GD incident on 2022-01-14 — TX

Operator
Atmos Energy Corporation - Mid-Tex
Cause
Locating Issue
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$129,307
Incident datetime
2022-01-14 16:00
Report number
Location
TX, TARRANT
Narrative
On january 14, 2022, a third-party contractor was directional drilling and bored into atmos energy's 16-inch steel gas main at 9301 white settlement road. The intermediate pressure main is a two-way feed. The technician arrived on the scene and confirmed the leak at 4:00 pm. Assistance was requested at 4:20 pm. At 4:08 pm the tech noted that fire department was on site indicating they were contacted prior to that time. This is the time provided in part a question 15. Other notes indicate the police department was also on the scene, however there is not a time given. Fire and police remained on scene to provide traffic and perimeter assistance. Stopple fittings were applied to control the release of gas and a split-weld sleeve was installed to repair the leak. These permanent repairs were completed on january 15, 2022, at 6:30 am. On june 15, 2022 at approximately 12:06 pm, it was determined that repairs costs had met the reporting threshold. A report was made to nrc within the hour. Regarding part c question 5 - the diameter of the puncture is 0.226 inches, but the form only allows whole numbers. Supplemented to provide answers in part c, question 2a and part e, question 3b. 12/19/2022 - further supplemented to change the sub-cause from facility marking or location not sufficient to incorrect facility records/maps.
Detailed record list
Occurred At
2022-01-14 16:00:00
Year
2022
Report Received Date
2022-07-15 00:00:00
Iyear
2022.0
Report Number
20220051.0
Supplemental Number
37524.0
Report Type
Supplemental Final
Operator Id
Name
Atmos Energy Corporation - Mid-Tex
Operator Street Address
5430 Lbj Freeway Suite 1800
Operator City Name
Dallas
Operator State Abbreviation
TX
Operator Postal Code
75240
Local Datetime
2022-01-14 16:00:00
Time Zone
Central
Daylight Savings Ind
Yes
Location Street Address
9301 White Settlement
Location City Name
White Settlement
Location County Name
Tarrant
Location State Abbreviation
TX
Location Postal Code
76108
Location Latitude
Location Longitude
-97.47542699
Flow Cont Stopple Fitng Ind
Yes
Nrc Rpt Datetime
2022-06-15 12:41:00
Nrc Rpt Num
Additional Nrc Report Numbers
1339031
Commodity Released Type
Natural Gas
Unintentional Release
15.369
Intentional Release
0.0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
No
Num Pub Evacuated
0.0
Incident Identified Datetime
2022-01-14 16:00:00
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Initial Responder Com Datetime
2022-01-14 16:08:00
On Site Datetime
2022-01-14 16:00:00
Federal
No
Location Type
Public Property
Incident Area Type
Underground
Incident Area Subtype
Under Pavement
Depth Of Cover
48.0
Other Underground Facilities
No
Crossing
No
Pipe Facility Type
Investor Owned
System Part Involved
Main
Installation Year
1955.0
Pipe Diameter
16.0
Pipe Specification
Api 5l
Pipe Manufacturer
Unknown
Material Involved
Steel
Steel Seam Type
Other
Steel Seam Type Details
Unknown
Release Type
Mechanical Puncture
Puncture Axial
1.0
Puncture Circum
1.0
Class Location Type
Class 3 Location
Est Cost Oper Paid
0.0
Est Cost Prop Damage
129307.0
Est Cost Emergency
32882.0
Est Cost Other
0.0
Gas Cost In Mcf
7.874
Est Cost Unintentional Release
121.0
Est Cost Intentional Release
0.0
Prpty
162310.0
Commercial Affected
0.0
Industrial Affected
0.0
Residences Affected
0.0
Num Persons Hosp Not Ovnght
0.0
Num Injured Treated By Emt
0.0
Num Resident Building Affctd
0.0
Num Business Building Affctd
0.0
Accident Psig
30.0
Normal Psig
30.0
Mop Psig
60.0
Mop Cfr Section
192.619(A)(2)
Maop Established Date
1955-08-22 00:00:00
Accident Pressure
Pressure Did Not Exceed Maop
Gas Odorized System Type
Injection Pump
Gas Odorized Lvl Not Msrd Ind
Yes
Scada In Place Ind
No
Accident Identifier
Notification From Public
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
Yes
One Call System Ind
Yes
State Law Exempt Ind
No
Notify Cga Dirt
No
Public Row Ind
Yes
Public Subtype
City Street
Excavator Type
Contractor
Excavator Equipment
Boring
Work Performed
Sewer (Sanitary/storm)
One Call Notified Ind
Yes
One Call Ticket Num
2251192444
One Call Center Name
Texas 811
Locator Type
Contract Locator
Visible Marks
Yes
Service Interruption
No
Root Cause Category
Locating Issue
Root Cause Type
Facility Not Marked Due To Incorrect Facility Records/maps
Preparer Name
J**** C*******
Preparer Title
Compliance Analyst
Preparer Email
J*************@a**********.com
Preparer Telephone
214-535-6117
Local Contact Name
R***** W*******
Local Contact Email
R**************@a**********.com
Local Contact Telephone
8172072998
Authorizer Name
J*** K******
Authorizer Title
Sr Vp Technical Services
Authorizer Telephone
214-206-2701
Authorizer Email
J***********@a**********.com
Narrative
On january 14, 2022, a third-party contractor was directional drilling and bored into atmos energy's 16-inch steel gas main at 9301 white settlement road. The intermediate pressure main is a two-way feed. The technician arrived on the scene and confirmed the leak at 4:00 pm. Assistance was requested at 4:20 pm. At 4:08 pm the tech noted that fire department was on site indicating they were contacted prior to that time. This is the time provided in part a question 15. Other notes indicate the police department was also on the scene, however there is not a time given. Fire and police remained on scene to provide traffic and perimeter assistance. Stopple fittings were applied to control the release of gas and a split-weld sleeve was installed to repair the leak. These permanent repairs were completed on january 15, 2022, at 6:30 am. On june 15, 2022 at approximately 12:06 pm, it was determined that repairs costs had met the reporting threshold. A report was made to nrc within the hour. Regarding part c question 5 - the diameter of the puncture is 0.226 inches, but the form only allows whole numbers. Supplemented to provide answers in part c, question 2a and part e, question 3b. 12/19/2022 - further supplemented to change the sub-cause from facility marking or location not sufficient to incorrect facility records/maps.
Occurred At 2022-01-14 16:00:00
Year 2022
Report Received Date 2022-07-15 00:00:00
Iyear 2022.0
Report Number 20220051.0
Supplemental Number 37524.0
Report Type Supplemental Final
Operator Id 31348 PHMSA Enforcement
Name Atmos Energy Corporation - Mid-Tex
Operator Street Address 5430 Lbj Freeway Suite 1800
Operator City Name Dallas
Operator State Abbreviation TX
Operator Postal Code 75240
Local Datetime 2022-01-14 16:00:00
Time Zone Central
Daylight Savings Ind Yes
Location Street Address 9301 White Settlement
Location City Name White Settlement
Location County Name Tarrant
Location State Abbreviation TX
Location Postal Code 76108
Location Latitude 32.76051149 Google Maps OpenStreetMap
Location Longitude -97.47542699 Google Maps OpenStreetMap
Flow Cont Stopple Fitng Ind Yes
Nrc Rpt Datetime 2022-06-15 12:41:00
Nrc Rpt Num 1338839 NRC Report How to search
Additional Nrc Report Numbers 1339031
Commodity Released Type Natural Gas
Unintentional Release 15.369
Intentional Release 0.0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind No
Num Pub Evacuated 0.0
Incident Identified Datetime 2022-01-14 16:00:00
Communication State Fed Ind Yes
Party Initiated Communication Operator
Initial Responder Com Datetime 2022-01-14 16:08:00
On Site Datetime 2022-01-14 16:00:00
Federal No
Location Type Public Property
Incident Area Type Underground
Incident Area Subtype Under Pavement
Depth Of Cover 48.0
Other Underground Facilities No
Crossing No
Pipe Facility Type Investor Owned
System Part Involved Main
Installation Year 1955.0
Pipe Diameter 16.0
Pipe Specification Api 5l
Pipe Manufacturer Unknown
Material Involved Steel
Steel Seam Type Other
Steel Seam Type Details Unknown
Release Type Mechanical Puncture
Puncture Axial 1.0
Puncture Circum 1.0
Class Location Type Class 3 Location
Est Cost Oper Paid 0.0
Est Cost Prop Damage 129307.0
Est Cost Emergency 32882.0
Est Cost Other 0.0
Gas Cost In Mcf 7.874
Est Cost Unintentional Release 121.0
Est Cost Intentional Release 0.0
Prpty 162310.0
Commercial Affected 0.0
Industrial Affected 0.0
Residences Affected 0.0
Num Persons Hosp Not Ovnght 0.0
Num Injured Treated By Emt 0.0
Num Resident Building Affctd 0.0
Num Business Building Affctd 0.0
Accident Psig 30.0
Normal Psig 30.0
Mop Psig 60.0
Mop Cfr Section 192.619(A)(2) View CFR 49 §192
Maop Established Date 1955-08-22 00:00:00
Accident Pressure Pressure Did Not Exceed Maop
Gas Odorized System Type Injection Pump
Gas Odorized Lvl Not Msrd Ind Yes
Scada In Place Ind No
Accident Identifier Notification From Public
Investigation Status No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Excavation Damage
Cause Details Excavation Damage By Third Party
Ex Party Type Excavation Damage By Third Party
Prior Notification Ind Yes
One Call System Ind Yes
State Law Exempt Ind No
Notify Cga Dirt No
Public Row Ind Yes
Public Subtype City Street
Excavator Type Contractor
Excavator Equipment Boring
Work Performed Sewer (Sanitary/storm)
One Call Notified Ind Yes
One Call Ticket Num 2251192444
One Call Center Name Texas 811
Locator Type Contract Locator
Visible Marks Yes
Service Interruption No
Root Cause Category Locating Issue
Root Cause Type Facility Not Marked Due To Incorrect Facility Records/maps
Preparer Name J**** C*******
Preparer Title Compliance Analyst
Preparer Email J*************@a**********.com
Preparer Telephone 214-535-6117
Local Contact Name R***** W*******
Local Contact Email R**************@a**********.com
Local Contact Telephone 8172072998
Authorizer Name J*** K******
Authorizer Title Sr Vp Technical Services
Authorizer Telephone 214-206-2701
Authorizer Email J***********@a**********.com
Narrative On january 14, 2022, a third-party contractor was directional drilling and bored into atmos energy's 16-inch steel gas main at 9301 white settlement road. The intermediate pressure main is a two-way feed. The technician arrived on the scene and confirmed the leak at 4:00 pm. Assistance was requested at 4:20 pm. At 4:08 pm the tech noted that fire department was on site indicating they were contacted prior to that time. This is the time provided in part a question 15. Other notes indicate the police department was also on the scene, however there is not a time given. Fire and police remained on scene to provide traffic and perimeter assistance. Stopple fittings were applied to control the release of gas and a split-weld sleeve was installed to repair the leak. These permanent repairs were completed on january 15, 2022, at 6:30 am. On june 15, 2022 at approximately 12:06 pm, it was determined that repairs costs had met the reporting threshold. A report was made to nrc within the hour. Regarding part c question 5 - the diameter of the puncture is 0.226 inches, but the form only allows whole numbers. Supplemented to provide answers in part c, question 2a and part e, question 3b. 12/19/2022 - further supplemented to change the sub-cause from facility marking or location not sufficient to incorrect facility records/maps.

All rights reserved. Copyright © by ClearPHMSA