GTG incident on 2022-03-23 — TX

Operator
Atmos Pipeline - Texas
Cause
Other Outside Force Damage
Commodity
Natural Gas
Program
GTG
Damage and Injuries
1 fatality 0 injuries
Property damage (nominal)
$1,550,000
Incident datetime
2022-03-23 03:00
Report number
Location
TX
Narrative
Preliminary investigation indicates that on march 23, 2022, a vehicle traveling at a high rate of speed going southbound in the northbound lanes of hwy 360 crossed over u.S. 287 southbound service road, traveled an additional 125 feet, and struck an atmos energy measuring station near mansfield, texas. The gas ignited. The system pressure was at 655 psig at the time of the incident. Atmos energy was notified by emergency responders at approximately 1:40 a.M. And atmos energy personnel arrived onsite at 2:40 a.M. The fire department had the area sealed off until 3:00 a.M., at which time the technician was able to access the scene and determine that our facility was involved. At 3:43 a.M., an upstream valve was activated to stop the flow of gas, which resulted in the loss of service to atmos energys customer, sienergy. Sienergy informed atmos energy that it had approximately 1,110 customers downstream that lost service. The fire department evacuated a one-mile radius. Regarding question a23 of this report, the number of persons evacuated is unknown, however there were 593 structures in the evacuation zone.
Detailed record list
Report Received Date
2022-04-22 00:00:00
Iyear
2022
Report Number
20220048
Supplemental Number
37133
Report Type
Supplemental Final
Operator Id
Name
Atmos Pipeline - Texas
Operator Street Address
5420 Lbj Freeway, Suite 1500
Operator City Name
Dallas
Operator State Abbreviation
TX
Operator Postal Code
75240
Local Datetime
2022-03-23 04:30:00
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Nrc Rpt Num
Nrc Rpt Datetime
2022-03-23 04:21:00
Additional Nrc Report Numbers
1331898
Commodity Released Type
Natural Gas
Unintentional Release
33202
Intentional Release
0
Accompanying Liquid
0
Fatality Ind
Yes
Num Emp Fatalities
0
Num Contr Fatalities
0
Num Er Fatalities
0
Num Worker Fatalities
0
Num Gp Fatalities
1
Fatal
1
Injury Ind
No
Injure
0
Status When Identified
Normal Operation, Includes Pauses During Maintenance
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2022-03-23 03:43:00
Restart Datetime
2022-03-30 20:30:00
Ignite Ind
Yes
Ignite Datetime
2022-03-23 01:14:00
How Extinguished
Other
How Extinguished Other Detail
Shut Valve
Gas Consumed By Fire In Mcf
33202
Explode Ind
No
Num Pub Evacuated
593
Incident Identified Datetime
2022-03-23 03:00:00
On Site Datetime
2022-03-23 02:40:00
On Off Shore
Onshore
Onshore State Abbreviation
Tx
Onshore Postal Code
76063
Onshore City Name
Mansfield
Onshore County Name
Ellis
Designated Location
Survey Station No.
Designated Name
162
Pipe Fac Name
Line X64
Segment Name
Ms 8981.1
Federal
No
Location Type
Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
System Part Involved
Onshore Regulator/metering Station Equipment And Piping
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
8
Puddle Weld Ind
No
Pipe Wall Thickness
0.322
Pipe Smys
52000
Pipe Specification
X52
Pipe Seam Type
Longitudinal Erw - High Frequency
Pipe Manufacturer
Unknown
Pipe Coating Type
Paint
Coating Applied Ind
Yes
Installation Year
2017
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Rupture
Rupture Orient
Circumferential
Rupture Length
4
Rupture Width
4
Class Location Type
Class 1 Location
Could Be Hca
No
Pir Radius
184
Heat Damage Ind
No
Non Heat Damage Ind
No
Hca Fatalities Ind
No
Did Occur In Mca Ind
Yes
Mca Paved Surface Freeway Ind
Yes
Est Cost Oper Paid
60000
Est Cost Unintentional Release
175751
Est Cost Intentional Release
0
Est Cost Prop Damage
1550000
Est Cost Emergency
50000
Est Cost Other
0
Gas Cost In Mcf
5.2934
Prpty
1835751
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
1100
Num Business Building Affctd
10
Wildlife Impact Ind
No
Accident Psig
655
Gas Flow In Pipe In Mcf
318.72
Mop Psig
960
Mop Cfr Section
192.619(A)(2)
Maop Established Date
2017-12-17 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Gas Required Odorized Ind
Yes
Gas Odorized Ind
Yes
Pipeline Function
Transmission System
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Accident Identifier
Notification From Emergency Responder
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Car crashed into station.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Other Outside Force Damage
Cause Details
Damage By Car, Truck, Or Other Motorized Vehicle/equipment Not Engaged In Excavation
Outside Force Type
Damage By Car, Truck, Or Other Motorized Vehicle/equipment Not Engaged In Excavation
Vehicle Subtype
Third Party
Driver Issued Citation Ind
Yes
Citation Other Ind
Yes
Citation Other Detail
Unknown, Not Provided In The Police Report
Driver In Control Ind
Unknown
Estimated Speed Unknown Ind
Yes
Vehicle Type
Passenger Car
Vehicle Travel From
Roadway
Vehicle Travel Distance Ft
125
Protections Installed Ind
Yes
Protection Barricades Ind
Yes
Preparer Name
J***** B******
Preparer Title
Operations Manager
Preparer Email
J*************@a**********.com
Preparer Telephone
214-206-2606
Local Contact Name
J***** B******
Local Contact Email
J*************@a**********.com
Local Contact Telephone
214-206-2606
Authorizer Name
M**** S*****
Authorizer Title
Vp Technical Services
Authorizer Telephone
214-206-2033
Authorizer Email
M***********@a**********.com
Narrative
Preliminary investigation indicates that on march 23, 2022, a vehicle traveling at a high rate of speed going southbound in the northbound lanes of hwy 360 crossed over u.S. 287 southbound service road, traveled an additional 125 feet, and struck an atmos energy measuring station near mansfield, texas. The gas ignited. The system pressure was at 655 psig at the time of the incident. Atmos energy was notified by emergency responders at approximately 1:40 a.M. And atmos energy personnel arrived onsite at 2:40 a.M. The fire department had the area sealed off until 3:00 a.M., at which time the technician was able to access the scene and determine that our facility was involved. At 3:43 a.M., an upstream valve was activated to stop the flow of gas, which resulted in the loss of service to atmos energys customer, sienergy. Sienergy informed atmos energy that it had approximately 1,110 customers downstream that lost service. The fire department evacuated a one-mile radius. Regarding question a23 of this report, the number of persons evacuated is unknown, however there were 593 structures in the evacuation zone.
Report Received Date 2022-04-22 00:00:00
Iyear 2022
Report Number 20220048
Supplemental Number 37133
Report Type Supplemental Final
Operator Id 31978 PHMSA Enforcement
Name Atmos Pipeline - Texas
Operator Street Address 5420 Lbj Freeway, Suite 1500
Operator City Name Dallas
Operator State Abbreviation TX
Operator Postal Code 75240
Local Datetime 2022-03-23 04:30:00
Time Zone Central
Daylight Savings Ind Yes
Location Latitude 32.52089 Google Maps OpenStreetMap
Location Longitude -97.08222 Google Maps OpenStreetMap
Nrc Rpt Num 1331720 NRC Report How to search
Nrc Rpt Datetime 2022-03-23 04:21:00
Additional Nrc Report Numbers 1331898
Commodity Released Type Natural Gas
Unintentional Release 33202
Intentional Release 0
Accompanying Liquid 0
Fatality Ind Yes
Num Emp Fatalities 0
Num Contr Fatalities 0
Num Er Fatalities 0
Num Worker Fatalities 0
Num Gp Fatalities 1
Fatal 1
Injury Ind No
Injure 0
Status When Identified Normal Operation, Includes Pauses During Maintenance
Shutdown Due Accident Ind Yes
Shutdown Datetime 2022-03-23 03:43:00
Restart Datetime 2022-03-30 20:30:00
Ignite Ind Yes
Ignite Datetime 2022-03-23 01:14:00
How Extinguished Other
How Extinguished Other Detail Shut Valve
Gas Consumed By Fire In Mcf 33202
Explode Ind No
Num Pub Evacuated 593
Incident Identified Datetime 2022-03-23 03:00:00
On Site Datetime 2022-03-23 02:40:00
On Off Shore Onshore
Onshore State Abbreviation Tx
Onshore Postal Code 76063
Onshore City Name Mansfield
Onshore County Name Ellis
Designated Location Survey Station No.
Designated Name 162
Pipe Fac Name Line X64
Segment Name Ms 8981.1
Federal No
Location Type Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
System Part Involved Onshore Regulator/metering Station Equipment And Piping
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 8
Puddle Weld Ind No
Pipe Wall Thickness 0.322
Pipe Smys 52000
Pipe Specification X52
Pipe Seam Type Longitudinal Erw - High Frequency
Pipe Manufacturer Unknown
Pipe Coating Type Paint
Coating Applied Ind Yes
Installation Year 2017
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Rupture
Rupture Orient Circumferential
Rupture Length 4
Rupture Width 4
Class Location Type Class 1 Location
Could Be Hca No
Pir Radius 184
Heat Damage Ind No
Non Heat Damage Ind No
Hca Fatalities Ind No
Did Occur In Mca Ind Yes
Mca Paved Surface Freeway Ind Yes
Est Cost Oper Paid 60000
Est Cost Unintentional Release 175751
Est Cost Intentional Release 0
Est Cost Prop Damage 1550000
Est Cost Emergency 50000
Est Cost Other 0
Gas Cost In Mcf 5.2934
Prpty 1835751
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 1100
Num Business Building Affctd 10
Wildlife Impact Ind No
Accident Psig 655
Gas Flow In Pipe In Mcf 318.72
Mop Psig 960
Mop Cfr Section 192.619(A)(2) View CFR 49 §192
Maop Established Date 2017-12-17 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Gas Required Odorized Ind Yes
Gas Odorized Ind Yes
Pipeline Function Transmission System
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Accident Identifier Notification From Emergency Responder
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Car crashed into station.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Other Outside Force Damage
Cause Details Damage By Car, Truck, Or Other Motorized Vehicle/equipment Not Engaged In Excavation
Outside Force Type Damage By Car, Truck, Or Other Motorized Vehicle/equipment Not Engaged In Excavation
Vehicle Subtype Third Party
Driver Issued Citation Ind Yes
Citation Other Ind Yes
Citation Other Detail Unknown, Not Provided In The Police Report
Driver In Control Ind Unknown
Estimated Speed Unknown Ind Yes
Vehicle Type Passenger Car
Vehicle Travel From Roadway
Vehicle Travel Distance Ft 125
Protections Installed Ind Yes
Protection Barricades Ind Yes
Preparer Name J***** B******
Preparer Title Operations Manager
Preparer Email J*************@a**********.com
Preparer Telephone 214-206-2606
Local Contact Name J***** B******
Local Contact Email J*************@a**********.com
Local Contact Telephone 214-206-2606
Authorizer Name M**** S*****
Authorizer Title Vp Technical Services
Authorizer Telephone 214-206-2033
Authorizer Email M***********@a**********.com
Narrative Preliminary investigation indicates that on march 23, 2022, a vehicle traveling at a high rate of speed going southbound in the northbound lanes of hwy 360 crossed over u.S. 287 southbound service road, traveled an additional 125 feet, and struck an atmos energy measuring station near mansfield, texas. The gas ignited. The system pressure was at 655 psig at the time of the incident. Atmos energy was notified by emergency responders at approximately 1:40 a.M. And atmos energy personnel arrived onsite at 2:40 a.M. The fire department had the area sealed off until 3:00 a.M., at which time the technician was able to access the scene and determine that our facility was involved. At 3:43 a.M., an upstream valve was activated to stop the flow of gas, which resulted in the loss of service to atmos energys customer, sienergy. Sienergy informed atmos energy that it had approximately 1,110 customers downstream that lost service. The fire department evacuated a one-mile radius. Regarding question a23 of this report, the number of persons evacuated is unknown, however there were 593 structures in the evacuation zone.

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