HL incident on 2021-12-01 — TX

Operator
Alon Usa, Lp
Cause
Corrosion Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$5,000
Incident datetime
2021-12-01 12:30
Report number
Location
TX
Narrative
The pipeline was in the process of being permanently decommissioned. As part of the decommissioning plan, nitrogen was re-introduced. The pipeline had been represented as filled with nitrogen when acquired from the previous operator. A nitrogen pressure drop was detected on the line, and the decommissioning activities were stopped. Ground patrols were commenced to walk the line from the pig's last known location. Further investigation revealed a release of aged gasoline material initially in the general area of eastland, tx. Agency notifications were made and spill response activities were commenced at the site. Cause of failure was determined to be external corrosion due to exposure to brackish water containing CO2. Additional evidence of potential interference from buried metallic pipe was identified during excavation of the site.
Detailed record list
Report Received Date
2021-12-30 00:00:00
Iyear
2021
Report Number
20210355
Supplemental Number
36977
Report Type
Supplemental Final
Operator Id
Name
Alon Usa, Lp
Operator Street Address
200 Refinery Rd
Operator City Name
Big Spring
Operator State Abbreviation
TX
Operator Postal Code
79721
Local Datetime
2021-12-01 12:30:00
Time Zone
Central
Daylight Savings Ind
No
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
100
Recovered Bbls
45
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Ground Patrol By Operator Or Its Contractor
Operator Type
Operator Employee
Incident Identified Datetime
2021-12-01 12:30:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Status When Identified
Idle
Communication State Fed Ind
Yes
Party Initiated Communication
Operator
Initial Responder Com Datetime
2021-12-01 12:51:00
On Site Datetime
2021-12-01 16:30:00
Confirmed Discovery Datetime
2021-12-01 12:30:00
Nrc Rpt Datetime
2021-12-01 12:51:00
Nrc Rpt Num
Ignite Ind
No
Upstream Action Taken
Operational Control
Upstream Oprtnl Cntrl Detail
Operator Had Ceased Purge Prior To Discovery.
Downstream Action Taken
Operational Control
Downstream Oprtnl Cntrl Detail
Line Was Predominantly Empty. Downstream Valve Was Left Open To Allow For Gravity Drain.
Notify Qualified Indiv Ind
No
Oil Spill Removal Org Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Dfw Pipeline
Segment Name
Abilene To Mingus
Onshore State Abbreviation
Tx
Onshore Postal Code
76448
Onshore County Name
Eastland
Designated Location
Milepost
Designated Name
Mp 60
Federal
No
Location Type
Originated On Operator-Controlled Property, But Then Flowed Or Migrated Off The Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
24
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Body
Puddle Weld Ind
No
Pipe Diameter
6
Pipe Wall Thickness
0.188
Pipe Smys
42000
Pipe Specification
5l
Pipe Seam Type
Erw - High Frequency
Pipe Manufacturer
Unknown
Pipe Coating Type
Asphalt
Coating Applied Ind
No
Installation Year
1984
Manufactured Year
1984
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Other
Leak Type Other
3"x3" Corrosion Hole
Wildlife Impact Ind
Yes
Fish Aquatic Impact Ind
Yes
Terrestrial Impact Ind
Yes
Soil Contamination
Yes
Long Term Assessment
Yes
Remediation Ind
Yes
Surface Water Remed Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
Yes
Surface Contam Ind
Yes
Amount Released
70
Rel Water Name
Colony Creek. Not Flowing At Time Of Release, Standing Pools Of Water Only.
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
5000
Est Cost Emergency
1400000
Est Cost Environmental
150000
Est Cost Other
0
Prpty
1555000
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
291
Mop Psig
1440
Mop Cfr Section
Component Design Pressure �195.406(A)(2)
Maop Established Date
1982-01-01 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
Yes
Exceed Restriction Ind
No
Phmsa Restriction Ind
Not Mandated
Internal Inspection Ind
Yes
Operation Complications Ind
Yes
Low Flow Ind
Yes
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
External Corrosion
Internal External
External Corrosion
Visual Exam Results
Localized Pitting
Other Corrosion Ind
Yes
Corrosion Type Details
External Corrosion From Exposure To Brackish Water (Water Containing Some Salt) Containing Carbon Dioxide.
Metallurgical Basis Ind
Yes
Underground Location
Yes
Under Cathodic Protection Ind
Yes
Cathodic Pro Start Year
1982
Shielding Evident
Yes
Cathodic Survey Type
No
Prior Damage
Yes
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Extrnl Cor Stray Current Ind
Yes
Preparer Name
M****** S******
Preparer Title
Director Row Management And Reg Compliance
Preparer Email
M**************@d*************.com
Preparer Telephone
6306498016
Prepared Date
2022-08-14 00:00:00
Local Contact Name
M****** S******
Local Contact Email
Director Row Management And Reg Compliance
Local Contact Telephone
6306498016
Authorizer Name
M****** S******
Authorizer Telephone
6306498016
Authorizer Title
Director Row Management And Reg Compliance
Authorizer Email
M**************@d*************.com
Narrative
The pipeline was in the process of being permanently decommissioned. As part of the decommissioning plan, nitrogen was re-introduced. The pipeline had been represented as filled with nitrogen when acquired from the previous operator. A nitrogen pressure drop was detected on the line, and the decommissioning activities were stopped. Ground patrols were commenced to walk the line from the pig's last known location. Further investigation revealed a release of aged gasoline material initially in the general area of eastland, tx. Agency notifications were made and spill response activities were commenced at the site. Cause of failure was determined to be external corrosion due to exposure to brackish water containing CO2. Additional evidence of potential interference from buried metallic pipe was identified during excavation of the site.
Report Received Date 2021-12-30 00:00:00
Iyear 2021
Report Number 20210355
Supplemental Number 36977
Report Type Supplemental Final
Operator Id 31443 PHMSA Enforcement
Name Alon Usa, Lp
Operator Street Address 200 Refinery Rd
Operator City Name Big Spring
Operator State Abbreviation TX
Operator Postal Code 79721
Local Datetime 2021-12-01 12:30:00
Time Zone Central
Daylight Savings Ind No
Location Latitude 32.49814 Google Maps OpenStreetMap
Location Longitude -98.77996 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 100
Recovered Bbls 45
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Ground Patrol By Operator Or Its Contractor
Operator Type Operator Employee
Incident Identified Datetime 2021-12-01 12:30:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Status When Identified Idle
Communication State Fed Ind Yes
Party Initiated Communication Operator
Initial Responder Com Datetime 2021-12-01 12:51:00
On Site Datetime 2021-12-01 16:30:00
Confirmed Discovery Datetime 2021-12-01 12:30:00
Nrc Rpt Datetime 2021-12-01 12:51:00
Nrc Rpt Num 1323339 NRC Report How to search
Ignite Ind No
Upstream Action Taken Operational Control
Upstream Oprtnl Cntrl Detail Operator Had Ceased Purge Prior To Discovery.
Downstream Action Taken Operational Control
Downstream Oprtnl Cntrl Detail Line Was Predominantly Empty. Downstream Valve Was Left Open To Allow For Gravity Drain.
Notify Qualified Indiv Ind No
Oil Spill Removal Org Ind No
Num Pub Evacuated 0
Pipe Fac Name Dfw Pipeline
Segment Name Abilene To Mingus
Onshore State Abbreviation Tx
Onshore Postal Code 76448
Onshore County Name Eastland
Designated Location Milepost
Designated Name Mp 60
Federal No
Location Type Originated On Operator-Controlled Property, But Then Flowed Or Migrated Off The Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 24
Crossing No
Pipe Facility Type Intrastate
Item Involved Pipe
Pipe Type Pipe Body
Puddle Weld Ind No
Pipe Diameter 6
Pipe Wall Thickness 0.188
Pipe Smys 42000
Pipe Specification 5l
Pipe Seam Type Erw - High Frequency
Pipe Manufacturer Unknown
Pipe Coating Type Asphalt
Coating Applied Ind No
Installation Year 1984
Manufactured Year 1984
Material Involved Carbon Steel
Release Type Leak
Leak Type Other
Leak Type Other 3"x3" Corrosion Hole
Wildlife Impact Ind Yes
Fish Aquatic Impact Ind Yes
Terrestrial Impact Ind Yes
Soil Contamination Yes
Long Term Assessment Yes
Remediation Ind Yes
Surface Water Remed Ind Yes
Soil Remed Ind Yes
Water Contam Ind Yes
Surface Contam Ind Yes
Amount Released 70
Rel Water Name Colony Creek. Not Flowing At Time Of Release, Standing Pools Of Water Only.
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 5000
Est Cost Emergency 1400000
Est Cost Environmental 150000
Est Cost Other 0
Prpty 1555000
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 291
Mop Psig 1440
Mop Cfr Section Component Design Pressure �195.406(A)(2) View CFR 49 §192
Maop Established Date 1982-01-01 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind Yes
Exceed Restriction Ind No
Phmsa Restriction Ind Not Mandated
Internal Inspection Ind Yes
Operation Complications Ind Yes
Low Flow Ind Yes
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind No
Cpm In Place Ind No
Investigation Status No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details External Corrosion
Internal External External Corrosion
Visual Exam Results Localized Pitting
Other Corrosion Ind Yes
Corrosion Type Details External Corrosion From Exposure To Brackish Water (Water Containing Some Salt) Containing Carbon Dioxide.
Metallurgical Basis Ind Yes
Underground Location Yes
Under Cathodic Protection Ind Yes
Cathodic Pro Start Year 1982
Shielding Evident Yes
Cathodic Survey Type No
Prior Damage Yes
Collected Data Ind No
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Extrnl Cor Stray Current Ind Yes
Preparer Name M****** S******
Preparer Title Director Row Management And Reg Compliance
Preparer Email M**************@d*************.com
Preparer Telephone 6306498016
Prepared Date 2022-08-14 00:00:00
Local Contact Name M****** S******
Local Contact Email Director Row Management And Reg Compliance
Local Contact Telephone 6306498016
Authorizer Name M****** S******
Authorizer Telephone 6306498016
Authorizer Title Director Row Management And Reg Compliance
Authorizer Email M**************@d*************.com
Narrative The pipeline was in the process of being permanently decommissioned. As part of the decommissioning plan, nitrogen was re-introduced. The pipeline had been represented as filled with nitrogen when acquired from the previous operator. A nitrogen pressure drop was detected on the line, and the decommissioning activities were stopped. Ground patrols were commenced to walk the line from the pig's last known location. Further investigation revealed a release of aged gasoline material initially in the general area of eastland, tx. Agency notifications were made and spill response activities were commenced at the site. Cause of failure was determined to be external corrosion due to exposure to brackish water containing CO2. Additional evidence of potential interference from buried metallic pipe was identified during excavation of the site.

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