HL incident on 2021-10-15 — OK

Operator
Williams Field Services - Gulf Coast Company, Lp
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$400
Incident datetime
2021-10-15 03:30
Report number
Location
OK
Narrative
Williams operations personnel were notified of a gas detector alarm at ~3:30 am on october 15th, 2021. Williams techs responded and arrived on site to discover the dielectric fitting on the recently installed transmitter tubing had failed and the product was being released. Williams personnel donned respiratory protection and approached upwind to isolate the section of the tubing by closing the pit200 transmitter root valve. Once the section of 3/8" tubing was isolated, approximately 10' of length, the product contained and to vent off until pressure was completely relieved. Once tubing was isolated and at zero pressure, the failed fitting was removed and replaced with new tubing.
Detailed record list
Report Received Date
2021-11-04 00:00:00
Iyear
2021
Report Number
20210313
Supplemental Number
35959
Report Type
Original Final
Operator Id
Name
Williams Field Services - Gulf Coast Company, Lp
Operator Street Address
One Williams Center P.o. Box 645
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74172
Local Datetime
2021-10-15 03:30:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Anhydrous Ammonia
Unintentional Release Bbls
1.96
Intentional Release Bbls
0.1
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime
2021-10-15 03:30:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Tubing Was Isolated And System Did Not Need To Be Shut Down
On Site Datetime
2021-10-15 05:00:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Dpkd - Ammonia
Segment Name
1894
Onshore State Abbreviation
Tx
Onshore Postal Code
77536
Onshore City Name
Deer Park
Onshore County Name
Harris County
Designated Location
Milepost/valve Station
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Tubing
Installation Year
2021
Material Involved
Material Other Than Carbon Steel
Material Details
Stainless Steel
Release Type
Other
Release Type Details
Swagelok Dielectric Fitting
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
258
Est Cost Prop Damage
400
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
658
Accident Psig
372
Mop Psig
686
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
10
Internal Inspection Ind
No
Other Inspection Ind
Yes
Internal Inspection Details
3/8" Stainless Steel Tubing
Operation Complications Ind
Yes
Other Complications Ind
Yes
Inspect Comp Details
3/8" Stainless Steel Tubing
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Controller performed actions as required.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Defective Or Loose Tubing Or Fitting
Eq Failure Type
Defective Or Loose Tubing Or Fitting
Additional Breakdown Ind
Yes
Preparer Name
E**** R********
Preparer Title
Regulatory Compliance Specialist Sr.
Preparer Email
E****************@w*******.com
Preparer Telephone
7132152846
Prepared Date
2021-11-04 00:00:00
Authorizer Name
T**** G****
Authorizer Telephone
3605942137
Authorizer Title
Manager Pipeline Safety
Authorizer Email
T**********@w*******.com
Narrative
Williams operations personnel were notified of a gas detector alarm at ~3:30 am on october 15th, 2021. Williams techs responded and arrived on site to discover the dielectric fitting on the recently installed transmitter tubing had failed and the product was being released. Williams personnel donned respiratory protection and approached upwind to isolate the section of the tubing by closing the pit200 transmitter root valve. Once the section of 3/8" tubing was isolated, approximately 10' of length, the product contained and to vent off until pressure was completely relieved. Once tubing was isolated and at zero pressure, the failed fitting was removed and replaced with new tubing.
Report Received Date 2021-11-04 00:00:00
Iyear 2021
Report Number 20210313
Supplemental Number 35959
Report Type Original Final
Operator Id 994 PHMSA Enforcement
Name Williams Field Services - Gulf Coast Company, Lp
Operator Street Address One Williams Center P.o. Box 645
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74172
Local Datetime 2021-10-15 03:30:00
Location Latitude 29.721356 Google Maps OpenStreetMap
Location Longitude -95.107697 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Anhydrous Ammonia
Unintentional Release Bbls 1.96
Intentional Release Bbls 0.1
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime 2021-10-15 03:30:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Tubing Was Isolated And System Did Not Need To Be Shut Down
On Site Datetime 2021-10-15 05:00:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Dpkd - Ammonia
Segment Name 1894
Onshore State Abbreviation Tx
Onshore Postal Code 77536
Onshore City Name Deer Park
Onshore County Name Harris County
Designated Location Milepost/valve Station
Designated Name 0
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Tubing
Installation Year 2021
Material Involved Material Other Than Carbon Steel
Material Details Stainless Steel
Release Type Other
Release Type Details Swagelok Dielectric Fitting
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 258
Est Cost Prop Damage 400
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 658
Accident Psig 372
Mop Psig 686
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 10
Internal Inspection Ind No
Other Inspection Ind Yes
Internal Inspection Details 3/8" Stainless Steel Tubing
Operation Complications Ind Yes
Other Complications Ind Yes
Inspect Comp Details 3/8" Stainless Steel Tubing
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Controller performed actions as required.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Defective Or Loose Tubing Or Fitting
Eq Failure Type Defective Or Loose Tubing Or Fitting
Additional Breakdown Ind Yes
Preparer Name E**** R********
Preparer Title Regulatory Compliance Specialist Sr.
Preparer Email E****************@w*******.com
Preparer Telephone 7132152846
Prepared Date 2021-11-04 00:00:00
Authorizer Name T**** G****
Authorizer Telephone 3605942137
Authorizer Title Manager Pipeline Safety
Authorizer Email T**********@w*******.com
Narrative Williams operations personnel were notified of a gas detector alarm at ~3:30 am on october 15th, 2021. Williams techs responded and arrived on site to discover the dielectric fitting on the recently installed transmitter tubing had failed and the product was being released. Williams personnel donned respiratory protection and approached upwind to isolate the section of the tubing by closing the pit200 transmitter root valve. Once the section of 3/8" tubing was isolated, approximately 10' of length, the product contained and to vent off until pressure was completely relieved. Once tubing was isolated and at zero pressure, the failed fitting was removed and replaced with new tubing.

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