HL incident on 2021-10-21 — OK

Operator
Magellan Pipeline Company, Lp
Cause
Incorrect Operation
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2021-10-21 14:15
Report number
Location
OK
Narrative
At 14:15 on october 21, 2021, magellan operations personnel were conducting a daily facility inspection when product was discovered at a low point drain near the receive manifold. Upon further investigation, it was discovered that a build-up of old tape and pipe dope kept the plug from fully sealing which allowed product to leak by. A new, clean plug was installed and cleanup activities were initiated. Modifications are being made to the winterization procedure to specify that a new or clean plug should be installed following winterization activities. Supplemental/final (12-01-2021): part g
Detailed record list
Report Received Date
2021-11-19 00:00:00
Iyear
2021
Report Number
20210327
Supplemental Number
36062
Report Type
Supplemental Final
Operator Id
Name
Magellan Pipeline Company, Lp
Operator Street Address
100 West 5th Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2021-10-21 14:15:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
2.4
Recovered Bbls
2.4
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2021-10-21 14:15:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
The Facility Was Bypassed And Isolated From Mainline Operations.
On Site Datetime
2021-10-21 14:15:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Willmar Station
Segment Name
Fac Id 780
Onshore State Abbreviation
Mn
Onshore Postal Code
56201
Onshore City Name
Willmar
Onshore County Name
Kandiyohi
Designated Location
Milepost/valve Station
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Auxiliary Piping (E.g. Drain Lines)
Installation Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
230
Est Cost Prop Damage
0
Est Cost Emergency
25000
Est Cost Environmental
0
Est Cost Other
0
Prpty
25230
Accident Psig
400
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The low point drain leak was isolated within the facility and did not impact operations for ops control.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Equipment Not Installed Properly
Operation Type
Equipment Not Installed Properly
Related Inadequate Proc Ind
Yes
Category Type
Routine Maintenance
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
S****** L******
Preparer Title
Ai Analyst
Preparer Email
S**************@m*********.com
Preparer Telephone
918-574-7327
Preparer Fax
918-574-7376
Prepared Date
2021-12-01 00:00:00
Authorizer Name
G**** R****
Authorizer Telephone
918-574-7165
Authorizer Title
Supervisor Integrity Management
Authorizer Email
G**********@m*********.com
Narrative
At 14:15 on october 21, 2021, magellan operations personnel were conducting a daily facility inspection when product was discovered at a low point drain near the receive manifold. Upon further investigation, it was discovered that a build-up of old tape and pipe dope kept the plug from fully sealing which allowed product to leak by. A new, clean plug was installed and cleanup activities were initiated. Modifications are being made to the winterization procedure to specify that a new or clean plug should be installed following winterization activities. Supplemental/final (12-01-2021): part g
Report Received Date 2021-11-19 00:00:00
Iyear 2021
Report Number 20210327
Supplemental Number 36062
Report Type Supplemental Final
Operator Id 22610 PHMSA Enforcement
Name Magellan Pipeline Company, Lp
Operator Street Address 100 West 5th Street
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74103
Local Datetime 2021-10-21 14:15:00
Location Latitude 45.104828 Google Maps OpenStreetMap
Location Longitude -95.081786 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls 2.4
Recovered Bbls 2.4
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2021-10-21 14:15:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain The Facility Was Bypassed And Isolated From Mainline Operations.
On Site Datetime 2021-10-21 14:15:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Willmar Station
Segment Name Fac Id 780
Onshore State Abbreviation Mn
Onshore Postal Code 56201
Onshore City Name Willmar
Onshore County Name Kandiyohi
Designated Location Milepost/valve Station
Designated Name 0
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Auxiliary Piping (E.g. Drain Lines)
Installation Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Connection Failure
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Usa Drinking Ind Yes
Usa Drinking Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 230
Est Cost Prop Damage 0
Est Cost Emergency 25000
Est Cost Environmental 0
Est Cost Other 0
Prpty 25230
Accident Psig 400
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The low point drain leak was isolated within the facility and did not impact operations for ops control.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Equipment Not Installed Properly
Operation Type Equipment Not Installed Properly
Related Inadequate Proc Ind Yes
Category Type Routine Maintenance
Operator Qualification Ind Yes
Qualified Individuals Yes, They Were Qualified For The Task(S)
Preparer Name S****** L******
Preparer Title Ai Analyst
Preparer Email S**************@m*********.com
Preparer Telephone 918-574-7327
Preparer Fax 918-574-7376
Prepared Date 2021-12-01 00:00:00
Authorizer Name G**** R****
Authorizer Telephone 918-574-7165
Authorizer Title Supervisor Integrity Management
Authorizer Email G**********@m*********.com
Narrative At 14:15 on october 21, 2021, magellan operations personnel were conducting a daily facility inspection when product was discovered at a low point drain near the receive manifold. Upon further investigation, it was discovered that a build-up of old tape and pipe dope kept the plug from fully sealing which allowed product to leak by. A new, clean plug was installed and cleanup activities were initiated. Modifications are being made to the winterization procedure to specify that a new or clean plug should be installed following winterization activities. Supplemental/final (12-01-2021): part g

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