HL incident on 2021-09-03 — GA

Operator
Colonial Pipeline Co
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$14,494
Incident datetime
2021-09-03 07:15
Report number
Location
GA
Narrative
On 9/4/2021 at 7:51 a routine station check identified product overflowing at the l1 injection pump drain pan. Pressure was relieved from the idle pump circuit and pump piston packing was adjusted. It was then discovered that the drain line to the station sump was plugged resulting in the overflow to the ground. Product was found in a valve well adjacent to the injection pump. An estimated 7 gallons of gasoline was collected and an additional 2 gallons is estimated in the excavated soil. No external notifications were required. No additional action is required. A supplemental final report will be issued after all costs associated with response to the release are quantified. Update: sludge/debris was discovered to have clogged the 1 inch drain line from the pump drain basin to the station sump, causing the drain to backup, fill the basin, and eventually result in a product overflow. The injection pump and drain line were installed in 1963, however, the exact date for the mop is unknown. A process was implemented to proactively flush the injection pump drain line to ensure it is clear of any debris before use.
Detailed record list
Report Received Date
2021-10-01 00:00:00
Iyear
2021
Report Number
20210284
Supplemental Number
36709
Report Type
Supplemental Final
Operator Id
Name
Colonial Pipeline Co
Operator Street Address
1000 Lake St.
Operator City Name
Alpharetta
Operator State Abbreviation
GA
Operator Postal Code
30009
Local Datetime
2021-09-04 07:15:00
Time Zone
Central
Daylight Savings Ind
Yes
Location Latitude
Location Longitude
-86.80294942
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
0.2
Recovered Bbls
0.2
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2021-09-03 07:15:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Status When Identified
Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind
No
Shutdown Explain
Leak Occurred On An Injection Pump Drain Line, Pipeline Could Still Operate
Communication State Fed Ind
No
On Site Datetime
2021-09-04 07:15:00
Confirmed Discovery Datetime
2021-09-04 07:15:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Notify Qualified Indiv Ind
No
Oil Spill Removal Org Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Pelham Junction
Segment Name
Pelham To Atlanta
Onshore State Abbreviation
Al
Onshore Postal Code
35124
Onshore City Name
Pelham
Onshore County Name
Shelby
Designated Location
Survey Station No.
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Drain Lines
Installation Year
1963
Manufactured Year
1963
Material Involved
Carbon Steel
Release Type
Overfill Or Overflow
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
16
Est Cost Prop Damage
14494
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
14510
Num Persons Hosp Not Ovnght
0
Num Injured Treated By Emt
0
Num Resident Building Affctd
0
Num Business Building Affctd
0
Accident Psig
0
Mop Psig
275
Mop Cfr Section
Component Design Pressure �195.406(A)(2)
Maop Established Date
1963-01-01 00:00:00
Maop Reversal Flow Ind
No
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
L1 injection pump drain line was plugged. Controller actions did not contribute to the incident.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Other Equipment Failure
Eq Failure Type
Other Equipment Failure
Failure Details
Drain Line Was Clogged Which Caused Product To Back Up And Overflow The Pump Drain Basin.
Additional Improper Mntnce Ind
Yes
Preparer Name
D***** L******
Preparer Title
Compliance Coordinator
Preparer Email
D*******@c******.com
Preparer Telephone
770.819.3574
Prepared Date
2022-05-27 00:00:00
Authorizer Name
Q****** F******
Authorizer Telephone
6787622270
Authorizer Title
Director Pipeline Compliance
Authorizer Email
Q*******@c******.com
Narrative
On 9/4/2021 at 7:51 a routine station check identified product overflowing at the l1 injection pump drain pan. Pressure was relieved from the idle pump circuit and pump piston packing was adjusted. It was then discovered that the drain line to the station sump was plugged resulting in the overflow to the ground. Product was found in a valve well adjacent to the injection pump. An estimated 7 gallons of gasoline was collected and an additional 2 gallons is estimated in the excavated soil. No external notifications were required. No additional action is required. A supplemental final report will be issued after all costs associated with response to the release are quantified. Update: sludge/debris was discovered to have clogged the 1 inch drain line from the pump drain basin to the station sump, causing the drain to backup, fill the basin, and eventually result in a product overflow. The injection pump and drain line were installed in 1963, however, the exact date for the mop is unknown. A process was implemented to proactively flush the injection pump drain line to ensure it is clear of any debris before use.
Report Received Date 2021-10-01 00:00:00
Iyear 2021
Report Number 20210284
Supplemental Number 36709
Report Type Supplemental Final
Operator Id 2552 PHMSA Enforcement
Name Colonial Pipeline Co
Operator Street Address 1000 Lake St.
Operator City Name Alpharetta
Operator State Abbreviation GA
Operator Postal Code 30009
Local Datetime 2021-09-04 07:15:00
Time Zone Central
Daylight Savings Ind Yes
Location Latitude 33.28180097 Google Maps OpenStreetMap
Location Longitude -86.80294942 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 0.2
Recovered Bbls 0.2
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2021-09-03 07:15:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Status When Identified Normal Operation, Includes Pauses Between Batches And During Maintenance
Shutdown Due Accident Ind No
Shutdown Explain Leak Occurred On An Injection Pump Drain Line, Pipeline Could Still Operate
Communication State Fed Ind No
On Site Datetime 2021-09-04 07:15:00
Confirmed Discovery Datetime 2021-09-04 07:15:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Notify Qualified Indiv Ind No
Oil Spill Removal Org Ind No
Num Pub Evacuated 0
Pipe Fac Name Pelham Junction
Segment Name Pelham To Atlanta
Onshore State Abbreviation Al
Onshore Postal Code 35124
Onshore City Name Pelham
Onshore County Name Shelby
Designated Location Survey Station No.
Designated Name 0
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Drain Lines
Installation Year 1963
Manufactured Year 1963
Material Involved Carbon Steel
Release Type Overfill Or Overflow
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 16
Est Cost Prop Damage 14494
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 14510
Num Persons Hosp Not Ovnght 0
Num Injured Treated By Emt 0
Num Resident Building Affctd 0
Num Business Building Affctd 0
Accident Psig 0
Mop Psig 275
Mop Cfr Section Component Design Pressure �195.406(A)(2) View CFR 49 §192
Maop Established Date 1963-01-01 00:00:00
Maop Reversal Flow Ind No
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details L1 injection pump drain line was plugged. Controller actions did not contribute to the incident.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Other Equipment Failure
Eq Failure Type Other Equipment Failure
Failure Details Drain Line Was Clogged Which Caused Product To Back Up And Overflow The Pump Drain Basin.
Additional Improper Mntnce Ind Yes
Preparer Name D***** L******
Preparer Title Compliance Coordinator
Preparer Email D*******@c******.com
Preparer Telephone 770.819.3574
Prepared Date 2022-05-27 00:00:00
Authorizer Name Q****** F******
Authorizer Telephone 6787622270
Authorizer Title Director Pipeline Compliance
Authorizer Email Q*******@c******.com
Narrative On 9/4/2021 at 7:51 a routine station check identified product overflowing at the l1 injection pump drain pan. Pressure was relieved from the idle pump circuit and pump piston packing was adjusted. It was then discovered that the drain line to the station sump was plugged resulting in the overflow to the ground. Product was found in a valve well adjacent to the injection pump. An estimated 7 gallons of gasoline was collected and an additional 2 gallons is estimated in the excavated soil. No external notifications were required. No additional action is required. A supplemental final report will be issued after all costs associated with response to the release are quantified. Update: sludge/debris was discovered to have clogged the 1 inch drain line from the pump drain basin to the station sump, causing the drain to backup, fill the basin, and eventually result in a product overflow. The injection pump and drain line were installed in 1963, however, the exact date for the mop is unknown. A process was implemented to proactively flush the injection pump drain line to ensure it is clear of any debris before use.

All rights reserved. Copyright © by ClearPHMSA