GD incident on 2021-12-08 — MI

Operator
Consumers Energy Co
Cause
Excavation Issue
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$575
Incident datetime
2021-12-08 16:43
Report number
Location
MI, OAKLAND
Narrative
On wednesday, december 8, 2021 at approximately 16:43 hours, consumers energy received notification of a natural gas pipeline excavation damage from the contractor performing (boring) work in the 300 block of eleven mile road, royal oak, (oakland county) michigan. A gas service worker (gsw) was dispatched and arrived onsite at approximately 17:08 hours and confirmed a damaged and blowing 4-inch natural gas pipeline at 315 eleven mile road. Distribution employees were dispatched at 17:02 hours and arrived onsite at approximately 18:34 hours. The distribution crew excavated at remote locations and applied squeezers to contain the blowing gas. The damaged pipeline segment was cut out and replaced with approximately 6-foot of 4-inch medium-pressure plastic pipe and normal operations resumed on thursday, december 9, 2021 at approximately 14:00 hours. Three commercial customers experienced a loss of service as a result of the damage and subsequent repair. Consumers energy service employees remained onsite and continuously monitored the location until the gas was contained and the pipeline segment was repaired. No fatalities or injuries occurred as a result of the damage.
Detailed record list
Occurred At
2021-12-08 16:43:00
Year
2021
Report Received Date
2022-01-07 00:00:00
Iyear
2021.0
Report Number
20220003.0
Supplemental Number
36421.0
Report Type
Supplemental Final
Operator Id
Name
Consumers Energy Co
Operator Street Address
One Energy Plaza
Operator City Name
Jackson
Operator State Abbreviation
MI
Operator Postal Code
49201
Local Datetime
2021-12-08 16:43:00
Time Zone
Eastern
Daylight Savings Ind
Yes
Location Street Address
E. 11 Mile Road
Location City Name
Royal Oak
Location County Name
Oakland
Location State Abbreviation
MI
Location Postal Code
48067
Location Latitude
Location Longitude
Flow Cont Squeeze Off Ind
Yes
Nrc Rpt Datetime
2021-12-08 23:49:00
Nrc Rpt Num
Additional Nrc Report Numbers
1324232
Commodity Released Type
Natural Gas
Unintentional Release
3421.0
Intentional Release
0.0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
No
Num Pub Evacuated
0.0
Incident Identified Datetime
2021-12-08 16:43:00
Communication State Fed Ind
No
On Site Datetime
2021-12-08 17:08:00
Federal
No
Location Type
Utility Right-Of-Way / Easement
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
48.0
Other Underground Facilities
No
Crossing
No
Pipe Facility Type
Investor Owned
System Part Involved
Main
Installation Year
2016.0
Pipe Diameter
4.0
Pipe Specification
D2513
Pipe Manufacturer
Performance Pipe
Material Involved
Plastic
Plastic Type
Polyethylene (Pe)
Plastic Sdr
11
Material Pe Pipe Code
2708
Release Type
Mechanical Puncture
Puncture Axial
3.0
Puncture Circum
9.0
Class Location Type
Class 3 Location
Est Cost Oper Paid
0.0
Est Cost Prop Damage
575.0
Est Cost Emergency
15392.0
Est Cost Other
0.0
Gas Cost In Mcf
4.18
Est Cost Unintentional Release
14300.0
Est Cost Intentional Release
0.0
Prpty
30267.0
Commercial Affected
3.0
Industrial Affected
0.0
Residences Affected
0.0
Num Persons Hosp Not Ovnght
0.0
Num Injured Treated By Emt
0.0
Num Resident Building Affctd
0.0
Num Business Building Affctd
3.0
Accident Psig
55.0
Normal Psig
55.0
Mop Psig
60.0
Mop Cfr Section
192.619(A)(2)
Maop Established Date
2016-07-28 00:00:00
Accident Pressure
Pressure Did Not Exceed Maop
Gas Odorized System Type
Injection Pump
Gas Odorized Lvl Not Msrd Ind
Yes
Scada In Place Ind
No
Accident Identifier
Notification From Third Party That Caused The Incident
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
Yes
One Call System Ind
Yes
State Law Exempt Ind
No
Notify Cga Dirt
Yes
Public Row Ind
Yes
Public Subtype
City Street
Excavator Type
Contractor
Excavator Equipment
Boring
Work Performed
Water
One Call Notified Ind
Yes
One Call Ticket Num
B013270027
Locator Type
Contract Locator
Visible Marks
Yes
Service Interruption
No
Root Cause Category
Excavation Issue
Root Cause Type
Excavator Failed To Maintain Clearance After Verifying Marks
Preparer Name
C******* K***
Preparer Title
Senior Engineering Technical Analyst Ii
Preparer Email
C************@c********.com
Preparer Telephone
989-280-2963
Local Contact Name
C******* K***
Local Contact Email
C************@c********.com
Local Contact Telephone
989-280-2963
Authorizer Name
J**** P****
Authorizer Title
Gas Compliance Manager
Authorizer Telephone
989-791-5749
Authorizer Email
J**********@c********.com
Narrative
On wednesday, december 8, 2021 at approximately 16:43 hours, consumers energy received notification of a natural gas pipeline excavation damage from the contractor performing (boring) work in the 300 block of eleven mile road, royal oak, (oakland county) michigan. A gas service worker (gsw) was dispatched and arrived onsite at approximately 17:08 hours and confirmed a damaged and blowing 4-inch natural gas pipeline at 315 eleven mile road. Distribution employees were dispatched at 17:02 hours and arrived onsite at approximately 18:34 hours. The distribution crew excavated at remote locations and applied squeezers to contain the blowing gas. The damaged pipeline segment was cut out and replaced with approximately 6-foot of 4-inch medium-pressure plastic pipe and normal operations resumed on thursday, december 9, 2021 at approximately 14:00 hours. Three commercial customers experienced a loss of service as a result of the damage and subsequent repair. Consumers energy service employees remained onsite and continuously monitored the location until the gas was contained and the pipeline segment was repaired. No fatalities or injuries occurred as a result of the damage.
Occurred At 2021-12-08 16:43:00
Year 2021
Report Received Date 2022-01-07 00:00:00
Iyear 2021.0
Report Number 20220003.0
Supplemental Number 36421.0
Report Type Supplemental Final
Operator Id 2748 PHMSA Enforcement
Name Consumers Energy Co
Operator Street Address One Energy Plaza
Operator City Name Jackson
Operator State Abbreviation MI
Operator Postal Code 49201
Local Datetime 2021-12-08 16:43:00
Time Zone Eastern
Daylight Savings Ind Yes
Location Street Address E. 11 Mile Road
Location City Name Royal Oak
Location County Name Oakland
Location State Abbreviation MI
Location Postal Code 48067
Location Latitude 42.48993 Google Maps OpenStreetMap
Location Longitude -83.14136 Google Maps OpenStreetMap
Flow Cont Squeeze Off Ind Yes
Nrc Rpt Datetime 2021-12-08 23:49:00
Nrc Rpt Num 1324037 NRC Report How to search
Additional Nrc Report Numbers 1324232
Commodity Released Type Natural Gas
Unintentional Release 3421.0
Intentional Release 0.0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind No
Num Pub Evacuated 0.0
Incident Identified Datetime 2021-12-08 16:43:00
Communication State Fed Ind No
On Site Datetime 2021-12-08 17:08:00
Federal No
Location Type Utility Right-Of-Way / Easement
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 48.0
Other Underground Facilities No
Crossing No
Pipe Facility Type Investor Owned
System Part Involved Main
Installation Year 2016.0
Pipe Diameter 4.0
Pipe Specification D2513
Pipe Manufacturer Performance Pipe
Material Involved Plastic
Plastic Type Polyethylene (Pe)
Plastic Sdr 11
Material Pe Pipe Code 2708
Release Type Mechanical Puncture
Puncture Axial 3.0
Puncture Circum 9.0
Class Location Type Class 3 Location
Est Cost Oper Paid 0.0
Est Cost Prop Damage 575.0
Est Cost Emergency 15392.0
Est Cost Other 0.0
Gas Cost In Mcf 4.18
Est Cost Unintentional Release 14300.0
Est Cost Intentional Release 0.0
Prpty 30267.0
Commercial Affected 3.0
Industrial Affected 0.0
Residences Affected 0.0
Num Persons Hosp Not Ovnght 0.0
Num Injured Treated By Emt 0.0
Num Resident Building Affctd 0.0
Num Business Building Affctd 3.0
Accident Psig 55.0
Normal Psig 55.0
Mop Psig 60.0
Mop Cfr Section 192.619(A)(2) View CFR 49 §192
Maop Established Date 2016-07-28 00:00:00
Accident Pressure Pressure Did Not Exceed Maop
Gas Odorized System Type Injection Pump
Gas Odorized Lvl Not Msrd Ind Yes
Scada In Place Ind No
Accident Identifier Notification From Third Party That Caused The Incident
Investigation Status No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Excavation Damage
Cause Details Excavation Damage By Third Party
Ex Party Type Excavation Damage By Third Party
Prior Notification Ind Yes
One Call System Ind Yes
State Law Exempt Ind No
Notify Cga Dirt Yes
Public Row Ind Yes
Public Subtype City Street
Excavator Type Contractor
Excavator Equipment Boring
Work Performed Water
One Call Notified Ind Yes
One Call Ticket Num B013270027
Locator Type Contract Locator
Visible Marks Yes
Service Interruption No
Root Cause Category Excavation Issue
Root Cause Type Excavator Failed To Maintain Clearance After Verifying Marks
Preparer Name C******* K***
Preparer Title Senior Engineering Technical Analyst Ii
Preparer Email C************@c********.com
Preparer Telephone 989-280-2963
Local Contact Name C******* K***
Local Contact Email C************@c********.com
Local Contact Telephone 989-280-2963
Authorizer Name J**** P****
Authorizer Title Gas Compliance Manager
Authorizer Telephone 989-791-5749
Authorizer Email J**********@c********.com
Narrative On wednesday, december 8, 2021 at approximately 16:43 hours, consumers energy received notification of a natural gas pipeline excavation damage from the contractor performing (boring) work in the 300 block of eleven mile road, royal oak, (oakland county) michigan. A gas service worker (gsw) was dispatched and arrived onsite at approximately 17:08 hours and confirmed a damaged and blowing 4-inch natural gas pipeline at 315 eleven mile road. Distribution employees were dispatched at 17:02 hours and arrived onsite at approximately 18:34 hours. The distribution crew excavated at remote locations and applied squeezers to contain the blowing gas. The damaged pipeline segment was cut out and replaced with approximately 6-foot of 4-inch medium-pressure plastic pipe and normal operations resumed on thursday, december 9, 2021 at approximately 14:00 hours. Three commercial customers experienced a loss of service as a result of the damage and subsequent repair. Consumers energy service employees remained onsite and continuously monitored the location until the gas was contained and the pipeline segment was repaired. No fatalities or injuries occurred as a result of the damage.

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