Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2021-10-23 — OK
Operator
Magellan Terminals Holdings, Lp
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$22,000
Incident datetime
2021-10-23 08:25
Report number
Location
OK
Narrative
At 08:25 on october 23, 2021, magellan operations personnel were conducting a daily facility inspection when the tank 422 mixer was found leaking from the tattletale. Product was transferred from the tank and cleanup activities were initiated. Upon further investigation it was determined that the inner bearing failed which allowed the seal on the tank mixer to wear and eventually fail. To prevent recurrence, the gear box and seal were replaced. The tank was then placed back into service. Supplemental/final (03-16-2022) part h narrative
Detailed record list
Report Received Date
2021-11-18 00:00:00
Iyear
2021
Report Number
20210324
Supplemental Number
36478
Report Type
Supplemental Final
Operator Id
31580
Name
Magellan Terminals Holdings, Lp
Operator Street Address
100 West 5th Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2021-10-23 08:25:00
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
29.751489
Location Longitude
-95.203937
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Mixture Of Refined Products (Transmix Or Other Mixture)
Unintentional Release Bbls
3
Recovered Bbls
3
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2021-10-23 08:25:00
System Part Involved
Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore
Onshore
Status When Identified
Idle
Communication State Fed Ind
No
On Site Datetime
2021-10-23 08:25:00
Confirmed Discovery Datetime
2021-10-23 08:25:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Notify Qualified Indiv Ind
Yes
Qualified Indiv Notif Datetime
2021-10-23 08:25:00
Oil Spill Removal Org Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Galena Park Terminal
Segment Name
Fac Id 474
Onshore State Abbreviation
Tx
Onshore Postal Code
77547
Onshore City Name
Galena Park
Onshore County Name
Harris
Designated Location
Milepost
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Tank, Including Attached Appurtenances
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Tank/vessel
Tank Vessel Subtype
Mixer
Tank Type
Atmospheric
Safe Fill Level
55.5
Safe Fill Level Exceeded Ind
No
Api Std Out Of Service Year
2021
Api Std In Service Year
2021
Installation Year
2012
Manufactured Year
2012
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
2058
Est Cost Prop Damage
22000
Est Cost Emergency
6451
Est Cost Environmental
0
Est Cost Other
0
Prpty
30509
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
12.1
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
Seal (Not Pump Seal) Or Packing
Eq Additional Other Ind
Yes
Eq Additional Other Details
Normal Wear
Preparer Name
S****** L******
Preparer Title
Ai Analyst
Preparer Email
S**************@m*********.com
Preparer Telephone
918-574-7327
Preparer Fax
918-574-7376
Prepared Date
2022-03-21 00:00:00
Authorizer Name
G**** R****
Authorizer Telephone
918-574-7165
Authorizer Title
Supervisor Integrity Management
Authorizer Email
G**********@m*********.com
Narrative
At 08:25 on october 23, 2021, magellan operations personnel were conducting a daily facility inspection when the tank 422 mixer was found leaking from the tattletale. Product was transferred from the tank and cleanup activities were initiated. Upon further investigation it was determined that the inner bearing failed which allowed the seal on the tank mixer to wear and eventually fail. To prevent recurrence, the gear box and seal were replaced. The tank was then placed back into service. Supplemental/final (03-16-2022) part h narrative
| Report Received Date | 2021-11-18 00:00:00 |
|---|---|
| Iyear | 2021 |
| Report Number | 20210324 |
| Supplemental Number | 36478 |
| Report Type | Supplemental Final |
| Operator Id | 31580 PHMSA Enforcement |
| Name | Magellan Terminals Holdings, Lp |
| Operator Street Address | 100 West 5th Street |
| Operator City Name | Tulsa |
| Operator State Abbreviation | OK |
| Operator Postal Code | 74103 |
| Local Datetime | 2021-10-23 08:25:00 |
| Time Zone | Central |
| Daylight Savings Ind | Yes |
| Location Latitude | 29.751489 Google Maps OpenStreetMap |
| Location Longitude | -95.203937 Google Maps OpenStreetMap |
| Commodity Released Type | Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions |
| Commodity Subtype | Mixture Of Refined Products (Transmix Or Other Mixture) |
| Unintentional Release Bbls | 3 |
| Recovered Bbls | 3 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Accident Identifier | Local Operating Personnel, Including Contractors |
| Operator Type | Operator Employee |
| Incident Identified Datetime | 2021-10-23 08:25:00 |
| System Part Involved | Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances |
| On Off Shore | Onshore |
| Status When Identified | Idle |
| Communication State Fed Ind | No |
| On Site Datetime | 2021-10-23 08:25:00 |
| Confirmed Discovery Datetime | 2021-10-23 08:25:00 |
| Nrc Rpt Num | Nrc Notification Not Required NRC Report How to search |
| Ignite Ind | No |
| Notify Qualified Indiv Ind | Yes |
| Qualified Indiv Notif Datetime | 2021-10-23 08:25:00 |
| Oil Spill Removal Org Ind | No |
| Num Pub Evacuated | 0 |
| Pipe Fac Name | Galena Park Terminal |
| Segment Name | Fac Id 474 |
| Onshore State Abbreviation | Tx |
| Onshore Postal Code | 77547 |
| Onshore City Name | Galena Park |
| Onshore County Name | Harris |
| Designated Location | Milepost |
| Designated Name | 0 |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Tank, Including Attached Appurtenances |
| Crossing | No |
| Pipe Facility Type | Intrastate |
| Item Involved | Tank/vessel |
| Tank Vessel Subtype | Mixer |
| Tank Type | Atmospheric |
| Safe Fill Level | 55.5 |
| Safe Fill Level Exceeded Ind | No |
| Api Std Out Of Service Year | 2021 |
| Api Std In Service Year | 2021 |
| Installation Year | 2012 |
| Manufactured Year | 2012 |
| Material Involved | Carbon Steel |
| Release Type | Leak |
| Leak Type | Seal Or Packing |
| Wildlife Impact Ind | No |
| Soil Contamination | Yes |
| Long Term Assessment | No |
| Remediation Ind | No |
| Water Contam Ind | No |
| Could Be Hca | Yes |
| Commodity Reached Hca | Yes |
| High Pop Ind | Yes |
| High Pop Yes No | Yes |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 2058 |
| Est Cost Prop Damage | 22000 |
| Est Cost Emergency | 6451 |
| Est Cost Environmental | 0 |
| Est Cost Other | 0 |
| Prpty | 30509 |
| Num Persons Hosp Not Ovnght | 0 |
| Num Injured Treated By Emt | 0 |
| Num Resident Building Affctd | 0 |
| Num Business Building Affctd | 0 |
| Accident Psig | 12.1 |
| Pressure Restriction Ind | No |
| Pipeline Function | > 20% Smys Regulated Transmission |
| Scada In Place Ind | Yes |
| Scada Operating Ind | Yes |
| Scada Functional Ind | Yes |
| Scada Detection Ind | No |
| Scada Conf Ind | No |
| Cpm In Place Ind | No |
| Investigation Status | No, the facility was not monitored by a controller(s) at the time of the accident |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Equipment Failure |
| Cause Details | Non-Threaded Connection Failure |
| Eq Failure Type | Non-Threaded Connection Failure |
| Other Non Threaded Ind | Seal (Not Pump Seal) Or Packing |
| Eq Additional Other Ind | Yes |
| Eq Additional Other Details | Normal Wear |
| Preparer Name | S****** L****** |
| Preparer Title | Ai Analyst |
| Preparer Email | S**************@m*********.com |
| Preparer Telephone | 918-574-7327 |
| Preparer Fax | 918-574-7376 |
| Prepared Date | 2022-03-21 00:00:00 |
| Authorizer Name | G**** R**** |
| Authorizer Telephone | 918-574-7165 |
| Authorizer Title | Supervisor Integrity Management |
| Authorizer Email | G**********@m*********.com |
| Narrative | At 08:25 on october 23, 2021, magellan operations personnel were conducting a daily facility inspection when the tank 422 mixer was found leaking from the tattletale. Product was transferred from the tank and cleanup activities were initiated. Upon further investigation it was determined that the inner bearing failed which allowed the seal on the tank mixer to wear and eventually fail. To prevent recurrence, the gear box and seal were replaced. The tank was then placed back into service. Supplemental/final (03-16-2022) part h narrative |
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