GTG incident on 2022-01-21 — TX

Operator
Enable Oklahoma Intrastate Transmission, Llc
Cause
Equipment Failure
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$9,500
Incident datetime
2022-01-21 08:30
Report number
Location
TX
Narrative
On 01/21/2022 a relief valve was discovered venting when a energy transfer employee arrived at the northeast power station in oologah, oklahoma. Gauges were installed to verify pressures. The relief valve was immediately closed and upon investigation it was determined that a reportable release of natural gas had occurred. The nrc was notified (nrc# 1327084, 1327011) and an investigation was initiated to determine cause. It was determined that regulator malfunction had occurred due to ice buildup on the regulator. The regulator was de-iced and the relief valve was rebuilt before being placed back into service. Extreme temperatures of 16 degrees occured on ths day and contributed to icing of the regulator, and ultimately caused the release.
Detailed record list
Report Received Date
2022-02-14 00:00:00
Iyear
2022
Report Number
20220012
Supplemental Number
36873
Report Type
Supplemental Final
Operator Id
Name
Enable Oklahoma Intrastate Transmission, Llc
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2022-01-21 08:30:00
Time Zone
Central
Daylight Savings Ind
No
Location Latitude
Location Longitude
Nrc Rpt Num
Nrc Rpt Datetime
2022-01-21 09:46:00
Additional Nrc Report Numbers
1327084
Commodity Released Type
Natural Gas
Unintentional Release
4172
Intentional Release
0
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Status When Identified
Normal Operation, Includes Pauses During Maintenance
Shutdown Due Accident Ind
No
Shutdown Explain
Valve Was Closed To Re-Seat Relief Valve
Communication State Fed Ind
No
Ignite Ind
No
Num Pub Evacuated
0
Incident Identified Datetime
2022-01-21 08:30:00
On Site Datetime
2022-01-21 08:30:00
On Off Shore
Onshore
Onshore State Abbreviation
Ok
Onshore Postal Code
74053
Onshore City Name
Oologah
Onshore County Name
Rogers
Designated Location
Not Applicable
Pipe Fac Name
Northeast Power Station
Segment Name
Northeast Power Station
Federal
No
Location Type
Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
System Part Involved
Onshore Regulator/metering Station Equipment And Piping
Item Involved
Regulator/control Valve
Installation Year
Unknown
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Other
Leak Type Other
Regulator Failure Due To Icing
Class Location Type
Class 3 Location
Could Be Hca
Yes
Determination Method
Method2
Pir Radius
407
Heat Damage Ind
No
Non Heat Damage Ind
No
Est Cost Oper Paid
0
Est Cost Unintentional Release
16313
Est Cost Intentional Release
0
Est Cost Prop Damage
9500
Est Cost Emergency
500
Est Cost Other
0
Gas Cost In Mcf
3.91
Prpty
26313
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Wildlife Impact Ind
No
Accident Psig
390
Gas Flow In Pipe In Mcf
2.68
Mop Psig
605
Mop Cfr Section
192.619(A)(2)
Maop Established Date
2019-05-23 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Gas Required Odorized Ind
No
Pipeline Function
Transmission System
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Equipment failure
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Malfunction Of Control/relief Equipment
Eq Failure Type
Malfunction Of Control/relief Equipment
Pressure Regulator Ind
Yes
Eq Additional Other Ind
Yes
Eq Additional Other Details
Icing
Nf Temperature Ind
Yes
Eqf Control Releaf Ind
Yes
Preparer Name
J**** C****
Preparer Title
Sr. Manager Regulatory Compliance
Preparer Email
J**********@e*************
Preparer Telephone
4055768230
Local Contact Name
J**** C****
Local Contact Email
J**********@e*************.com
Local Contact Telephone
4055768230
Authorizer Name
J**** C****
Authorizer Title
Lead Specialist
Authorizer Telephone
4055768230
Authorizer Email
J**********@e*************.com
Narrative
On 01/21/2022 a relief valve was discovered venting when a energy transfer employee arrived at the northeast power station in oologah, oklahoma. Gauges were installed to verify pressures. The relief valve was immediately closed and upon investigation it was determined that a reportable release of natural gas had occurred. The nrc was notified (nrc# 1327084, 1327011) and an investigation was initiated to determine cause. It was determined that regulator malfunction had occurred due to ice buildup on the regulator. The regulator was de-iced and the relief valve was rebuilt before being placed back into service. Extreme temperatures of 16 degrees occured on ths day and contributed to icing of the regulator, and ultimately caused the release.
Report Received Date 2022-02-14 00:00:00
Iyear 2022
Report Number 20220012
Supplemental Number 36873
Report Type Supplemental Final
Operator Id 26330 PHMSA Enforcement
Name Enable Oklahoma Intrastate Transmission, Llc
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2022-01-21 08:30:00
Time Zone Central
Daylight Savings Ind No
Location Latitude 36.429269 Google Maps OpenStreetMap
Location Longitude -95.70107 Google Maps OpenStreetMap
Nrc Rpt Num 1327011 NRC Report How to search
Nrc Rpt Datetime 2022-01-21 09:46:00
Additional Nrc Report Numbers 1327084
Commodity Released Type Natural Gas
Unintentional Release 4172
Intentional Release 0
Accompanying Liquid 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Status When Identified Normal Operation, Includes Pauses During Maintenance
Shutdown Due Accident Ind No
Shutdown Explain Valve Was Closed To Re-Seat Relief Valve
Communication State Fed Ind No
Ignite Ind No
Num Pub Evacuated 0
Incident Identified Datetime 2022-01-21 08:30:00
On Site Datetime 2022-01-21 08:30:00
On Off Shore Onshore
Onshore State Abbreviation Ok
Onshore Postal Code 74053
Onshore City Name Oologah
Onshore County Name Rogers
Designated Location Not Applicable
Pipe Fac Name Northeast Power Station
Segment Name Northeast Power Station
Federal No
Location Type Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
System Part Involved Onshore Regulator/metering Station Equipment And Piping
Item Involved Regulator/control Valve
Installation Year Unknown
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Other
Leak Type Other Regulator Failure Due To Icing
Class Location Type Class 3 Location
Could Be Hca Yes
Determination Method Method2
Pir Radius 407
Heat Damage Ind No
Non Heat Damage Ind No
Est Cost Oper Paid 0
Est Cost Unintentional Release 16313
Est Cost Intentional Release 0
Est Cost Prop Damage 9500
Est Cost Emergency 500
Est Cost Other 0
Gas Cost In Mcf 3.91
Prpty 26313
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Wildlife Impact Ind No
Accident Psig 390
Gas Flow In Pipe In Mcf 2.68
Mop Psig 605
Mop Cfr Section 192.619(A)(2) View CFR 49 §192
Maop Established Date 2019-05-23 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Gas Required Odorized Ind No
Pipeline Function Transmission System
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Equipment failure
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Malfunction Of Control/relief Equipment
Eq Failure Type Malfunction Of Control/relief Equipment
Pressure Regulator Ind Yes
Eq Additional Other Ind Yes
Eq Additional Other Details Icing
Nf Temperature Ind Yes
Eqf Control Releaf Ind Yes
Preparer Name J**** C****
Preparer Title Sr. Manager Regulatory Compliance
Preparer Email J**********@e*************
Preparer Telephone 4055768230
Local Contact Name J**** C****
Local Contact Email J**********@e*************.com
Local Contact Telephone 4055768230
Authorizer Name J**** C****
Authorizer Title Lead Specialist
Authorizer Telephone 4055768230
Authorizer Email J**********@e*************.com
Narrative On 01/21/2022 a relief valve was discovered venting when a energy transfer employee arrived at the northeast power station in oologah, oklahoma. Gauges were installed to verify pressures. The relief valve was immediately closed and upon investigation it was determined that a reportable release of natural gas had occurred. The nrc was notified (nrc# 1327084, 1327011) and an investigation was initiated to determine cause. It was determined that regulator malfunction had occurred due to ice buildup on the regulator. The regulator was de-iced and the relief valve was rebuilt before being placed back into service. Extreme temperatures of 16 degrees occured on ths day and contributed to icing of the regulator, and ultimately caused the release.

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