GTG incident on 2022-09-20 — NC

Operator
Piedmont Natural Gas Co Inc
Cause
Notification Issue
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$165,750
Incident datetime
2022-09-20 14:05
Report number
Location
NC
Narrative
A contractor damaged a 10" steel main with a trackhoe while in the process of digging a proposed retention pond. The contractor did not contact the one-call center for the area being excavated.
Detailed record list
Report Received Date
2022-10-13 00:00:00
Iyear
2022
Report Number
20220109
Supplemental Number
37431
Report Type
Supplemental Final
Operator Id
Name
Piedmont Natural Gas Co Inc
Operator Street Address
525 South Tryon Street
Operator City Name
Charlotte
Operator State Abbreviation
NC
Operator Postal Code
28202
Local Datetime
2022-09-20 14:05:00
Time Zone
Eastern
Daylight Savings Ind
No
Location Latitude
Location Longitude
Nrc Rpt Num
Nrc Rpt Datetime
2022-09-20 16:18:00
Additional Nrc Report Numbers
1347952
Commodity Released Type
Natural Gas
Unintentional Release
13029
Intentional Release
0
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Status When Identified
Normal Operation, Includes Pauses During Maintenance
Shutdown Due Accident Ind
No
Shutdown Explain
A Section Of The Pipeline Was Blocked Off.
Communication State Fed Ind
No
Ignite Ind
No
Upstream Action Taken
Valve Closure
Upstream Valve Close Datetime
2022-09-20 15:38:00
Downstream Action Taken
Valve Closure
Downstream Vlv Close Datetime
2022-09-21 19:23:00
Num Pub Evacuated
0
Incident Identified Datetime
2022-09-20 14:05:00
On Site Datetime
2022-09-20 14:11:00
On Off Shore
Onshore
Onshore State Abbreviation
Nc
Onshore Postal Code
28031
Onshore City Name
Cornelius
Onshore County Name
Mecklenburg
Designated Location
Not Applicable
Pipe Fac Name
Line 369
Segment Name
415035
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
42
Other Underground Facilities
No
Crossing
No
Pipe Facility Type
Intrastate
System Part Involved
Onshore Pipeline, Including Valve Sites
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
10
Puddle Weld Ind
No
Pipe Wall Thickness
0.307
Pipe Smys
35000
Pipe Specification
Unknown
Pipe Seam Type
Seamless
Pipe Manufacturer
Unknown
Pipe Coating Type
Coal Tar
Coating Applied Ind
Unknown
Installation Year
1959
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Mechanical Puncture
Puncture Axial
24
Puncture Circum
10
Class Location Type
Class 3 Location
Could Be Hca
Yes
Determination Method
Method1
Not Flammable Ind
Not Flammable
Heat Damage Ind
No
Non Heat Damage Ind
No
Est Cost Oper Paid
0
Est Cost Unintentional Release
78174
Est Cost Intentional Release
0
Est Cost Prop Damage
165750
Est Cost Emergency
29250
Est Cost Other
0
Gas Cost In Mcf
6
Prpty
273174
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Wildlife Impact Ind
No
Accident Psig
675
Gas Flow In Pipe In Mcf
11823
Mop Psig
796
Mop Cfr Section
Maop Established Date
1970-07-01 00:00:00
Maop Reversal Flow Ind
Bi-Directional
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Gas Required Odorized Ind
Yes
Gas Odorized Ind
Yes
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Length Segment Isolated
16368
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
Transmission System
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Accident Identifier
Notification From Third Party That Caused The Incident
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Pipe was damaged by a 3rd party company.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
Yes
Landowner Ind
Yes
State Law Exempt Ind
No
Notify Cga Dirt
No
Private Row Ind
Yes
Private Subtype
Private Landowner
Excavator Type
Contractor
Excavator Equipment
Backhoe/trackhoe
Work Performed
Drainage
One Call Notified Ind
No
Service Interruption
Yes
Service Interruption Hours
48
Root Cause Category
Notification Issue
Root Cause Type
No Notification Made To The One-Call Center/811
Preparer Name
C********** R******
Preparer Title
Gas Regulatory Compliance Analyst
Preparer Email
C******************@d**********.com
Preparer Telephone
704-731-4680
Authorizer Name
F***** B****
Authorizer Title
Manager- Pipeline Safety
Authorizer Telephone
704-731-4618
Authorizer Email
F***********@d**********.com
Narrative
A contractor damaged a 10" steel main with a trackhoe while in the process of digging a proposed retention pond. The contractor did not contact the one-call center for the area being excavated.
Report Received Date 2022-10-13 00:00:00
Iyear 2022
Report Number 20220109
Supplemental Number 37431
Report Type Supplemental Final
Operator Id 15518 PHMSA Enforcement
Name Piedmont Natural Gas Co Inc
Operator Street Address 525 South Tryon Street
Operator City Name Charlotte
Operator State Abbreviation NC
Operator Postal Code 28202
Local Datetime 2022-09-20 14:05:00
Time Zone Eastern
Daylight Savings Ind No
Location Latitude 35.274273 Google Maps OpenStreetMap
Location Longitude -80.53506 Google Maps OpenStreetMap
Nrc Rpt Num 1347796 NRC Report How to search
Nrc Rpt Datetime 2022-09-20 16:18:00
Additional Nrc Report Numbers 1347952
Commodity Released Type Natural Gas
Unintentional Release 13029
Intentional Release 0
Accompanying Liquid 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Status When Identified Normal Operation, Includes Pauses During Maintenance
Shutdown Due Accident Ind No
Shutdown Explain A Section Of The Pipeline Was Blocked Off.
Communication State Fed Ind No
Ignite Ind No
Upstream Action Taken Valve Closure
Upstream Valve Close Datetime 2022-09-20 15:38:00
Downstream Action Taken Valve Closure
Downstream Vlv Close Datetime 2022-09-21 19:23:00
Num Pub Evacuated 0
Incident Identified Datetime 2022-09-20 14:05:00
On Site Datetime 2022-09-20 14:11:00
On Off Shore Onshore
Onshore State Abbreviation Nc
Onshore Postal Code 28031
Onshore City Name Cornelius
Onshore County Name Mecklenburg
Designated Location Not Applicable
Pipe Fac Name Line 369
Segment Name 415035
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 42
Other Underground Facilities No
Crossing No
Pipe Facility Type Intrastate
System Part Involved Onshore Pipeline, Including Valve Sites
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 10
Puddle Weld Ind No
Pipe Wall Thickness 0.307
Pipe Smys 35000
Pipe Specification Unknown
Pipe Seam Type Seamless
Pipe Manufacturer Unknown
Pipe Coating Type Coal Tar
Coating Applied Ind Unknown
Installation Year 1959
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Mechanical Puncture
Puncture Axial 24
Puncture Circum 10
Class Location Type Class 3 Location
Could Be Hca Yes
Determination Method Method1
Not Flammable Ind Not Flammable
Heat Damage Ind No
Non Heat Damage Ind No
Est Cost Oper Paid 0
Est Cost Unintentional Release 78174
Est Cost Intentional Release 0
Est Cost Prop Damage 165750
Est Cost Emergency 29250
Est Cost Other 0
Gas Cost In Mcf 6
Prpty 273174
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Wildlife Impact Ind No
Accident Psig 675
Gas Flow In Pipe In Mcf 11823
Mop Psig 796
Mop Cfr Section 192.619(C) View CFR 49 §192
Maop Established Date 1970-07-01 00:00:00
Maop Reversal Flow Ind Bi-Directional
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Gas Required Odorized Ind Yes
Gas Odorized Ind Yes
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Length Segment Isolated 16368
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function Transmission System
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Accident Identifier Notification From Third Party That Caused The Incident
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Pipe was damaged by a 3rd party company.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Excavation Damage
Cause Details Excavation Damage By Third Party
Ex Party Type Excavation Damage By Third Party
Prior Notification Ind Yes
Landowner Ind Yes
State Law Exempt Ind No
Notify Cga Dirt No
Private Row Ind Yes
Private Subtype Private Landowner
Excavator Type Contractor
Excavator Equipment Backhoe/trackhoe
Work Performed Drainage
One Call Notified Ind No
Service Interruption Yes
Service Interruption Hours 48
Root Cause Category Notification Issue
Root Cause Type No Notification Made To The One-Call Center/811
Preparer Name C********** R******
Preparer Title Gas Regulatory Compliance Analyst
Preparer Email C******************@d**********.com
Preparer Telephone 704-731-4680
Authorizer Name F***** B****
Authorizer Title Manager- Pipeline Safety
Authorizer Telephone 704-731-4618
Authorizer Email F***********@d**********.com
Narrative A contractor damaged a 10" steel main with a trackhoe while in the process of digging a proposed retention pond. The contractor did not contact the one-call center for the area being excavated.

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