HL incident on 2021-11-01 — TX

Operator
West Texas Gulf Pipeline Co
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$1,000
Incident datetime
2021-11-01 11:03
Report number
Location
TX
Narrative
On 11/01/21 at approximately 11:03am while conducting a station check, a tech noticed a pool of crude oil on the ground along the tank 44 suction line. This line was idle at the time the release was found. Upon excavation of the line it was discovered that there was pin hole on the pipe at the 3 o'clock position. Approximately 2 barrels of crude had leaked into the surrounding soil. A clamp was installed to stop the leak. A crew was called to remove all free product and soil for remediation. Permanent repair of the line will occur when scheduling will allow some down time for this system.
Detailed record list
Report Received Date
2021-11-22 00:00:00
Iyear
2021
Report Number
20210331
Supplemental Number
36033
Report Type
Original Final
Operator Id
Name
West Texas Gulf Pipeline Co
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2021-11-01 11:03:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
2
Recovered Bbls
2
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2021-11-01 11:03:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Tank 44 Suction Line Was Idle At Time Of Release
On Site Datetime
2021-11-01 13:24:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Wortham Station
Segment Name
Tank 44 Suction Fill Line
Onshore State Abbreviation
Tx
Onshore Postal Code
77659
Onshore City Name
Wortham
Onshore County Name
Freestone
Designated Location
Milepost/valve Station
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
120
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
36
Pipe Wall Thickness
0.375
Pipe Smys
42000
Pipe Specification
Api 5l X-42
Pipe Seam Type
Erw - High Frequency
Pipe Manufacturer
Whitco
Pipe Coating Type
Fusion Bonded Epoxy(Fbe)
Installation Year
2018
Manufactured Year
2018
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
168
Est Cost Prop Damage
1000
Est Cost Emergency
34000
Est Cost Environmental
5000
Est Cost Other
0
Prpty
40168
Accident Psig
5
Mop Psig
285
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
A review of the accident determined that there were no control room actions that contributed to the event.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Not Cut Open
Int Water Acid Ind
Yes
Int Microbiological Ind
Yes
Int Field Exam Basis Ind
Yes
Int Low Point Pipe Loc Ind
Yes
Corrosion Inhibitors
Yes
Corrosion Lining
No
Cleaning Dewatering
Not Applicable - Not Mainline Pipe
Corrosion Coupons
Not Applicable - Not Mainline Pipe
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
2018
Hydrtst Most Rcnt Pressure
364
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
N****** P********
Preparer Title
Dot Compliance Specialist
Preparer Email
N****************@e*************.com
Preparer Telephone
713-989-4527
Prepared Date
2021-11-22 00:00:00
Authorizer Name
C**** K*****
Authorizer Telephone
9795319036
Authorizer Title
Manager - Regulatory Compliance
Authorizer Email
C***********@e*************.com
Narrative
On 11/01/21 at approximately 11:03am while conducting a station check, a tech noticed a pool of crude oil on the ground along the tank 44 suction line. This line was idle at the time the release was found. Upon excavation of the line it was discovered that there was pin hole on the pipe at the 3 o'clock position. Approximately 2 barrels of crude had leaked into the surrounding soil. A clamp was installed to stop the leak. A crew was called to remove all free product and soil for remediation. Permanent repair of the line will occur when scheduling will allow some down time for this system.
Report Received Date 2021-11-22 00:00:00
Iyear 2021
Report Number 20210331
Supplemental Number 36033
Report Type Original Final
Operator Id 22442 PHMSA Enforcement
Name West Texas Gulf Pipeline Co
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2021-11-01 11:03:00
Location Latitude 31.777937 Google Maps OpenStreetMap
Location Longitude -96.400398 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 2
Recovered Bbls 2
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2021-11-01 11:03:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Tank 44 Suction Line Was Idle At Time Of Release
On Site Datetime 2021-11-01 13:24:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Wortham Station
Segment Name Tank 44 Suction Fill Line
Onshore State Abbreviation Tx
Onshore Postal Code 77659
Onshore City Name Wortham
Onshore County Name Freestone
Designated Location Milepost/valve Station
Designated Name 0
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 120
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 36
Pipe Wall Thickness 0.375
Pipe Smys 42000
Pipe Specification Api 5l X-42
Pipe Seam Type Erw - High Frequency
Pipe Manufacturer Whitco
Pipe Coating Type Fusion Bonded Epoxy(Fbe)
Installation Year 2018
Manufactured Year 2018
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 168
Est Cost Prop Damage 1000
Est Cost Emergency 34000
Est Cost Environmental 5000
Est Cost Other 0
Prpty 40168
Accident Psig 5
Mop Psig 285
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details A review of the accident determined that there were no control room actions that contributed to the event.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results Not Cut Open
Int Water Acid Ind Yes
Int Microbiological Ind Yes
Int Field Exam Basis Ind Yes
Int Low Point Pipe Loc Ind Yes
Corrosion Inhibitors Yes
Corrosion Lining No
Cleaning Dewatering Not Applicable - Not Mainline Pipe
Corrosion Coupons Not Applicable - Not Mainline Pipe
Collected Data Ind No
Has Hydrtst Conduc Before Ind Yes
Hydrtst Most Rcnt Year 2018
Hydrtst Most Rcnt Pressure 364
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name N****** P********
Preparer Title Dot Compliance Specialist
Preparer Email N****************@e*************.com
Preparer Telephone 713-989-4527
Prepared Date 2021-11-22 00:00:00
Authorizer Name C**** K*****
Authorizer Telephone 9795319036
Authorizer Title Manager - Regulatory Compliance
Authorizer Email C***********@e*************.com
Narrative On 11/01/21 at approximately 11:03am while conducting a station check, a tech noticed a pool of crude oil on the ground along the tank 44 suction line. This line was idle at the time the release was found. Upon excavation of the line it was discovered that there was pin hole on the pipe at the 3 o'clock position. Approximately 2 barrels of crude had leaked into the surrounding soil. A clamp was installed to stop the leak. A crew was called to remove all free product and soil for remediation. Permanent repair of the line will occur when scheduling will allow some down time for this system.

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