HL incident on 2021-08-11 — GA

Operator
Colonial Pipeline Co
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2021-08-11 00:36
Report number
Location
GA
Narrative
On 8/11/21, at approximately 00:36, a houston (htn) colonial operator smelled product conducting a yard check and began investigating the source. The operator noticed stained rocks surrounding the line 2 (l2) eva shipper valve. This led the operator to observe ultra low sulfur diesel (ulsd) in 3 access wells next to the valve. The operator informed the on-shift a & b operators. Htn l2 was shutdown pending investigation of the leak source and notifications were made to appropriate personnel. Operations at this valve required further investigation to determine the responsible party. A potential responsible party submitted a nrc call (nrc incident report # 1313343). The summary of this call included joint investigation actions underway to determine the leak source and responsible party. 8/12/21, colonial confirmed ownership of the leak source (responsible party). Colonial found the leak to be a result of a valve body guide plug malfunction. At approximately 11:00 cst, colonial discovered the spill response costs may exceed $50,000 and made a notification to the nrc (nrc incident report #1313487). Additionally, PHMSA aid was contacted to clarify incident report # 1313343 discussed above was the same leak. Other notifications were made as required. Approximately 100 gallons of ulsd was released and contained onsite. On 8/14/2021, colonial conducted a 48 hour updated notification to nrc incident # 1313487. This notification reported no significant changes other than the valve repair was completed on 8/13/21. An ia will be conducted for this incident.
Detailed record list
Report Received Date
2021-08-26 00:00:00
Iyear
2021
Report Number
20210242
Supplemental Number
35670
Report Type
Original Final
Operator Id
Name
Colonial Pipeline Co
Operator Street Address
1000 Lake St.
Operator City Name
Alpharetta
Operator State Abbreviation
GA
Operator Postal Code
30009
Local Datetime
2021-08-11 00:36:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
2.4
Recovered Bbls
2.4
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2021-08-11 00:36:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2021-08-11 00:40:00
Restart Datetime
2021-08-14 04:53:00
On Site Datetime
2021-08-11 00:36:00
Nrc Rpt Datetime
2021-08-12 12:43:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Line 2 Shipper Manifold
Segment Name
0120
Onshore State Abbreviation
Tx
Onshore Postal Code
77506
Onshore City Name
Houston
Onshore County Name
Harris
Designated Location
Milepost/valve Station
Designated Name
120
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
60
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Installation Year
2005
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Other
Leak Type Other
Valve Guide Plug Malfunction
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Other Pop Ind
Yes
Other Pop Yes No
No
Est Cost Oper Paid
0
Est Cost Gas Released
20717
Est Cost Prop Damage
0
Est Cost Emergency
204228
Est Cost Environmental
0
Est Cost Other
0
Prpty
224945
Accident Psig
74
Mop Psig
74
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Equipment failure
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Failure Of Equipment Body (Except Pump), Tank Plate, Or Other Material
Eq Failure Type
Failure Of Equipment Body (Except Pump), Tank Plate, Or Other Material
Eq Additional Other Ind
Yes
Eq Additional Other Details
Valve Body Guide Plug Malfunction
Preparer Name
R***** A** D*****
Preparer Title
Compliance Coordinator
Preparer Email
D*********@y****.com
Preparer Telephone
4097904288
Prepared Date
2021-08-26 00:00:00
Authorizer Name
M*** P*****
Authorizer Telephone
678-763-5911
Authorizer Title
Compliance Manager
Authorizer Email
M******@c******.com
Narrative
On 8/11/21, at approximately 00:36, a houston (htn) colonial operator smelled product conducting a yard check and began investigating the source. The operator noticed stained rocks surrounding the line 2 (l2) eva shipper valve. This led the operator to observe ultra low sulfur diesel (ulsd) in 3 access wells next to the valve. The operator informed the on-shift a & b operators. Htn l2 was shutdown pending investigation of the leak source and notifications were made to appropriate personnel. Operations at this valve required further investigation to determine the responsible party. A potential responsible party submitted a nrc call (nrc incident report # 1313343). The summary of this call included joint investigation actions underway to determine the leak source and responsible party. 8/12/21, colonial confirmed ownership of the leak source (responsible party). Colonial found the leak to be a result of a valve body guide plug malfunction. At approximately 11:00 cst, colonial discovered the spill response costs may exceed $50,000 and made a notification to the nrc (nrc incident report #1313487). Additionally, PHMSA aid was contacted to clarify incident report # 1313343 discussed above was the same leak. Other notifications were made as required. Approximately 100 gallons of ulsd was released and contained onsite. On 8/14/2021, colonial conducted a 48 hour updated notification to nrc incident # 1313487. This notification reported no significant changes other than the valve repair was completed on 8/13/21. An ia will be conducted for this incident.
Report Received Date 2021-08-26 00:00:00
Iyear 2021
Report Number 20210242
Supplemental Number 35670
Report Type Original Final
Operator Id 2552 PHMSA Enforcement
Name Colonial Pipeline Co
Operator Street Address 1000 Lake St.
Operator City Name Alpharetta
Operator State Abbreviation GA
Operator Postal Code 30009
Local Datetime 2021-08-11 00:36:00
Location Latitude 29.718597 Google Maps OpenStreetMap
Location Longitude -95.179549 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls 2.4
Recovered Bbls 2.4
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2021-08-11 00:36:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2021-08-11 00:40:00
Restart Datetime 2021-08-14 04:53:00
On Site Datetime 2021-08-11 00:36:00
Nrc Rpt Datetime 2021-08-12 12:43:00
Nrc Rpt Num 1313487 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Line 2 Shipper Manifold
Segment Name 0120
Onshore State Abbreviation Tx
Onshore Postal Code 77506
Onshore City Name Houston
Onshore County Name Harris
Designated Location Milepost/valve Station
Designated Name 120
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 60
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Installation Year 2005
Material Involved Carbon Steel
Release Type Leak
Leak Type Other
Leak Type Other Valve Guide Plug Malfunction
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Other Pop Ind Yes
Other Pop Yes No No
Est Cost Oper Paid 0
Est Cost Gas Released 20717
Est Cost Prop Damage 0
Est Cost Emergency 204228
Est Cost Environmental 0
Est Cost Other 0
Prpty 224945
Accident Psig 74
Mop Psig 74
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Equipment failure
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Failure Of Equipment Body (Except Pump), Tank Plate, Or Other Material
Eq Failure Type Failure Of Equipment Body (Except Pump), Tank Plate, Or Other Material
Eq Additional Other Ind Yes
Eq Additional Other Details Valve Body Guide Plug Malfunction
Preparer Name R***** A** D*****
Preparer Title Compliance Coordinator
Preparer Email D*********@y****.com
Preparer Telephone 4097904288
Prepared Date 2021-08-26 00:00:00
Authorizer Name M*** P*****
Authorizer Telephone 678-763-5911
Authorizer Title Compliance Manager
Authorizer Email M******@c******.com
Narrative On 8/11/21, at approximately 00:36, a houston (htn) colonial operator smelled product conducting a yard check and began investigating the source. The operator noticed stained rocks surrounding the line 2 (l2) eva shipper valve. This led the operator to observe ultra low sulfur diesel (ulsd) in 3 access wells next to the valve. The operator informed the on-shift a & b operators. Htn l2 was shutdown pending investigation of the leak source and notifications were made to appropriate personnel. Operations at this valve required further investigation to determine the responsible party. A potential responsible party submitted a nrc call (nrc incident report # 1313343). The summary of this call included joint investigation actions underway to determine the leak source and responsible party. 8/12/21, colonial confirmed ownership of the leak source (responsible party). Colonial found the leak to be a result of a valve body guide plug malfunction. At approximately 11:00 cst, colonial discovered the spill response costs may exceed $50,000 and made a notification to the nrc (nrc incident report #1313487). Additionally, PHMSA aid was contacted to clarify incident report # 1313343 discussed above was the same leak. Other notifications were made as required. Approximately 100 gallons of ulsd was released and contained onsite. On 8/14/2021, colonial conducted a 48 hour updated notification to nrc incident # 1313487. This notification reported no significant changes other than the valve repair was completed on 8/13/21. An ia will be conducted for this incident.

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