GTG incident on 2022-07-22 — TX

Operator
Energy Transfer Company
Cause
Material Failure Of Pipe Or Weld
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$208,500
Incident datetime
2022-07-22 10:10
Report number
Location
TX
Narrative
On 7/22/22 at approximately 10:10, a producer contacted energy transfer operations personnel to report a loss of pressure and well shut in bienville parrish. The 2 wells reported to be shut in were both inlets into the energy transfer pipeline referenced as 20101088 tristate 9047 chk weyerhaeuser 15-1. Operations personnel were mobilized and enroute to shut manual valves to isolate the segment of pipeline. The upstream and downstream valves were shut in and energy transfer personnel located a pipeline rupture on the weyerhaeuser 15-1. Once isolated, the pipeline was allowed to blowdown at the rupture site. A segment of pipe was located outside of the rupture area and was preserved to send for metallurgical analysis. Reports were made to the la state police on 722/22 at 10:22 and la dnr on 7/22/22 at 11:46. Nrc notifications were made (1342244 & 48-hr follow up 1342376). Metallurgical analysis is being completed on the sample recovered from the rupture site. The segment of pipe affected has been replaced and was placed back in service on 8/5/22 at 18:00. Metallurgical analysis indicated internal environmental cracking as the cause likely due to interaction between corrosion inhibitor and components of the gas stream. Since the time of the failure the pipeline was subjected to a hydrostatic pressure strength and spike test.
Detailed record list
Report Received Date
2022-08-16 00:00:00
Iyear
2022
Report Number
20220085
Supplemental Number
37840
Report Type
Supplemental Final
Operator Id
Name
Energy Transfer Company
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2022-07-22 10:10:00
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Nrc Rpt Num
Nrc Rpt Datetime
2022-07-22 11:34:00
Additional Nrc Report Numbers
1342376
Commodity Released Type
Natural Gas
Unintentional Release
8200
Intentional Release
0
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Status When Identified
Normal Operation, Includes Pauses During Maintenance
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2022-07-22 10:52:00
Restart Datetime
2022-08-05 18:00:00
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Initial Responder Com Datetime
2022-07-22 10:22:00
Ignite Ind
No
Upstream Action Taken
Valve Closure
Upstream Valve Close Datetime
2022-07-22 10:52:00
Downstream Action Taken
Valve Closure
Downstream Vlv Close Datetime
2022-07-22 10:39:00
Num Pub Evacuated
0
Incident Identified Datetime
2022-07-22 10:10:00
On Site Datetime
2022-07-22 11:15:00
On Off Shore
Onshore
Onshore State Abbreviation
La
Onshore Postal Code
71068
Onshore City Name
Not Within A Municipality
Onshore County Name
Bienville
Designated Location
Not Applicable
Pipe Fac Name
Tristate 9047, Chk Weyerhaeuser 15-1
Segment Name
20101088
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
204
Other Underground Facilities
No
Crossing
No
Pipe Facility Type
Intrastate
System Part Involved
Onshore Pipeline, Including Valve Sites
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
8.625
Puddle Weld Ind
No
Pipe Wall Thickness
0.188
Pipe Smys
52000
Pipe Specification
Api-5lx
Pipe Seam Type
Seamless
Pipe Manufacturer
Unknown
Pipe Coating Type
Epoxy
Coating Applied Ind
No
Installation Year
2010
Manufactured Year
2007
Material Involved
Carbon Steel
Release Type
Rupture
Rupture Orient
Longitudinal
Rupture Length
240
Rupture Width
20
Class Location Type
Class 1 Location
Could Be Hca
No
Pir Radius
239
Heat Damage Ind
No
Non Heat Damage Ind
No
Did Occur In Mca Ind
No
Est Cost Oper Paid
8000
Est Cost Unintentional Release
57072
Est Cost Intentional Release
0
Est Cost Prop Damage
208500
Est Cost Emergency
0
Est Cost Other
0
Gas Cost In Mcf
6.96
Prpty
273572
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Wildlife Impact Ind
No
Accident Psig
1145
Gas Flow In Pipe In Mcf
100
Mop Psig
1440
Mop Cfr Section
192.619(A)(1)
Maop Established Date
2010-03-01 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Gas Required Odorized Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Length Segment Isolated
10050
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
Type C Gathering
Scada In Place Ind
No
Accident Identifier
Notification From Public
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Material Failure Of Pipe Or Weld
Cause Details
Environmental Cracking-Related
Pwjf Failure Type
Environmental Cracking-Related
Metallurgical Ind
Yes
Stress Subtype
Other
Stress Details
Internal Environmental Cracking
Additional Crack Ind
Yes
Post Constr Pressure Test Val
2102
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
2019
Hydrtst Most Rcnt Pressure
1400
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
A***** M*****
Preparer Title
Lead Specialist - Regulatory Compliance
Preparer Email
A************@e*************.com
Preparer Telephone
903-243-6541
Authorizer Name
C**** K*****
Authorizer Title
Manager - Regulatory Compliance
Authorizer Telephone
713-989-7077
Authorizer Email
C***********@e*************.com
Narrative
On 7/22/22 at approximately 10:10, a producer contacted energy transfer operations personnel to report a loss of pressure and well shut in bienville parrish. The 2 wells reported to be shut in were both inlets into the energy transfer pipeline referenced as 20101088 tristate 9047 chk weyerhaeuser 15-1. Operations personnel were mobilized and enroute to shut manual valves to isolate the segment of pipeline. The upstream and downstream valves were shut in and energy transfer personnel located a pipeline rupture on the weyerhaeuser 15-1. Once isolated, the pipeline was allowed to blowdown at the rupture site. A segment of pipe was located outside of the rupture area and was preserved to send for metallurgical analysis. Reports were made to the la state police on 722/22 at 10:22 and la dnr on 7/22/22 at 11:46. Nrc notifications were made (1342244 & 48-hr follow up 1342376). Metallurgical analysis is being completed on the sample recovered from the rupture site. The segment of pipe affected has been replaced and was placed back in service on 8/5/22 at 18:00. Metallurgical analysis indicated internal environmental cracking as the cause likely due to interaction between corrosion inhibitor and components of the gas stream. Since the time of the failure the pipeline was subjected to a hydrostatic pressure strength and spike test.
Report Received Date 2022-08-16 00:00:00
Iyear 2022
Report Number 20220085
Supplemental Number 37840
Report Type Supplemental Final
Operator Id 32099 PHMSA Enforcement
Name Energy Transfer Company
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2022-07-22 10:10:00
Time Zone Central
Daylight Savings Ind Yes
Location Latitude 32.36651 Google Maps OpenStreetMap
Location Longitude -93.35471 Google Maps OpenStreetMap
Nrc Rpt Num 1342244 NRC Report How to search
Nrc Rpt Datetime 2022-07-22 11:34:00
Additional Nrc Report Numbers 1342376
Commodity Released Type Natural Gas
Unintentional Release 8200
Intentional Release 0
Accompanying Liquid 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Status When Identified Normal Operation, Includes Pauses During Maintenance
Shutdown Due Accident Ind Yes
Shutdown Datetime 2022-07-22 10:52:00
Restart Datetime 2022-08-05 18:00:00
Communication State Fed Ind Yes
Party Initiated Communication Operator
Initial Responder Com Datetime 2022-07-22 10:22:00
Ignite Ind No
Upstream Action Taken Valve Closure
Upstream Valve Close Datetime 2022-07-22 10:52:00
Downstream Action Taken Valve Closure
Downstream Vlv Close Datetime 2022-07-22 10:39:00
Num Pub Evacuated 0
Incident Identified Datetime 2022-07-22 10:10:00
On Site Datetime 2022-07-22 11:15:00
On Off Shore Onshore
Onshore State Abbreviation La
Onshore Postal Code 71068
Onshore City Name Not Within A Municipality
Onshore County Name Bienville
Designated Location Not Applicable
Pipe Fac Name Tristate 9047, Chk Weyerhaeuser 15-1
Segment Name 20101088
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 204
Other Underground Facilities No
Crossing No
Pipe Facility Type Intrastate
System Part Involved Onshore Pipeline, Including Valve Sites
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 8.625
Puddle Weld Ind No
Pipe Wall Thickness 0.188
Pipe Smys 52000
Pipe Specification Api-5lx
Pipe Seam Type Seamless
Pipe Manufacturer Unknown
Pipe Coating Type Epoxy
Coating Applied Ind No
Installation Year 2010
Manufactured Year 2007
Material Involved Carbon Steel
Release Type Rupture
Rupture Orient Longitudinal
Rupture Length 240
Rupture Width 20
Class Location Type Class 1 Location
Could Be Hca No
Pir Radius 239
Heat Damage Ind No
Non Heat Damage Ind No
Did Occur In Mca Ind No
Est Cost Oper Paid 8000
Est Cost Unintentional Release 57072
Est Cost Intentional Release 0
Est Cost Prop Damage 208500
Est Cost Emergency 0
Est Cost Other 0
Gas Cost In Mcf 6.96
Prpty 273572
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Wildlife Impact Ind No
Accident Psig 1145
Gas Flow In Pipe In Mcf 100
Mop Psig 1440
Mop Cfr Section 192.619(A)(1) View CFR 49 §192
Maop Established Date 2010-03-01 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Gas Required Odorized Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Length Segment Isolated 10050
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function Type C Gathering
Scada In Place Ind No
Accident Identifier Notification From Public
Investigation Status No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Material Failure Of Pipe Or Weld
Cause Details Environmental Cracking-Related
Pwjf Failure Type Environmental Cracking-Related
Metallurgical Ind Yes
Stress Subtype Other
Stress Details Internal Environmental Cracking
Additional Crack Ind Yes
Post Constr Pressure Test Val 2102
Collected Data Ind No
Has Hydrtst Conduc Before Ind Yes
Hydrtst Most Rcnt Year 2019
Hydrtst Most Rcnt Pressure 1400
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name A***** M*****
Preparer Title Lead Specialist - Regulatory Compliance
Preparer Email A************@e*************.com
Preparer Telephone 903-243-6541
Authorizer Name C**** K*****
Authorizer Title Manager - Regulatory Compliance
Authorizer Telephone 713-989-7077
Authorizer Email C***********@e*************.com
Narrative On 7/22/22 at approximately 10:10, a producer contacted energy transfer operations personnel to report a loss of pressure and well shut in bienville parrish. The 2 wells reported to be shut in were both inlets into the energy transfer pipeline referenced as 20101088 tristate 9047 chk weyerhaeuser 15-1. Operations personnel were mobilized and enroute to shut manual valves to isolate the segment of pipeline. The upstream and downstream valves were shut in and energy transfer personnel located a pipeline rupture on the weyerhaeuser 15-1. Once isolated, the pipeline was allowed to blowdown at the rupture site. A segment of pipe was located outside of the rupture area and was preserved to send for metallurgical analysis. Reports were made to the la state police on 722/22 at 10:22 and la dnr on 7/22/22 at 11:46. Nrc notifications were made (1342244 & 48-hr follow up 1342376). Metallurgical analysis is being completed on the sample recovered from the rupture site. The segment of pipe affected has been replaced and was placed back in service on 8/5/22 at 18:00. Metallurgical analysis indicated internal environmental cracking as the cause likely due to interaction between corrosion inhibitor and components of the gas stream. Since the time of the failure the pipeline was subjected to a hydrostatic pressure strength and spike test.

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