HL incident on 2021-11-11 — OH

Operator
Marathon Pipe Line Llc
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$2,200
Incident datetime
2021-11-11 06:37
Report number
Location
OH
Narrative
Operator personnel identified a cracked multi-port valve associated with a thermal relief valve spraying diesel fuel. Pipeline was shut down, a new valve was installed, and pipeline restarted. Impacted gravel and soil was removed from the site. The cause of the failed multi-port valve is pending analytical results. Following the accident, additional support/bracing was added to prevent reoccurrence. On january 17, 2022, marathon pipe line received the evaluation report from the manufacturer stating the failure was caused by fatigue which can by caused by excessive movement or vibration from an external source. Parts a, b, c, d, e new questions were answered. Part g was updated.
Detailed record list
Report Received Date
2021-11-29 00:00:00
Iyear
2021
Report Number
20210333
Supplemental Number
36293
Report Type
Supplemental Final
Operator Id
Name
Marathon Pipe Line Llc
Operator Street Address
539 South Main Street
Operator City Name
Findlay
Operator State Abbreviation
OH
Operator Postal Code
45840
Local Datetime
2021-11-11 06:37:00
Time Zone
Eastern
Daylight Savings Ind
No
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
0.5
Recovered Bbls
0.5
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2021-11-11 06:37:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Communication State Fed Ind
No
On Site Datetime
2021-11-11 06:37:00
Confirmed Discovery Datetime
2021-11-11 07:25:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Notify Qualified Indiv Ind
No
Oil Spill Removal Org Ind
No
Num Pub Evacuated
0
Pipe Fac Name
East Sparta Tank Farm
Segment Name
Valve Associated With A Thermal Relief
Onshore State Abbreviation
Oh
Onshore Postal Code
44626
Onshore City Name
East Sparta
Onshore County Name
Stark
Designated Location
Milepost
Designated Name
Facility
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Installation Year
2017
Manufactured Year
2017
Material Involved
Material Other Than Carbon Steel
Material Details
Stainless Steel
Release Type
Leak
Leak Type
Crack
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Usa Ecological Ind
Yes
Usa Ecological Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
53
Est Cost Prop Damage
2200
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
2253
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
1830
Mop Psig
3204
Mop Cfr Section
Subpart E Pressure Test �195.406(A)(3)
Maop Established Date
2017-04-07 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind
Yes
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Failure Of Equipment Body (Except Pump), Tank Plate, Or Other Material
Eq Failure Type
Failure Of Equipment Body (Except Pump), Tank Plate, Or Other Material
Additional Vibration Ind
Yes
Preparer Name
K*** E******
Preparer Title
Health Environmental And Safety Professional
Preparer Email
K********@m****************.com
Preparer Telephone
14193063329
Prepared Date
2022-02-02 00:00:00
Local Contact Name
K*** E******
Local Contact Email
K********@m****************.com
Local Contact Telephone
14193063329
Authorizer Name
A**** W* M*******
Authorizer Telephone
210-626-6343
Authorizer Title
Regulatory Compliance Manager
Authorizer Email
A*********@m****************.com
Narrative
Operator personnel identified a cracked multi-port valve associated with a thermal relief valve spraying diesel fuel. Pipeline was shut down, a new valve was installed, and pipeline restarted. Impacted gravel and soil was removed from the site. The cause of the failed multi-port valve is pending analytical results. Following the accident, additional support/bracing was added to prevent reoccurrence. On january 17, 2022, marathon pipe line received the evaluation report from the manufacturer stating the failure was caused by fatigue which can by caused by excessive movement or vibration from an external source. Parts a, b, c, d, e new questions were answered. Part g was updated.
Report Received Date 2021-11-29 00:00:00
Iyear 2021
Report Number 20210333
Supplemental Number 36293
Report Type Supplemental Final
Operator Id 32147 PHMSA Enforcement
Name Marathon Pipe Line Llc
Operator Street Address 539 South Main Street
Operator City Name Findlay
Operator State Abbreviation OH
Operator Postal Code 45840
Local Datetime 2021-11-11 06:37:00
Time Zone Eastern
Daylight Savings Ind No
Location Latitude 40.676195 Google Maps OpenStreetMap
Location Longitude -81.347826 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls 0.5
Recovered Bbls 0.5
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2021-11-11 06:37:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Status When Identified Normal Operation, Includes Pauses Between Batches And During Maintenance
Communication State Fed Ind No
On Site Datetime 2021-11-11 06:37:00
Confirmed Discovery Datetime 2021-11-11 07:25:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Notify Qualified Indiv Ind No
Oil Spill Removal Org Ind No
Num Pub Evacuated 0
Pipe Fac Name East Sparta Tank Farm
Segment Name Valve Associated With A Thermal Relief
Onshore State Abbreviation Oh
Onshore Postal Code 44626
Onshore City Name East Sparta
Onshore County Name Stark
Designated Location Milepost
Designated Name Facility
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Installation Year 2017
Manufactured Year 2017
Material Involved Material Other Than Carbon Steel
Material Details Stainless Steel
Release Type Leak
Leak Type Crack
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Usa Drinking Ind Yes
Usa Drinking Yes No Yes
Usa Ecological Ind Yes
Usa Ecological Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 53
Est Cost Prop Damage 2200
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 2253
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 1830
Mop Psig 3204
Mop Cfr Section Subpart E Pressure Test �195.406(A)(3) View CFR 49 §192
Maop Established Date 2017-04-07 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind Yes
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Failure Of Equipment Body (Except Pump), Tank Plate, Or Other Material
Eq Failure Type Failure Of Equipment Body (Except Pump), Tank Plate, Or Other Material
Additional Vibration Ind Yes
Preparer Name K*** E******
Preparer Title Health Environmental And Safety Professional
Preparer Email K********@m****************.com
Preparer Telephone 14193063329
Prepared Date 2022-02-02 00:00:00
Local Contact Name K*** E******
Local Contact Email K********@m****************.com
Local Contact Telephone 14193063329
Authorizer Name A**** W* M*******
Authorizer Telephone 210-626-6343
Authorizer Title Regulatory Compliance Manager
Authorizer Email A*********@m****************.com
Narrative Operator personnel identified a cracked multi-port valve associated with a thermal relief valve spraying diesel fuel. Pipeline was shut down, a new valve was installed, and pipeline restarted. Impacted gravel and soil was removed from the site. The cause of the failed multi-port valve is pending analytical results. Following the accident, additional support/bracing was added to prevent reoccurrence. On january 17, 2022, marathon pipe line received the evaluation report from the manufacturer stating the failure was caused by fatigue which can by caused by excessive movement or vibration from an external source. Parts a, b, c, d, e new questions were answered. Part g was updated.

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