HL incident on 2021-11-07 — TX

Operator
Enterprise Crude Pipeline Llc
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$22,000
Incident datetime
2021-11-07 18:00
Report number
Location
TX
Narrative
On 11/7/2021 at 6:00 pm, operations discovered crude dripping from aboveground piping in the manifold 100 at houston ship channel. The manifold was already isolated at the time of discovery. Field examination determined that the leak occurred due to internal corrosion of the pipe. A plidco clamp was installed to repair the pipe. Enterprise notified trrc at 7:27 pm once the volume was estimated to exceed 5 gallons.
Detailed record list
Report Received Date
2021-12-03 00:00:00
Iyear
2021
Report Number
20210337
Supplemental Number
36073
Report Type
Original Final
Operator Id
Name
Enterprise Crude Pipeline Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2021-11-07 18:00:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
2
Recovered Bbls
2
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2021-11-07 18:00:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Already Isolated At The Time Of The Accident
On Site Datetime
2021-11-07 18:00:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Houston Ship Channel
Segment Name
Manifold 100
Onshore State Abbreviation
Tx
Onshore Postal Code
77015
Onshore City Name
Houston
Onshore County Name
Harris
Designated Location
Milepost/valve Station
Designated Name
Manifold 100
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
8
Pipe Wall Thickness
0.375
Pipe Smys
Unknown
Pipe Specification
Unknown
Pipe Seam Type
Seamless
Pipe Manufacturer
Unknown
Pipe Coating Type
Fusion Bonded Epoxy(Fbe)
Installation Year
1996
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
135
Est Cost Prop Damage
22000
Est Cost Emergency
25000
Est Cost Environmental
0
Est Cost Other
0
Prpty
47135
Accident Psig
5
Mop Psig
285
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Localized Pitting
Int Microbiological Ind
Yes
Int Field Exam Basis Ind
Yes
Int Low Point Pipe Loc Ind
Yes
Corrosion Inhibitors
No
Corrosion Lining
No
Cleaning Dewatering
Not Applicable - Not Mainline Pipe
Corrosion Coupons
Not Applicable - Not Mainline Pipe
Collected Data Ind
Yes
Ultrasonic Ind
Yes
Ultrasonic Recent Year
2021
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
Yes
Exm Other Type
Aut
Exm Other Rcnt Year
2021
Exm Other Rcnt Ind
Yes
Preparer Name
Y******* B**
Preparer Title
Pipeline Compliance Engineer
Preparer Email
Y***@e****.com
Preparer Telephone
713-381-5650
Prepared Date
2021-12-03 00:00:00
Authorizer Name
Y******* B**
Authorizer Telephone
713-381-5650
Authorizer Title
Pipeline Compliance Engineer
Authorizer Email
Y***@e****.com
Narrative
On 11/7/2021 at 6:00 pm, operations discovered crude dripping from aboveground piping in the manifold 100 at houston ship channel. The manifold was already isolated at the time of discovery. Field examination determined that the leak occurred due to internal corrosion of the pipe. A plidco clamp was installed to repair the pipe. Enterprise notified trrc at 7:27 pm once the volume was estimated to exceed 5 gallons.
Report Received Date 2021-12-03 00:00:00
Iyear 2021
Report Number 20210337
Supplemental Number 36073
Report Type Original Final
Operator Id 30829 PHMSA Enforcement
Name Enterprise Crude Pipeline Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2021-11-07 18:00:00
Location Latitude 29.748 Google Maps OpenStreetMap
Location Longitude -95.1295 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 2
Recovered Bbls 2
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2021-11-07 18:00:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Already Isolated At The Time Of The Accident
On Site Datetime 2021-11-07 18:00:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Houston Ship Channel
Segment Name Manifold 100
Onshore State Abbreviation Tx
Onshore Postal Code 77015
Onshore City Name Houston
Onshore County Name Harris
Designated Location Milepost/valve Station
Designated Name Manifold 100
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 8
Pipe Wall Thickness 0.375
Pipe Smys Unknown
Pipe Specification Unknown
Pipe Seam Type Seamless
Pipe Manufacturer Unknown
Pipe Coating Type Fusion Bonded Epoxy(Fbe)
Installation Year 1996
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 135
Est Cost Prop Damage 22000
Est Cost Emergency 25000
Est Cost Environmental 0
Est Cost Other 0
Prpty 47135
Accident Psig 5
Mop Psig 285
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind No
Cpm In Place Ind No
Investigation Status No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results Localized Pitting
Int Microbiological Ind Yes
Int Field Exam Basis Ind Yes
Int Low Point Pipe Loc Ind Yes
Corrosion Inhibitors No
Corrosion Lining No
Cleaning Dewatering Not Applicable - Not Mainline Pipe
Corrosion Coupons Not Applicable - Not Mainline Pipe
Collected Data Ind Yes
Ultrasonic Ind Yes
Ultrasonic Recent Year 2021
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind Yes
Exm Other Type Aut
Exm Other Rcnt Year 2021
Exm Other Rcnt Ind Yes
Preparer Name Y******* B**
Preparer Title Pipeline Compliance Engineer
Preparer Email Y***@e****.com
Preparer Telephone 713-381-5650
Prepared Date 2021-12-03 00:00:00
Authorizer Name Y******* B**
Authorizer Telephone 713-381-5650
Authorizer Title Pipeline Compliance Engineer
Authorizer Email Y***@e****.com
Narrative On 11/7/2021 at 6:00 pm, operations discovered crude dripping from aboveground piping in the manifold 100 at houston ship channel. The manifold was already isolated at the time of discovery. Field examination determined that the leak occurred due to internal corrosion of the pipe. A plidco clamp was installed to repair the pipe. Enterprise notified trrc at 7:27 pm once the volume was estimated to exceed 5 gallons.

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