GTG incident on 2022-02-27 — TX

Operator
Energy Transfer Company
Cause
Equipment Failure
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$500
Incident datetime
2022-02-27 06:20
Report number
Location
TX
Narrative
On 2/27/22 at 6:20, energy transfer gas control called energy transfer (etc) operations technician to notify him of a station esd at the bryson facility. Etc operations technician arrived at the bryson facility at 7:05 and found the station blowdown actively releasing natural gas to atmosphere. Etc operations technician identified the valve that failed to close during the esd and at 7:09 he manually closed the valve to stop the release. The quantity of gas released was calculated and determined to be reportable at 08:20. Initial notification was made to the nrc (report # 1329823) at 8:50 on 2/27/22. The 48-hour update was made to nrc (report # 1329940) at 8:41 on 3/01/22. Further investigation indicated the versa valve on the control valve failed to operate, therefore the control valve failed to close and allowed the release of natural gas from 9166 bryson tap - bryson compressor station 16-inch pipeline. The reason for the esd was loss of instrument air pressure. The 9166 bryson tap - bryson compressor station 16-inch pipeline was idle at the time of the esd. The pipeline was not shutdown as it was not currently needed, however it was available to return to service when needed, at 11:50 on 2/27/22.
Detailed record list
Report Received Date
2022-03-28 00:00:00
Iyear
2022
Report Number
20220038
Supplemental Number
36620
Report Type
Supplemental Final
Operator Id
Name
Energy Transfer Company
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2022-02-27 06:20:00
Time Zone
Central
Daylight Savings Ind
No
Location Latitude
Location Longitude
Nrc Rpt Num
Nrc Rpt Datetime
2022-02-27 08:53:00
Additional Nrc Report Numbers
1329940
Commodity Released Type
Natural Gas
Unintentional Release
4375.3
Intentional Release
0
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Status When Identified
Idle
Communication State Fed Ind
No
Ignite Ind
No
Upstream Action Taken
Valve Closure
Upstream Valve Close Datetime
2022-02-27 06:20:00
Downstream Action Taken
Valve Closure
Downstream Vlv Close Datetime
2022-02-27 07:09:00
Num Pub Evacuated
0
Incident Identified Datetime
2022-02-27 06:20:00
On Site Datetime
2022-02-27 07:05:00
On Off Shore
Onshore
Onshore State Abbreviation
Tx
Onshore Postal Code
76427
Onshore City Name
Bryson
Onshore County Name
Jack
Designated Location
Not Applicable
Pipe Fac Name
Bryson Tap - Bryson Compressor Station
Segment Name
9166 Bryson Tap_ Bryson Comp Station 16-Inch
Federal
No
Location Type
Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
System Part Involved
Onshore Pipeline, Including Valve Sites
Item Involved
Regulator/control Valve
Installation Year
2013
Manufactured Year
2013
Material Involved
Carbon Steel
Release Type
Other
Release Type Details
Release From Station Blowdown
Class Location Type
Class 1 Location
Could Be Hca
No
Pir Radius
384
Heat Damage Ind
No
Non Heat Damage Ind
No
Did Occur In Mca Ind
No
Est Cost Oper Paid
0
Est Cost Unintentional Release
20258
Est Cost Intentional Release
0
Est Cost Prop Damage
500
Est Cost Emergency
0
Est Cost Other
0
Gas Cost In Mcf
4.63
Prpty
20758
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Wildlife Impact Ind
No
Accident Psig
679
Gas Flow In Pipe In Mcf
0
Mop Psig
944
Mop Cfr Section
192.619(A)(1)
Maop Established Date
1974-01-01 00:00:00
Maop Reversal Flow Ind
Bi-Directional
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Gas Required Odorized Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Length Segment Isolated
50
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
Transmission System
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Accident Identifier
Controller
Operator Type
Operator Employee
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Controller actions did not affect the incident.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Malfunction Of Control/relief Equipment
Eq Failure Type
Malfunction Of Control/relief Equipment
Control Valve Ind
Yes
Instrumentation Ind
Yes
Eq Additional Other Ind
Yes
Eq Additional Other Details
Versa Valve Failed To Shift
Nf Temperature Ind
Yes
Preparer Name
A***** M*****
Preparer Title
Lead Specialist
Preparer Email
A************@e*************.com
Preparer Telephone
903-243-6541
Authorizer Name
C**** K*****
Authorizer Title
Manager - Regulatory Compliance
Authorizer Telephone
713-989-7077
Authorizer Email
C***********@e*************.com
Narrative
On 2/27/22 at 6:20, energy transfer gas control called energy transfer (etc) operations technician to notify him of a station esd at the bryson facility. Etc operations technician arrived at the bryson facility at 7:05 and found the station blowdown actively releasing natural gas to atmosphere. Etc operations technician identified the valve that failed to close during the esd and at 7:09 he manually closed the valve to stop the release. The quantity of gas released was calculated and determined to be reportable at 08:20. Initial notification was made to the nrc (report # 1329823) at 8:50 on 2/27/22. The 48-hour update was made to nrc (report # 1329940) at 8:41 on 3/01/22. Further investigation indicated the versa valve on the control valve failed to operate, therefore the control valve failed to close and allowed the release of natural gas from 9166 bryson tap - bryson compressor station 16-inch pipeline. The reason for the esd was loss of instrument air pressure. The 9166 bryson tap - bryson compressor station 16-inch pipeline was idle at the time of the esd. The pipeline was not shutdown as it was not currently needed, however it was available to return to service when needed, at 11:50 on 2/27/22.
Report Received Date 2022-03-28 00:00:00
Iyear 2022
Report Number 20220038
Supplemental Number 36620
Report Type Supplemental Final
Operator Id 32099 PHMSA Enforcement
Name Energy Transfer Company
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2022-02-27 06:20:00
Time Zone Central
Daylight Savings Ind No
Location Latitude 33.10916 Google Maps OpenStreetMap
Location Longitude -98.411693 Google Maps OpenStreetMap
Nrc Rpt Num 1329823 NRC Report How to search
Nrc Rpt Datetime 2022-02-27 08:53:00
Additional Nrc Report Numbers 1329940
Commodity Released Type Natural Gas
Unintentional Release 4375.3
Intentional Release 0
Accompanying Liquid 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Status When Identified Idle
Communication State Fed Ind No
Ignite Ind No
Upstream Action Taken Valve Closure
Upstream Valve Close Datetime 2022-02-27 06:20:00
Downstream Action Taken Valve Closure
Downstream Vlv Close Datetime 2022-02-27 07:09:00
Num Pub Evacuated 0
Incident Identified Datetime 2022-02-27 06:20:00
On Site Datetime 2022-02-27 07:05:00
On Off Shore Onshore
Onshore State Abbreviation Tx
Onshore Postal Code 76427
Onshore City Name Bryson
Onshore County Name Jack
Designated Location Not Applicable
Pipe Fac Name Bryson Tap - Bryson Compressor Station
Segment Name 9166 Bryson Tap_ Bryson Comp Station 16-Inch
Federal No
Location Type Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
System Part Involved Onshore Pipeline, Including Valve Sites
Item Involved Regulator/control Valve
Installation Year 2013
Manufactured Year 2013
Material Involved Carbon Steel
Release Type Other
Release Type Details Release From Station Blowdown
Class Location Type Class 1 Location
Could Be Hca No
Pir Radius 384
Heat Damage Ind No
Non Heat Damage Ind No
Did Occur In Mca Ind No
Est Cost Oper Paid 0
Est Cost Unintentional Release 20258
Est Cost Intentional Release 0
Est Cost Prop Damage 500
Est Cost Emergency 0
Est Cost Other 0
Gas Cost In Mcf 4.63
Prpty 20758
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Wildlife Impact Ind No
Accident Psig 679
Gas Flow In Pipe In Mcf 0
Mop Psig 944
Mop Cfr Section 192.619(A)(1) View CFR 49 §192
Maop Established Date 1974-01-01 00:00:00
Maop Reversal Flow Ind Bi-Directional
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Gas Required Odorized Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Length Segment Isolated 50
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function Transmission System
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Accident Identifier Controller
Operator Type Operator Employee
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Controller actions did not affect the incident.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Malfunction Of Control/relief Equipment
Eq Failure Type Malfunction Of Control/relief Equipment
Control Valve Ind Yes
Instrumentation Ind Yes
Eq Additional Other Ind Yes
Eq Additional Other Details Versa Valve Failed To Shift
Nf Temperature Ind Yes
Preparer Name A***** M*****
Preparer Title Lead Specialist
Preparer Email A************@e*************.com
Preparer Telephone 903-243-6541
Authorizer Name C**** K*****
Authorizer Title Manager - Regulatory Compliance
Authorizer Telephone 713-989-7077
Authorizer Email C***********@e*************.com
Narrative On 2/27/22 at 6:20, energy transfer gas control called energy transfer (etc) operations technician to notify him of a station esd at the bryson facility. Etc operations technician arrived at the bryson facility at 7:05 and found the station blowdown actively releasing natural gas to atmosphere. Etc operations technician identified the valve that failed to close during the esd and at 7:09 he manually closed the valve to stop the release. The quantity of gas released was calculated and determined to be reportable at 08:20. Initial notification was made to the nrc (report # 1329823) at 8:50 on 2/27/22. The 48-hour update was made to nrc (report # 1329940) at 8:41 on 3/01/22. Further investigation indicated the versa valve on the control valve failed to operate, therefore the control valve failed to close and allowed the release of natural gas from 9166 bryson tap - bryson compressor station 16-inch pipeline. The reason for the esd was loss of instrument air pressure. The 9166 bryson tap - bryson compressor station 16-inch pipeline was idle at the time of the esd. The pipeline was not shutdown as it was not currently needed, however it was available to return to service when needed, at 11:50 on 2/27/22.

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