GD incident on 2022-10-03 — MI

Operator
Consumers Energy Co
Cause
Locating Issue
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$31,896
Incident datetime
2022-10-03 13:23
Report number
Location
MI, KALAMAZOO
Narrative
On october 3, 2022, at approximately 13:23 hours consumers energy received notification of a natural gas pipeline damage near interstate highway 94 (I-94) and portage street, kalamazoo (kalamazoo county) michigan. A gas service worker (gsw) was dispatched and arrived onsite at approximately 13:42 hours. The gsw confirmed a third-party contractor cutting in a new entrance ramp to I-94 damaged a natural gas pipeline, which was later determined to be a 6-inch steel high pressure pipeline. The roadway was already closed to traffic when the damaged occurred due to the on-going construction. Police and fire departments were onsite and ensured no construction vehicles used the construction entrances into the area. Air traffic into the local airport was also diverted to prevent the potential for injury. No fatalities or injuries occurred because of the pipeline damage and subsequent gas release. A distribution crew arrived onsite at approximately 14:02 hours and an isolation plan to stop gas from blowing was developed. To isolate, the crew utilized an existing pressure control fitting to the north of the damage location and multiple valves were utilized south of the damage location. Gas was controlled at approximately 18:30 hours, the damaged segment was removed and replaced with 28-inches of 6-inch steel pipeline. Repairs were completed and normal operations resumed on october 4, 2022, at approximately 03:00 hours. No loss of service to customers occurred because of the pipeline damage. Further investigation determined the staking contractor failed to stake the requested location and provided an inaccurate positive response code, causing the contractor to damage the underground natural gas pipeline.
Detailed record list
Occurred At
2022-10-03 13:23:00
Year
2022
Report Received Date
2022-11-02 00:00:00
Iyear
2022.0
Report Number
20220069.0
Supplemental Number
38282.0
Report Type
Supplemental Final
Operator Id
Name
Consumers Energy Co
Operator Street Address
One Energy Plaza
Operator City Name
Jackson
Operator State Abbreviation
MI
Operator Postal Code
49201
Local Datetime
2022-10-03 13:23:00
Time Zone
Eastern
Daylight Savings Ind
Yes
Location Street Address
Interstate 94 & Portage Road
Location City Name
Portage
Location County Name
Kalamazoo
Location State Abbreviation
MI
Location Postal Code
49002
Location Latitude
Location Longitude
Flow Cont Key Crit Ind
Yes
Flow Cont Stopple Fitng Ind
Yes
Nrc Rpt Datetime
2022-10-03 16:47:00
Nrc Rpt Num
Additional Nrc Report Numbers
1349071
Commodity Released Type
Natural Gas
Unintentional Release
7578.0
Intentional Release
0.0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
No
Num Pub Evacuated
0.0
Incident Identified Datetime
2022-10-03 13:23:00
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Initial Responder Com Datetime
2022-10-03 13:45:00
On Site Datetime
2022-10-03 13:42:00
Federal
No
Location Type
Utility Right-Of-Way / Easement
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
120.0
Other Underground Facilities
No
Crossing
No
Pipe Facility Type
Investor Owned
System Part Involved
Main
Installation Year
1973.0
Pipe Diameter
6.0
Pipe Specification
Api 5l
Pipe Manufacturer
Unknown
Material Involved
Steel
Steel Seam Type
Seamless
Wt Steel
0.219
Release Type
Mechanical Puncture
Puncture Axial
2.0
Puncture Circum
18.8
Class Location Type
Class 3 Location
Est Cost Oper Paid
0.0
Est Cost Prop Damage
31896.0
Est Cost Emergency
62.0
Est Cost Other
0.0
Gas Cost In Mcf
8.95
Est Cost Unintentional Release
67823.0
Est Cost Intentional Release
0.0
Prpty
99781.0
Commercial Affected
0.0
Industrial Affected
0.0
Residences Affected
0.0
Num Persons Hosp Not Ovnght
0.0
Num Injured Treated By Emt
0.0
Num Resident Building Affctd
0.0
Num Business Building Affctd
0.0
Accident Psig
352.0
Normal Psig
352.0
Mop Psig
400.0
Mop Cfr Section
192.619(A)(2)
Maop Established Date
1973-08-16 00:00:00
Accident Pressure
Pressure Did Not Exceed Maop
Gas Odorized System Type
Injection Pump
Gas Odorized Lvl Not Msrd Ind
Yes
Scada In Place Ind
No
Accident Identifier
Notification From Third Party That Caused The Incident
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
Yes
One Call System Ind
Yes
State Law Exempt Ind
No
Notify Cga Dirt
Yes
Public Row Ind
Yes
Public Subtype
Interstate Highway
Excavator Type
Contractor
Excavator Equipment
Backhoe/trackhoe
Work Performed
Road Work
One Call Notified Ind
Yes
One Call Ticket Num
2.02209e+12
Locator Type
Contract Locator
Visible Marks
No
Service Interruption
No
Root Cause Category
Locating Issue
Root Cause Type
Facility Not Marked Due To Locator Error
Preparer Name
C******* Q* K***
Preparer Title
Senior Engineering Technical Analyst Ii
Preparer Email
C************@c********.com
Preparer Telephone
989-280-2963
Local Contact Name
C******* Q* K***
Local Contact Email
C************@c********.com
Local Contact Telephone
989-280-2963
Authorizer Name
J**** E* P****
Authorizer Title
Gas Compliance Manager
Authorizer Telephone
989-598-5031
Authorizer Email
J**********@c********.com
Narrative
On october 3, 2022, at approximately 13:23 hours consumers energy received notification of a natural gas pipeline damage near interstate highway 94 (I-94) and portage street, kalamazoo (kalamazoo county) michigan. A gas service worker (gsw) was dispatched and arrived onsite at approximately 13:42 hours. The gsw confirmed a third-party contractor cutting in a new entrance ramp to I-94 damaged a natural gas pipeline, which was later determined to be a 6-inch steel high pressure pipeline. The roadway was already closed to traffic when the damaged occurred due to the on-going construction. Police and fire departments were onsite and ensured no construction vehicles used the construction entrances into the area. Air traffic into the local airport was also diverted to prevent the potential for injury. No fatalities or injuries occurred because of the pipeline damage and subsequent gas release. A distribution crew arrived onsite at approximately 14:02 hours and an isolation plan to stop gas from blowing was developed. To isolate, the crew utilized an existing pressure control fitting to the north of the damage location and multiple valves were utilized south of the damage location. Gas was controlled at approximately 18:30 hours, the damaged segment was removed and replaced with 28-inches of 6-inch steel pipeline. Repairs were completed and normal operations resumed on october 4, 2022, at approximately 03:00 hours. No loss of service to customers occurred because of the pipeline damage. Further investigation determined the staking contractor failed to stake the requested location and provided an inaccurate positive response code, causing the contractor to damage the underground natural gas pipeline.
Occurred At 2022-10-03 13:23:00
Year 2022
Report Received Date 2022-11-02 00:00:00
Iyear 2022.0
Report Number 20220069.0
Supplemental Number 38282.0
Report Type Supplemental Final
Operator Id 2748 PHMSA Enforcement
Name Consumers Energy Co
Operator Street Address One Energy Plaza
Operator City Name Jackson
Operator State Abbreviation MI
Operator Postal Code 49201
Local Datetime 2022-10-03 13:23:00
Time Zone Eastern
Daylight Savings Ind Yes
Location Street Address Interstate 94 & Portage Road
Location City Name Portage
Location County Name Kalamazoo
Location State Abbreviation MI
Location Postal Code 49002
Location Latitude 42.246257 Google Maps OpenStreetMap
Location Longitude -85.558724 Google Maps OpenStreetMap
Flow Cont Key Crit Ind Yes
Flow Cont Stopple Fitng Ind Yes
Nrc Rpt Datetime 2022-10-03 16:47:00
Nrc Rpt Num 1348944 NRC Report How to search
Additional Nrc Report Numbers 1349071
Commodity Released Type Natural Gas
Unintentional Release 7578.0
Intentional Release 0.0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind No
Num Pub Evacuated 0.0
Incident Identified Datetime 2022-10-03 13:23:00
Communication State Fed Ind Yes
Party Initiated Communication Operator
Initial Responder Com Datetime 2022-10-03 13:45:00
On Site Datetime 2022-10-03 13:42:00
Federal No
Location Type Utility Right-Of-Way / Easement
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 120.0
Other Underground Facilities No
Crossing No
Pipe Facility Type Investor Owned
System Part Involved Main
Installation Year 1973.0
Pipe Diameter 6.0
Pipe Specification Api 5l
Pipe Manufacturer Unknown
Material Involved Steel
Steel Seam Type Seamless
Wt Steel 0.219
Release Type Mechanical Puncture
Puncture Axial 2.0
Puncture Circum 18.8
Class Location Type Class 3 Location
Est Cost Oper Paid 0.0
Est Cost Prop Damage 31896.0
Est Cost Emergency 62.0
Est Cost Other 0.0
Gas Cost In Mcf 8.95
Est Cost Unintentional Release 67823.0
Est Cost Intentional Release 0.0
Prpty 99781.0
Commercial Affected 0.0
Industrial Affected 0.0
Residences Affected 0.0
Num Persons Hosp Not Ovnght 0.0
Num Injured Treated By Emt 0.0
Num Resident Building Affctd 0.0
Num Business Building Affctd 0.0
Accident Psig 352.0
Normal Psig 352.0
Mop Psig 400.0
Mop Cfr Section 192.619(A)(2) View CFR 49 §192
Maop Established Date 1973-08-16 00:00:00
Accident Pressure Pressure Did Not Exceed Maop
Gas Odorized System Type Injection Pump
Gas Odorized Lvl Not Msrd Ind Yes
Scada In Place Ind No
Accident Identifier Notification From Third Party That Caused The Incident
Investigation Status No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Excavation Damage
Cause Details Excavation Damage By Third Party
Ex Party Type Excavation Damage By Third Party
Prior Notification Ind Yes
One Call System Ind Yes
State Law Exempt Ind No
Notify Cga Dirt Yes
Public Row Ind Yes
Public Subtype Interstate Highway
Excavator Type Contractor
Excavator Equipment Backhoe/trackhoe
Work Performed Road Work
One Call Notified Ind Yes
One Call Ticket Num 2.02209e+12
Locator Type Contract Locator
Visible Marks No
Service Interruption No
Root Cause Category Locating Issue
Root Cause Type Facility Not Marked Due To Locator Error
Preparer Name C******* Q* K***
Preparer Title Senior Engineering Technical Analyst Ii
Preparer Email C************@c********.com
Preparer Telephone 989-280-2963
Local Contact Name C******* Q* K***
Local Contact Email C************@c********.com
Local Contact Telephone 989-280-2963
Authorizer Name J**** E* P****
Authorizer Title Gas Compliance Manager
Authorizer Telephone 989-598-5031
Authorizer Email J**********@c********.com
Narrative On october 3, 2022, at approximately 13:23 hours consumers energy received notification of a natural gas pipeline damage near interstate highway 94 (I-94) and portage street, kalamazoo (kalamazoo county) michigan. A gas service worker (gsw) was dispatched and arrived onsite at approximately 13:42 hours. The gsw confirmed a third-party contractor cutting in a new entrance ramp to I-94 damaged a natural gas pipeline, which was later determined to be a 6-inch steel high pressure pipeline. The roadway was already closed to traffic when the damaged occurred due to the on-going construction. Police and fire departments were onsite and ensured no construction vehicles used the construction entrances into the area. Air traffic into the local airport was also diverted to prevent the potential for injury. No fatalities or injuries occurred because of the pipeline damage and subsequent gas release. A distribution crew arrived onsite at approximately 14:02 hours and an isolation plan to stop gas from blowing was developed. To isolate, the crew utilized an existing pressure control fitting to the north of the damage location and multiple valves were utilized south of the damage location. Gas was controlled at approximately 18:30 hours, the damaged segment was removed and replaced with 28-inches of 6-inch steel pipeline. Repairs were completed and normal operations resumed on october 4, 2022, at approximately 03:00 hours. No loss of service to customers occurred because of the pipeline damage. Further investigation determined the staking contractor failed to stake the requested location and provided an inaccurate positive response code, causing the contractor to damage the underground natural gas pipeline.

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