HL incident on 2021-10-23 — TX

Operator
Dixie Pipeline Company Llc
Cause
Material Failure Of Pipe Or Weld
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$300,000
Incident datetime
2021-10-23 10:44
Report number
Location
TX
Narrative
On may 23, 2021 at 09:05, enterprise houston control center (hcc) received a call from a landowner in seale, alabama reporting ice on the ground with a smell. At 10:44 enterprise confirmed a leak at mp 23.625 on the pipeline right-of-way and immediately isolated the section of pipeline. Enterprise determined the event to be reportable at 11:20 and reported to the nrc at 11:59. The pipeline was pigged to remove product from the pipeline and purged with nitrogen. A 70 feet section of mainline pipe was cut and removed from service. A new section of mainline pipe was pressure tested, installed, purged and returned to service. A 19.27 feet of mainline pipe containing the leak location was examined by metallurgical analysis. The results of the metallurgical analysis indicated that the leak occurred at a colony of interlinked, intergranular cracks consistent with high ph stress corrosion cracking (scc) were located in the base metal, near the seam weld, at the 9:24 orientation. A likely contributing factor to the failure/cracking was residual stresses from the seam welding process based on the presence of the cracking adjacent to the seam weld. The PHMSA accident division was notified on 10/23/2021 at 12:00. The 48-hour update to the nrc took place on 10/25/2021 at 09:16 # 1320339.
Detailed record list
Report Received Date
2021-11-19 00:00:00
Iyear
2021
Report Number
20210328
Supplemental Number
36583
Report Type
Supplemental Final
Operator Id
Name
Dixie Pipeline Company Llc
Operator Street Address
1100 Louisiana St.
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2021-10-23 09:05:00
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Other Hvl
Commodity Details
Propane
Unintentional Release Bbls
15
Intentional Release Bbls
868
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Public
Incident Identified Datetime
2021-10-23 10:44:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2021-10-23 10:44:00
Restart Datetime
2021-11-01 10:25:00
Communication State Fed Ind
No
On Site Datetime
2021-10-23 10:44:00
Confirmed Discovery Datetime
2021-10-23 10:44:00
Nrc Rpt Datetime
2021-10-23 11:59:00
Nrc Rpt Num
Additional Nrc Report Numbers
1320339
Ignite Ind
No
Upstream Action Taken
Valve Closure
Upstream Valve Close Datetime
2021-10-23 10:44:00
Upstream Valve Type Ind
Remotely Controlled
Downstream Action Taken
Valve Closure
Downstream Vlv Close Datetime
2021-10-23 10:44:00
Downstream Valve Type Ind
Remotely Controlled
Num Pub Evacuated
0
Pipe Fac Name
Opelika - Alma (Spur Line)
Segment Name
Dixie/119
Onshore State Abbreviation
Al
Onshore Postal Code
36875
Onshore City Name
Seale
Onshore County Name
Russell
Designated Location
Milepost
Designated Name
23.64
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
48
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Puddle Weld Ind
No
Pipe Diameter
6.625
Pipe Wall Thickness
0.172
Pipe Smys
42000
Pipe Specification
Api-5l
Pipe Seam Type
Erw - High Frequency
Pipe Manufacturer
American Steel
Pipe Coating Type
Coal Tar
Coating Applied Ind
Unknown
Installation Year
1965
Manufactured Year
1965
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Crack
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
58500
Est Cost Prop Damage
300000
Est Cost Emergency
10000
Est Cost Environmental
0
Est Cost Other
0
Prpty
368500
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
425
Mop Psig
1358
Mop Cfr Section
Subpart E Pressure Test �195.406(A)(3)
Maop Established Date
2003-04-30 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
180365
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
This was a crack in the pipeline which caused the leak.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Material Failure Of Pipe Or Weld
Cause Details
Environmental Cracking-Related
Metallurgical Ind
Yes
Failure Type
Environmental Cracking-Related
Stress Subtype
Stress Corrosion Cracking
Additional Crack Ind
Yes
Collected Data Ind
Yes
Axial Magnetic Flx Lkg Ind
Yes
Axial Recent Year
2020
Axial Rcnt Propul Method
Free Swimming
Axial Rcnt Attuned Detect
Metal Loss
Axial Rcnt Atnd Dtct Metal
Standard Resolution
Axial Previous Year
2015
Axial Prev Propul Method
Free Swimming
Axial Prev Attuned Detect
Metal Loss
Axial Prev Atnd Dtct Metal
Standard Resolution
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
2003
Hydrtst Most Rcnt Pressure
1912
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
N***** L* G*** J**
Preparer Title
Senior Pipeline Compliance Specialist
Preparer Email
N****@e****.com
Preparer Telephone
985-493-4629
Prepared Date
2022-04-14 00:00:00
Local Contact Name
N***** L* G*** J**
Local Contact Email
N****@e****.com
Local Contact Telephone
985-493-4629
Authorizer Name
N*** T*****
Authorizer Telephone
713-381-2493
Authorizer Title
Senior Compliance Manager
Authorizer Email
N*******@e****.com
Narrative
On may 23, 2021 at 09:05, enterprise houston control center (hcc) received a call from a landowner in seale, alabama reporting ice on the ground with a smell. At 10:44 enterprise confirmed a leak at mp 23.625 on the pipeline right-of-way and immediately isolated the section of pipeline. Enterprise determined the event to be reportable at 11:20 and reported to the nrc at 11:59. The pipeline was pigged to remove product from the pipeline and purged with nitrogen. A 70 feet section of mainline pipe was cut and removed from service. A new section of mainline pipe was pressure tested, installed, purged and returned to service. A 19.27 feet of mainline pipe containing the leak location was examined by metallurgical analysis. The results of the metallurgical analysis indicated that the leak occurred at a colony of interlinked, intergranular cracks consistent with high ph stress corrosion cracking (scc) were located in the base metal, near the seam weld, at the 9:24 orientation. A likely contributing factor to the failure/cracking was residual stresses from the seam welding process based on the presence of the cracking adjacent to the seam weld. The PHMSA accident division was notified on 10/23/2021 at 12:00. The 48-hour update to the nrc took place on 10/25/2021 at 09:16 # 1320339.
Report Received Date 2021-11-19 00:00:00
Iyear 2021
Report Number 20210328
Supplemental Number 36583
Report Type Supplemental Final
Operator Id 3445 PHMSA Enforcement
Name Dixie Pipeline Company Llc
Operator Street Address 1100 Louisiana St.
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2021-10-23 09:05:00
Time Zone Central
Daylight Savings Ind Yes
Location Latitude 32.340554 Google Maps OpenStreetMap
Location Longitude -85.092995 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Other Hvl
Commodity Details Propane
Unintentional Release Bbls 15
Intentional Release Bbls 868
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Notification From Public
Incident Identified Datetime 2021-10-23 10:44:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Status When Identified Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind Yes
Shutdown Datetime 2021-10-23 10:44:00
Restart Datetime 2021-11-01 10:25:00
Communication State Fed Ind No
On Site Datetime 2021-10-23 10:44:00
Confirmed Discovery Datetime 2021-10-23 10:44:00
Nrc Rpt Datetime 2021-10-23 11:59:00
Nrc Rpt Num 1320220 NRC Report How to search
Additional Nrc Report Numbers 1320339
Ignite Ind No
Upstream Action Taken Valve Closure
Upstream Valve Close Datetime 2021-10-23 10:44:00
Upstream Valve Type Ind Remotely Controlled
Downstream Action Taken Valve Closure
Downstream Vlv Close Datetime 2021-10-23 10:44:00
Downstream Valve Type Ind Remotely Controlled
Num Pub Evacuated 0
Pipe Fac Name Opelika - Alma (Spur Line)
Segment Name Dixie/119
Onshore State Abbreviation Al
Onshore Postal Code 36875
Onshore City Name Seale
Onshore County Name Russell
Designated Location Milepost
Designated Name 23.64
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 48
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Puddle Weld Ind No
Pipe Diameter 6.625
Pipe Wall Thickness 0.172
Pipe Smys 42000
Pipe Specification Api-5l
Pipe Seam Type Erw - High Frequency
Pipe Manufacturer American Steel
Pipe Coating Type Coal Tar
Coating Applied Ind Unknown
Installation Year 1965
Manufactured Year 1965
Material Involved Carbon Steel
Release Type Leak
Leak Type Crack
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 58500
Est Cost Prop Damage 300000
Est Cost Emergency 10000
Est Cost Environmental 0
Est Cost Other 0
Prpty 368500
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 425
Mop Psig 1358
Mop Cfr Section Subpart E Pressure Test �195.406(A)(3) View CFR 49 §192
Maop Established Date 2003-04-30 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 180365
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details This was a crack in the pipeline which caused the leak.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Material Failure Of Pipe Or Weld
Cause Details Environmental Cracking-Related
Metallurgical Ind Yes
Failure Type Environmental Cracking-Related
Stress Subtype Stress Corrosion Cracking
Additional Crack Ind Yes
Collected Data Ind Yes
Axial Magnetic Flx Lkg Ind Yes
Axial Recent Year 2020
Axial Rcnt Propul Method Free Swimming
Axial Rcnt Attuned Detect Metal Loss
Axial Rcnt Atnd Dtct Metal Standard Resolution
Axial Previous Year 2015
Axial Prev Propul Method Free Swimming
Axial Prev Attuned Detect Metal Loss
Axial Prev Atnd Dtct Metal Standard Resolution
Has Hydrtst Conduc Before Ind Yes
Hydrtst Most Rcnt Year 2003
Hydrtst Most Rcnt Pressure 1912
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name N***** L* G*** J**
Preparer Title Senior Pipeline Compliance Specialist
Preparer Email N****@e****.com
Preparer Telephone 985-493-4629
Prepared Date 2022-04-14 00:00:00
Local Contact Name N***** L* G*** J**
Local Contact Email N****@e****.com
Local Contact Telephone 985-493-4629
Authorizer Name N*** T*****
Authorizer Telephone 713-381-2493
Authorizer Title Senior Compliance Manager
Authorizer Email N*******@e****.com
Narrative On may 23, 2021 at 09:05, enterprise houston control center (hcc) received a call from a landowner in seale, alabama reporting ice on the ground with a smell. At 10:44 enterprise confirmed a leak at mp 23.625 on the pipeline right-of-way and immediately isolated the section of pipeline. Enterprise determined the event to be reportable at 11:20 and reported to the nrc at 11:59. The pipeline was pigged to remove product from the pipeline and purged with nitrogen. A 70 feet section of mainline pipe was cut and removed from service. A new section of mainline pipe was pressure tested, installed, purged and returned to service. A 19.27 feet of mainline pipe containing the leak location was examined by metallurgical analysis. The results of the metallurgical analysis indicated that the leak occurred at a colony of interlinked, intergranular cracks consistent with high ph stress corrosion cracking (scc) were located in the base metal, near the seam weld, at the 9:24 orientation. A likely contributing factor to the failure/cracking was residual stresses from the seam welding process based on the presence of the cracking adjacent to the seam weld. The PHMSA accident division was notified on 10/23/2021 at 12:00. The 48-hour update to the nrc took place on 10/25/2021 at 09:16 # 1320339.

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