GD incident on 2022-05-12 — MS

Operator
Atmos Energy Corporation - Mississippi
Cause
Locating Issue
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$10,001
Incident datetime
2022-05-12 08:45
Report number
Location
MS, MONROE
Narrative
Atmos energy's second-party contractor was in the process of replacing a critical valve on an 8-inch high pressure distribution line near aberdeen, ms. The project was being worked under mississippi onecall locate ticket #2204814572130, and proper locate practices were used prior to beginning the project using all available information on the assets in the area and locate technology. Unknown to atmos energy or the second party contractor, there was an unlocatable and unmapped 2-inch nipple and valve located in the vertical position on the carrier pipe, and this unmapped and unlocatable asset was damaged during excavation activities. The contractor responded to the damage using appropriate emergency response practices. In order to eliminate the hazardous condition, a stopple fitting was welded onto the carrier pipe and tapped. During the repair, the unintentional loss of gas exceeded the reportable threshold, and atmos energy reported the damage as an incident.
Detailed record list
Occurred At
2022-05-12 08:45:00
Year
2022
Report Received Date
2022-06-10 00:00:00
Iyear
2022.0
Report Number
20220040.0
Supplemental Number
37711.0
Report Type
Supplemental Final
Operator Id
Name
Atmos Energy Corporation - Mississippi
Operator Street Address
5430 Lbj Freeway Suite 1800
Operator City Name
Dallas
Operator State Abbreviation
TX
Operator Postal Code
75240
Local Datetime
2022-05-12 14:30:00
Time Zone
Central
Daylight Savings Ind
Yes
Location Street Address
100333 Imc Road
Location City Name
Aberdeen
Location County Name
Monroe
Location State Abbreviation
MS
Location Postal Code
39730
Location Latitude
Location Longitude
Flow Cont Key Crit Ind
Yes
Flow Cont Stopple Fitng Ind
Yes
Nrc Rpt Datetime
2022-05-12 14:42:00
Nrc Rpt Num
Additional Nrc Report Numbers
1335944
Commodity Released Type
Natural Gas
Unintentional Release
5914.0
Intentional Release
379.0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
No
Num Pub Evacuated
0.0
Incident Identified Datetime
2022-05-12 08:45:00
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Initial Responder Com Datetime
2022-05-12 08:45:00
On Site Datetime
2022-05-12 09:10:00
Federal
No
Location Type
Utility Right-Of-Way / Easement
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
42.0
Other Underground Facilities
No
Crossing
No
Pipe Facility Type
Investor Owned
System Part Involved
Main
Installation Year
1969.0
Manufactured Year
1969.0
Pipe Diameter
8.0
Pipe Specification
Api 5lx-1968
Pipe Manufacturer
Republic Steel
Material Involved
Steel
Steel Seam Type
Longitudinal Erw - Unknown Frequency
Wt Steel
0.188
Release Type
Leak
Leak Type
Other
Leak Type Other
2-Inch Nipple Sheared Off Pipe
Class Location Type
Class 1 Location
Est Cost Oper Paid
0.0
Est Cost Prop Damage
10001.0
Est Cost Emergency
12575.0
Est Cost Other
0.0
Gas Cost In Mcf
7.3268
Est Cost Unintentional Release
43331.0
Est Cost Intentional Release
2777.0
Prpty
68684.0
Commercial Affected
0.0
Industrial Affected
1.0
Residences Affected
0.0
Num Persons Hosp Not Ovnght
0.0
Num Injured Treated By Emt
0.0
Num Resident Building Affctd
0.0
Num Business Building Affctd
1.0
Accident Psig
250.0
Normal Psig
350.0
Mop Psig
385.0
Mop Cfr Section
192.619(A)(2)
Maop Established Date
1969-11-02 00:00:00
Accident Pressure
Pressure Did Not Exceed Maop
Gas Odorized System Type
Injection Pump
Gas Odorized Lvl Not Msrd Ind
Yes
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Contractor Working For The Operator
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Other than providing alerts to operations as the event occurred, the control room had no involvement in this incident.
Employee Drug Test Ind
No
Contractor Drug Test Ind
Yes
Num Contractors Tested
1
Num Contractors Failed
0
Cause
Excavation Damage
Cause Details
Excavation Damage By Operator's Contractor (Second Party)
Ex Party Type
Excavation Damage By Operator's Contractor (Second Party)
Notify Cga Dirt
No
Private Row Ind
Yes
Private Subtype
Private Easement
Pipeline Easement Row Ind
Yes
Excavator Type
Contractor
Excavator Equipment
Backhoe/trackhoe
Work Performed
Natural Gas
One Call Notified Ind
Yes
One Call Ticket Num
2.20428e+13
Locator Type
Contract Locator
Visible Marks
Yes
Service Interruption
Yes
Service Interruption Hours
11.0
Root Cause Category
Locating Issue
Root Cause Type
Facility Not Marked Due To Incorrect Facility Records/maps
Preparer Name
D*** M*****
Preparer Title
Manager Of Compliance
Preparer Email
D**********@a**********.com
Preparer Telephone
6015925360
Local Contact Name
W*** S*******
Local Contact Email
W************@a**********.com
Local Contact Telephone
6622512018
Authorizer Name
J**** E* M*******
Authorizer Title
Vice President Technical Services
Authorizer Telephone
6016249408
Authorizer Email
J*************@a**********.com
Narrative
Atmos energy's second-party contractor was in the process of replacing a critical valve on an 8-inch high pressure distribution line near aberdeen, ms. The project was being worked under mississippi onecall locate ticket #2204814572130, and proper locate practices were used prior to beginning the project using all available information on the assets in the area and locate technology. Unknown to atmos energy or the second party contractor, there was an unlocatable and unmapped 2-inch nipple and valve located in the vertical position on the carrier pipe, and this unmapped and unlocatable asset was damaged during excavation activities. The contractor responded to the damage using appropriate emergency response practices. In order to eliminate the hazardous condition, a stopple fitting was welded onto the carrier pipe and tapped. During the repair, the unintentional loss of gas exceeded the reportable threshold, and atmos energy reported the damage as an incident.
Occurred At 2022-05-12 08:45:00
Year 2022
Report Received Date 2022-06-10 00:00:00
Iyear 2022.0
Report Number 20220040.0
Supplemental Number 37711.0
Report Type Supplemental Final
Operator Id 12582 PHMSA Enforcement
Name Atmos Energy Corporation - Mississippi
Operator Street Address 5430 Lbj Freeway Suite 1800
Operator City Name Dallas
Operator State Abbreviation TX
Operator Postal Code 75240
Local Datetime 2022-05-12 14:30:00
Time Zone Central
Daylight Savings Ind Yes
Location Street Address 100333 Imc Road
Location City Name Aberdeen
Location County Name Monroe
Location State Abbreviation MS
Location Postal Code 39730
Location Latitude 33.768389 Google Maps OpenStreetMap
Location Longitude -88.57225 Google Maps OpenStreetMap
Flow Cont Key Crit Ind Yes
Flow Cont Stopple Fitng Ind Yes
Nrc Rpt Datetime 2022-05-12 14:42:00
Nrc Rpt Num 1335844 NRC Report How to search
Additional Nrc Report Numbers 1335944
Commodity Released Type Natural Gas
Unintentional Release 5914.0
Intentional Release 379.0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind No
Num Pub Evacuated 0.0
Incident Identified Datetime 2022-05-12 08:45:00
Communication State Fed Ind Yes
Party Initiated Communication Operator
Initial Responder Com Datetime 2022-05-12 08:45:00
On Site Datetime 2022-05-12 09:10:00
Federal No
Location Type Utility Right-Of-Way / Easement
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 42.0
Other Underground Facilities No
Crossing No
Pipe Facility Type Investor Owned
System Part Involved Main
Installation Year 1969.0
Manufactured Year 1969.0
Pipe Diameter 8.0
Pipe Specification Api 5lx-1968
Pipe Manufacturer Republic Steel
Material Involved Steel
Steel Seam Type Longitudinal Erw - Unknown Frequency
Wt Steel 0.188
Release Type Leak
Leak Type Other
Leak Type Other 2-Inch Nipple Sheared Off Pipe
Class Location Type Class 1 Location
Est Cost Oper Paid 0.0
Est Cost Prop Damage 10001.0
Est Cost Emergency 12575.0
Est Cost Other 0.0
Gas Cost In Mcf 7.3268
Est Cost Unintentional Release 43331.0
Est Cost Intentional Release 2777.0
Prpty 68684.0
Commercial Affected 0.0
Industrial Affected 1.0
Residences Affected 0.0
Num Persons Hosp Not Ovnght 0.0
Num Injured Treated By Emt 0.0
Num Resident Building Affctd 0.0
Num Business Building Affctd 1.0
Accident Psig 250.0
Normal Psig 350.0
Mop Psig 385.0
Mop Cfr Section 192.619(A)(2) View CFR 49 §192
Maop Established Date 1969-11-02 00:00:00
Accident Pressure Pressure Did Not Exceed Maop
Gas Odorized System Type Injection Pump
Gas Odorized Lvl Not Msrd Ind Yes
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Contractor Working For The Operator
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Other than providing alerts to operations as the event occurred, the control room had no involvement in this incident.
Employee Drug Test Ind No
Contractor Drug Test Ind Yes
Num Contractors Tested 1
Num Contractors Failed 0
Cause Excavation Damage
Cause Details Excavation Damage By Operator's Contractor (Second Party)
Ex Party Type Excavation Damage By Operator's Contractor (Second Party)
Notify Cga Dirt No
Private Row Ind Yes
Private Subtype Private Easement
Pipeline Easement Row Ind Yes
Excavator Type Contractor
Excavator Equipment Backhoe/trackhoe
Work Performed Natural Gas
One Call Notified Ind Yes
One Call Ticket Num 2.20428e+13
Locator Type Contract Locator
Visible Marks Yes
Service Interruption Yes
Service Interruption Hours 11.0
Root Cause Category Locating Issue
Root Cause Type Facility Not Marked Due To Incorrect Facility Records/maps
Preparer Name D*** M*****
Preparer Title Manager Of Compliance
Preparer Email D**********@a**********.com
Preparer Telephone 6015925360
Local Contact Name W*** S*******
Local Contact Email W************@a**********.com
Local Contact Telephone 6622512018
Authorizer Name J**** E* M*******
Authorizer Title Vice President Technical Services
Authorizer Telephone 6016249408
Authorizer Email J*************@a**********.com
Narrative Atmos energy's second-party contractor was in the process of replacing a critical valve on an 8-inch high pressure distribution line near aberdeen, ms. The project was being worked under mississippi onecall locate ticket #2204814572130, and proper locate practices were used prior to beginning the project using all available information on the assets in the area and locate technology. Unknown to atmos energy or the second party contractor, there was an unlocatable and unmapped 2-inch nipple and valve located in the vertical position on the carrier pipe, and this unmapped and unlocatable asset was damaged during excavation activities. The contractor responded to the damage using appropriate emergency response practices. In order to eliminate the hazardous condition, a stopple fitting was welded onto the carrier pipe and tapped. During the repair, the unintentional loss of gas exceeded the reportable threshold, and atmos energy reported the damage as an incident.

All rights reserved. Copyright © by ClearPHMSA