Incident details
Operator, cause, commodity and consequences with raw source fields.
GD incident on 2022-04-22 — IA
Operator
Black Hills Energy
Cause
Other Outside Force Damage
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$3,000
Incident datetime
2022-04-22 04:18
Report number
Location
IA, MONONA
Narrative
On 4/22/2022 at 04:18 central time black hills energy was notified by emergency responders of a residential fire and requested bhe to respond. The location is 302 maple in onawa iowa. Upon arrival the technician found the home engulfed in flames. The fire had caused damage to the meter and regulator. The service line was excavated at the street at a safe distance from the fire and cut off and capped.
Detailed record list
Occurred At
2022-04-22 04:18:00
Year
2022
Report Received Date
2022-05-20 00:00:00
Iyear
2022.0
Report Number
20220037.0
Supplemental Number
36688.0
Report Type
Original
Operator Id
15359
Name
Black Hills Energy
Operator Street Address
2287 College Road Po Box 2006
Operator City Name
Council Bluffs
Operator State Abbreviation
IA
Operator Postal Code
51502
Local Datetime
2022-04-22 04:18:00
Time Zone
Central
Daylight Savings Ind
Yes
Location Street Address
302 Maple
Location City Name
Onawa
Location County Name
Monona
Location State Abbreviation
IA
Location Postal Code
51040
Location Latitude
42.0212276
Location Longitude
-96.0879099
Flow Cont Squeeze Off Ind
Yes
Nrc Rpt Datetime
2022-04-22 06:06:00
Nrc Rpt Num
1334144
Additional Nrc Report Numbers
1334323
Commodity Released Type
Natural Gas
Unintentional Release
8.5
Intentional Release
0.0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
Yes
Ignite Datetime
2022-04-22 00:00:00
How Extinguished
Local/state/federal Emergency Responder
Gas Consumed By Fire In Mcf
8.5
Explode Ind
No
Num Pub Evacuated
1.0
Incident Identified Datetime
2022-04-22 04:18:00
On Site Datetime
2022-04-22 00:50:00
Federal
No
Location Type
Private Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance (E.g. Value Or Regulator Station, Outdoor Meter Set)
Crossing
No
Pipe Facility Type
Investor Owned
System Part Involved
Service
Installation Year
2000.0
Customer Type
Single Family Residential
Was Efv Installed Before Ind
No
Curb Valve Inst Before Inc Ind
No
Pipe Diameter
0.5
Pipe Specification
2406
Pipe Manufacturer
Unknown
Material Involved
Plastic
Plastic Type
Polyethylene (Pe)
Plastic Sdr
7
Material Pe Pipe Code
2406
Release Type
Other
Release Type Details
Leak Caused By Fire Damage To Meter And Regulator.
Class Location Type
Class 4 Location
Est Cost Oper Paid
11200.0
Est Cost Prop Damage
3000.0
Est Cost Emergency
15000.0
Est Cost Other
0.0
Gas Cost In Mcf
8.14
Est Cost Unintentional Release
69.0
Est Cost Intentional Release
0.0
Prpty
29269.0
Commercial Affected
0.0
Industrial Affected
0.0
Residences Affected
1.0
Num Persons Hosp Not Ovnght
0.0
Num Injured Treated By Emt
0.0
Num Resident Building Affctd
1.0
Num Business Building Affctd
0.0
Accident Psig
25.0
Normal Psig
25.0
Mop Psig
66.6
Mop Cfr Section
192.619(A)(1)
Maop Established Date
2000-01-30 00:00:00
Accident Pressure
Pressure Did Not Exceed Maop
Gas Odorized System Type
Injection Pump
Gas Odorized Level
0.5
Scada In Place Ind
No
Accident Identifier
Notification From Emergency Responder
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Other Outside Force Damage
Cause Details
Nearby Industrial, Man-Made, Or Other Fire/explosion As Primary Cause Of Incident
Outside Force Type
Nearby Industrial, Man-Made, Or Other Fire/explosion As Primary Cause Of Incident
Osf Nearby Industrial Ind
Yes
Preparer Name
A****** E******
Preparer Title
Supervisor Pipe Line Safety Professional
Preparer Email
T***********@b*************.com
Preparer Telephone
15635854014
Preparer Fax
563-583-0850
Local Contact Name
G*** H****
Local Contact Email
G*********@b*****************
Local Contact Telephone
1-402-221-2536
Authorizer Name
T*** J*** E******
Authorizer Title
Supervisor Pipe Line Safety Professional
Authorizer Telephone
15635854014
Authorizer Email
T***********@b*************.com
Narrative
On 4/22/2022 at 04:18 central time black hills energy was notified by emergency responders of a residential fire and requested bhe to respond. The location is 302 maple in onawa iowa. Upon arrival the technician found the home engulfed in flames. The fire had caused damage to the meter and regulator. The service line was excavated at the street at a safe distance from the fire and cut off and capped.
| Occurred At | 2022-04-22 04:18:00 |
|---|---|
| Year | 2022 |
| Report Received Date | 2022-05-20 00:00:00 |
| Iyear | 2022.0 |
| Report Number | 20220037.0 |
| Supplemental Number | 36688.0 |
| Report Type | Original |
| Operator Id | 15359 PHMSA Enforcement |
| Name | Black Hills Energy |
| Operator Street Address | 2287 College Road Po Box 2006 |
| Operator City Name | Council Bluffs |
| Operator State Abbreviation | IA |
| Operator Postal Code | 51502 |
| Local Datetime | 2022-04-22 04:18:00 |
| Time Zone | Central |
| Daylight Savings Ind | Yes |
| Location Street Address | 302 Maple |
| Location City Name | Onawa |
| Location County Name | Monona |
| Location State Abbreviation | IA |
| Location Postal Code | 51040 |
| Location Latitude | 42.0212276 Google Maps OpenStreetMap |
| Location Longitude | -96.0879099 Google Maps OpenStreetMap |
| Flow Cont Squeeze Off Ind | Yes |
| Nrc Rpt Datetime | 2022-04-22 06:06:00 |
| Nrc Rpt Num | 1334144 NRC Report How to search |
| Additional Nrc Report Numbers | 1334323 |
| Commodity Released Type | Natural Gas |
| Unintentional Release | 8.5 |
| Intentional Release | 0.0 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Ignite Ind | Yes |
| Ignite Datetime | 2022-04-22 00:00:00 |
| How Extinguished | Local/state/federal Emergency Responder |
| Gas Consumed By Fire In Mcf | 8.5 |
| Explode Ind | No |
| Num Pub Evacuated | 1.0 |
| Incident Identified Datetime | 2022-04-22 04:18:00 |
| On Site Datetime | 2022-04-22 00:50:00 |
| Federal | No |
| Location Type | Private Property |
| Incident Area Type | Aboveground |
| Incident Area Subtype | Typical Aboveground Facility Piping Or Appurtenance (E.g. Value Or Regulator Station, Outdoor Meter Set) |
| Crossing | No |
| Pipe Facility Type | Investor Owned |
| System Part Involved | Service |
| Installation Year | 2000.0 |
| Customer Type | Single Family Residential |
| Was Efv Installed Before Ind | No |
| Curb Valve Inst Before Inc Ind | No |
| Pipe Diameter | 0.5 |
| Pipe Specification | 2406 |
| Pipe Manufacturer | Unknown |
| Material Involved | Plastic |
| Plastic Type | Polyethylene (Pe) |
| Plastic Sdr | 7 |
| Material Pe Pipe Code | 2406 |
| Release Type | Other |
| Release Type Details | Leak Caused By Fire Damage To Meter And Regulator. |
| Class Location Type | Class 4 Location |
| Est Cost Oper Paid | 11200.0 |
| Est Cost Prop Damage | 3000.0 |
| Est Cost Emergency | 15000.0 |
| Est Cost Other | 0.0 |
| Gas Cost In Mcf | 8.14 |
| Est Cost Unintentional Release | 69.0 |
| Est Cost Intentional Release | 0.0 |
| Prpty | 29269.0 |
| Commercial Affected | 0.0 |
| Industrial Affected | 0.0 |
| Residences Affected | 1.0 |
| Num Persons Hosp Not Ovnght | 0.0 |
| Num Injured Treated By Emt | 0.0 |
| Num Resident Building Affctd | 1.0 |
| Num Business Building Affctd | 0.0 |
| Accident Psig | 25.0 |
| Normal Psig | 25.0 |
| Mop Psig | 66.6 |
| Mop Cfr Section | 192.619(A)(1) View CFR 49 §192 |
| Maop Established Date | 2000-01-30 00:00:00 |
| Accident Pressure | Pressure Did Not Exceed Maop |
| Gas Odorized System Type | Injection Pump |
| Gas Odorized Level | 0.5 |
| Scada In Place Ind | No |
| Accident Identifier | Notification From Emergency Responder |
| Investigation Status | No, the facility was not monitored by a controller(s) at the time of the incident |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Other Outside Force Damage |
| Cause Details | Nearby Industrial, Man-Made, Or Other Fire/explosion As Primary Cause Of Incident |
| Outside Force Type | Nearby Industrial, Man-Made, Or Other Fire/explosion As Primary Cause Of Incident |
| Osf Nearby Industrial Ind | Yes |
| Preparer Name | A****** E****** |
| Preparer Title | Supervisor Pipe Line Safety Professional |
| Preparer Email | T***********@b*************.com |
| Preparer Telephone | 15635854014 |
| Preparer Fax | 563-583-0850 |
| Local Contact Name | G*** H**** |
| Local Contact Email | G*********@b***************** |
| Local Contact Telephone | 1-402-221-2536 |
| Authorizer Name | T*** J*** E****** |
| Authorizer Title | Supervisor Pipe Line Safety Professional |
| Authorizer Telephone | 15635854014 |
| Authorizer Email | T***********@b*************.com |
| Narrative | On 4/22/2022 at 04:18 central time black hills energy was notified by emergency responders of a residential fire and requested bhe to respond. The location is 302 maple in onawa iowa. Upon arrival the technician found the home engulfed in flames. The fire had caused damage to the meter and regulator. The service line was excavated at the street at a safe distance from the fire and cut off and capped. |
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