HL incident on 2021-08-26 — PA

Operator
Buckeye Partners, Lp
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$25
Incident datetime
2021-08-26 09:30
Report number
Location
PA
Narrative
On 8/26/2021 at approximately 09:30 am local buckeye personnel while performing routine rounds, observed free product inside the scraper trap secondary containment area. The operator immediately opened the trap drain which stopped the release. Upon further investigation local operations discovered the o-ring located at the bottom of the scraper trap had failed causing product to be released from the bottom of the trap. The o-ring failed at the bottom side of the gasket due to the 30inch trap door hinges being worn and not sealing evenly when closing the door. The gasket wore away at the bottom edge at the 6 o'clock position. All free standing product was contained in secondary containment on the concrete pad. All internal and external notifications were made. Osro arrived on site. Clean up activities were completed. The initial report to the nrc stated a total of approximately 16 barrels was released however after response activities were complete it was determined 9 barrels was released. This was determined after cleanup activities indicated the recovered barrels consisted of approximately 50% water and dirt. There were no injuries. No further remediation is needed. 9/30/2021 a new scraper trap door will be installed before being put back into service.
Detailed record list
Report Received Date
2021-09-13 00:00:00
Iyear
2021
Report Number
20210256
Supplemental Number
35803
Report Type
Supplemental Final
Operator Id
Name
Buckeye Partners, Lp
Operator Street Address
The Buckeye Building 6161 Hamilton Boulevar
Operator City Name
Allentown
Operator State Abbreviation
PA
Operator Postal Code
18106
Local Datetime
2021-08-26 09:30:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
9
Recovered Bbls
9
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2021-08-26 09:30:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Pipeline Was Not Active At The Time Of The Release
On Site Datetime
2021-08-26 09:30:00
Nrc Rpt Datetime
2021-08-26 11:25:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Mechanicsburg Station
Segment Name
Mechanicsburg Station
Onshore State Abbreviation
Pa
Onshore Postal Code
17050
Onshore City Name
Mechanicsburg
Onshore County Name
Cumberland
Designated Location
Milepost/valve Station
Designated Name
Mp Station
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Scraper/pig Trap
Installation Year
1958
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Commercially Nav Yes No
No
High Pop Yes No
No
Other Pop Yes No
No
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Usa Ecological Yes No
No
Est Cost Oper Paid
0
Est Cost Gas Released
850
Est Cost Prop Damage
25
Est Cost Emergency
3200
Est Cost Environmental
0
Est Cost Other
0
Prpty
4075
Accident Psig
346
Mop Psig
1045
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The pipeline was not active at the time of the failure
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
O-Ring
Ief Addl Misalignment Ind
Yes
Preparer Name
D*** C*****
Preparer Title
Regional Sr Regulatory Specialist
Preparer Email
D******@b******.com
Preparer Telephone
484-707-1426
Prepared Date
2021-09-30 00:00:00
Authorizer Name
C****** P********
Authorizer Telephone
610-904-4113
Authorizer Title
Director Regulatory Compliance
Authorizer Email
C*********@b******.com
Narrative
On 8/26/2021 at approximately 09:30 am local buckeye personnel while performing routine rounds, observed free product inside the scraper trap secondary containment area. The operator immediately opened the trap drain which stopped the release. Upon further investigation local operations discovered the o-ring located at the bottom of the scraper trap had failed causing product to be released from the bottom of the trap. The o-ring failed at the bottom side of the gasket due to the 30inch trap door hinges being worn and not sealing evenly when closing the door. The gasket wore away at the bottom edge at the 6 o'clock position. All free standing product was contained in secondary containment on the concrete pad. All internal and external notifications were made. Osro arrived on site. Clean up activities were completed. The initial report to the nrc stated a total of approximately 16 barrels was released however after response activities were complete it was determined 9 barrels was released. This was determined after cleanup activities indicated the recovered barrels consisted of approximately 50% water and dirt. There were no injuries. No further remediation is needed. 9/30/2021 a new scraper trap door will be installed before being put back into service.
Report Received Date 2021-09-13 00:00:00
Iyear 2021
Report Number 20210256
Supplemental Number 35803
Report Type Supplemental Final
Operator Id 1845 PHMSA Enforcement
Name Buckeye Partners, Lp
Operator Street Address The Buckeye Building 6161 Hamilton Boulevar
Operator City Name Allentown
Operator State Abbreviation PA
Operator Postal Code 18106
Local Datetime 2021-08-26 09:30:00
Location Latitude 40.22723 Google Maps OpenStreetMap
Location Longitude -77.048106 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 9
Recovered Bbls 9
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2021-08-26 09:30:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Pipeline Was Not Active At The Time Of The Release
On Site Datetime 2021-08-26 09:30:00
Nrc Rpt Datetime 2021-08-26 11:25:00
Nrc Rpt Num 1314777 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Mechanicsburg Station
Segment Name Mechanicsburg Station
Onshore State Abbreviation Pa
Onshore Postal Code 17050
Onshore City Name Mechanicsburg
Onshore County Name Cumberland
Designated Location Milepost/valve Station
Designated Name Mp Station
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Scraper/pig Trap
Installation Year 1958
Material Involved Carbon Steel
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Commercially Nav Yes No No
High Pop Yes No No
Other Pop Yes No No
Usa Drinking Ind Yes
Usa Drinking Yes No Yes
Usa Ecological Yes No No
Est Cost Oper Paid 0
Est Cost Gas Released 850
Est Cost Prop Damage 25
Est Cost Emergency 3200
Est Cost Environmental 0
Est Cost Other 0
Prpty 4075
Accident Psig 346
Mop Psig 1045
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The pipeline was not active at the time of the failure
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind O-Ring
Ief Addl Misalignment Ind Yes
Preparer Name D*** C*****
Preparer Title Regional Sr Regulatory Specialist
Preparer Email D******@b******.com
Preparer Telephone 484-707-1426
Prepared Date 2021-09-30 00:00:00
Authorizer Name C****** P********
Authorizer Telephone 610-904-4113
Authorizer Title Director Regulatory Compliance
Authorizer Email C*********@b******.com
Narrative On 8/26/2021 at approximately 09:30 am local buckeye personnel while performing routine rounds, observed free product inside the scraper trap secondary containment area. The operator immediately opened the trap drain which stopped the release. Upon further investigation local operations discovered the o-ring located at the bottom of the scraper trap had failed causing product to be released from the bottom of the trap. The o-ring failed at the bottom side of the gasket due to the 30inch trap door hinges being worn and not sealing evenly when closing the door. The gasket wore away at the bottom edge at the 6 o'clock position. All free standing product was contained in secondary containment on the concrete pad. All internal and external notifications were made. Osro arrived on site. Clean up activities were completed. The initial report to the nrc stated a total of approximately 16 barrels was released however after response activities were complete it was determined 9 barrels was released. This was determined after cleanup activities indicated the recovered barrels consisted of approximately 50% water and dirt. There were no injuries. No further remediation is needed. 9/30/2021 a new scraper trap door will be installed before being put back into service.

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