**** R S*****
Local Contact Email R***********@t*******.com
Local Contact Telephone 16154655123
Authorizer Name P*** S******
Authorizer Title Senior Manager Usgo Regulatory Compliance
Authorizer Telephone 304-357-2245
Authorizer Email P***********@t*******.com
Narrative On 29 september 2022, tc energy technicians were performing a corrective work order to replace the hydraulic fluid in the 501-45a-34 valve. While performing the work, an incident occurred resulting in injuries and a release of gas. The incident was reported to the national response center, #1348627. The anr 2-501 pipeline mp582.6 to mp585.1 - 2-501 loop south end to mainline valve 46 (isolated segment), has been blown down and isolated. In addition, tc energy has suspended qualifications on covered tasks associated with the work being performed associated with the incident and conducted drug testing. The pipeline segment remained out of service until repair of the pipeline was completed. Repair to the pipeline included the replacement of the valve and valve operator. The pipeline was restarted and returned to full service on january 13, 2023 at 11:39 cst. The primary cause of the failure has been determined to be the result of the technician failing to confirm manufacturer's repair procedure and opening the valve during corrective maintenance to replace the hydraulic hand pump. Following the repair, when the valve was actuated using the hand pump, hydraulic oil began to move to the open side of the valve stem and the valve gate disengaged and moved in an uncontrolled manner. The result of this action caused a failure in the valve actuator connection and a release of pipeline fluids and hydraulic oil to the surrounding area.

All rights reserved. Copyright © by ClearPHMSA