HL incident on 2021-08-20 — LA

Operator
Crescent Midstream, Llc
Cause
Incorrect Operation
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2021-08-20 11:40
Report number
Location
LA
Narrative
Crescent was conducting riser maintenance on ei-259a. A water filtration unit was placed on the deck to filter the hydrostatic test water. The filtration crew connected the system to crescent's pipeline via a one inch valve. The valve was left in the open position. The section of pipe was active, but not flowing at the time. Shortly after the pipeline came online, crude oil was directed to the filtration inlet tank through the one inch valve. Crude oil over flowed the inlet tank on the temporary filtration unit resulting in a release of crude oil.
Detailed record list
Report Received Date
2021-09-20 00:00:00
Iyear
2021
Report Number
20210265
Supplemental Number
35754
Report Type
Original Final
Operator Id
Name
Crescent Midstream, Llc
Operator Street Address
263 Trinity Lane
Operator City Name
Gray
Operator State Abbreviation
LA
Operator Postal Code
70359
Local Datetime
2021-08-20 12:24:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.34
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2021-08-20 11:40:00
System Part Involved
Offshore Platform/deepwater Port, Including Platform-Mounted Equipment And Piping
On Off Shore
Offshore
Shutdown Due Accident Ind
No
Shutdown Explain
Incorrect Operation, 1" Valve Was Secured (Closed)
On Site Datetime
2021-08-20 11:45:00
Nrc Rpt Datetime
2021-08-20 12:24:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Off Water Depth
100
Off Accident Origin
On The Outer Continental Shelf (Ocs)
Off Ocs Area
Eugene Island
Off Ocs Block
259
Off Area Accident Type
Platform
Pipe Facility Type
Interstate
Item Involved
Other
Item Involved Details
Temporary Filtration System
Installation Year
Unknown
Material Involved
Carbon Steel
Release Type
Overfill Or Overflow
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
Yes
Ocean Seawater Ind
Yes
Amount Released
0.34
Rel Water Name
Gulf Of Mexico
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
25
Est Cost Prop Damage
0
Est Cost Emergency
200
Est Cost Environmental
0
Est Cost Other
0
Prpty
225
Accident Psig
30
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
< 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The release was a result of incorrect operation of a one inch ball valve during pipeline maintenance activity.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Operation Type
Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Overflow Other Ind
Valve Misalignment
Related Failure Follow Ind
Yes
Category Type
Other Maintenance
Operator Qualification Ind
Yes
Qualified Individuals
No, But They Were Performing The Task(S) Under The Direction And Observation Of A Qualified Individual
Preparer Name
D***** P****
Preparer Title
Safety Regulatory Compliance Supervisor
Preparer Email
D*****@c**********.com
Prepared Date
2021-09-20 00:00:00
Authorizer Name
D***** S****
Authorizer Telephone
985-772-3546
Authorizer Title
Vp Operations
Authorizer Email
D******@c**********.com
Narrative
Crescent was conducting riser maintenance on ei-259a. A water filtration unit was placed on the deck to filter the hydrostatic test water. The filtration crew connected the system to crescent's pipeline via a one inch valve. The valve was left in the open position. The section of pipe was active, but not flowing at the time. Shortly after the pipeline came online, crude oil was directed to the filtration inlet tank through the one inch valve. Crude oil over flowed the inlet tank on the temporary filtration unit resulting in a release of crude oil.
Report Received Date 2021-09-20 00:00:00
Iyear 2021
Report Number 20210265
Supplemental Number 35754
Report Type Original Final
Operator Id 39084 PHMSA Enforcement
Name Crescent Midstream, Llc
Operator Street Address 263 Trinity Lane
Operator City Name Gray
Operator State Abbreviation LA
Operator Postal Code 70359
Local Datetime 2021-08-20 12:24:00
Location Latitude 28.453569 Google Maps OpenStreetMap
Location Longitude -91.456368 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.34
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2021-08-20 11:40:00
System Part Involved Offshore Platform/deepwater Port, Including Platform-Mounted Equipment And Piping
On Off Shore Offshore
Shutdown Due Accident Ind No
Shutdown Explain Incorrect Operation, 1" Valve Was Secured (Closed)
On Site Datetime 2021-08-20 11:45:00
Nrc Rpt Datetime 2021-08-20 12:24:00
Nrc Rpt Num 1314243 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Off Water Depth 100
Off Accident Origin On The Outer Continental Shelf (Ocs)
Off Ocs Area Eugene Island
Off Ocs Block 259
Off Area Accident Type Platform
Pipe Facility Type Interstate
Item Involved Other
Item Involved Details Temporary Filtration System
Installation Year Unknown
Material Involved Carbon Steel
Release Type Overfill Or Overflow
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind Yes
Ocean Seawater Ind Yes
Amount Released 0.34
Rel Water Name Gulf Of Mexico
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 25
Est Cost Prop Damage 0
Est Cost Emergency 200
Est Cost Environmental 0
Est Cost Other 0
Prpty 225
Accident Psig 30
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function < 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The release was a result of incorrect operation of a one inch ball valve during pipeline maintenance activity.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Operation Type Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Overflow Other Ind Valve Misalignment
Related Failure Follow Ind Yes
Category Type Other Maintenance
Operator Qualification Ind Yes
Qualified Individuals No, But They Were Performing The Task(S) Under The Direction And Observation Of A Qualified Individual
Preparer Name D***** P****
Preparer Title Safety Regulatory Compliance Supervisor
Preparer Email D*****@c**********.com
Prepared Date 2021-09-20 00:00:00
Authorizer Name D***** S****
Authorizer Telephone 985-772-3546
Authorizer Title Vp Operations
Authorizer Email D******@c**********.com
Narrative Crescent was conducting riser maintenance on ei-259a. A water filtration unit was placed on the deck to filter the hydrostatic test water. The filtration crew connected the system to crescent's pipeline via a one inch valve. The valve was left in the open position. The section of pipe was active, but not flowing at the time. Shortly after the pipeline came online, crude oil was directed to the filtration inlet tank through the one inch valve. Crude oil over flowed the inlet tank on the temporary filtration unit resulting in a release of crude oil.

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