HL incident on 2021-07-22 — OH

Operator
Marathon Pipe Line Llc
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$40,000
Incident datetime
2021-07-22 07:15
Report number
Location
OH
Narrative
On july 22, 2021 at approximately 7:15 am pt, a marathon terminal 2 operator performing a routine facility inspection identified an active leak on an 8" appurtenance (nozzle) to tank 221. Tank 221 is an oily water tank inside of the tank farm of the marine terminal. The operator alerted company personnel and emergency activities were initiated immediately. Tank 221 was static at the time the leak was discovered, but operating systems (including pressure reliefs) tied to the tank were shutdown at approximately 7:30am. A temporary repair was implemented at approximately 8:00am on july 22, but the tank remained out of service to allow for a permanent repair to be coordinated and implemented. Impacted pipeline systems were restarted at 9:30am on july 22 once alternative operational plans were implemented. Tank 221 was then drained of liquid down to a level of 3.5 feet and a permanent repair was implemented on july 25, 2021 at 5pm. The tank was refilled and recommissioned the evening of july 26.
Detailed record list
Report Received Date
2021-08-19 00:00:00
Iyear
2021
Report Number
20210241
Supplemental Number
35652
Report Type
Original Final
Operator Id
Name
Marathon Pipe Line Llc
Operator Street Address
539 South Main Street
Operator City Name
Findlay
Operator State Abbreviation
OH
Operator Postal Code
45840
Local Datetime
2021-07-22 07:15:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.2
Recovered Bbls
0.2
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2021-07-22 07:15:00
System Part Involved
Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2021-07-22 07:30:00
Restart Datetime
2021-07-22 09:30:00
On Site Datetime
2021-07-22 07:20:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Long Beach Terminal 2
Segment Name
Tank 221 Nozzle
Onshore State Abbreviation
Ca
Onshore Postal Code
90813
Onshore City Name
Long Beach
Onshore County Name
Los Angeles
Designated Location
Milepost/valve Station
Designated Name
Facility
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Tank, Including Attached Appurtenances
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Tank/vessel
Tank Vessel Subtype
Appurtenance
Tank Type
Atmospheric
Api Std Out Of Service Year
2007
Api Std In Service Year
2018
Installation Year
1955
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
40000
Est Cost Emergency
1000
Est Cost Environmental
0
Est Cost Other
0
Prpty
41000
Accident Psig
12
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
< 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
There was no abnormal operation of the tank during the incident.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Localized Pitting
Int Water Acid Ind
Yes
Int Field Exam Basis Ind
Yes
Int Low Point Pipe Loc Ind
Yes
Corrosion Inhibitors
No
Corrosion Lining
No
Cleaning Dewatering
Not Applicable - Not Mainline Pipe
Corrosion Coupons
Not Applicable - Not Mainline Pipe
Preparer Name
A***** R*********
Preparer Title
Hes Professional
Preparer Email
A***********@m****************.com
Preparer Telephone
7148801713
Prepared Date
2021-08-19 00:00:00
Authorizer Name
A**** M*******
Authorizer Telephone
210-626-6343
Authorizer Title
Environmental Safety And Security Manager
Authorizer Email
A*********@m****************.com
Narrative
On july 22, 2021 at approximately 7:15 am pt, a marathon terminal 2 operator performing a routine facility inspection identified an active leak on an 8" appurtenance (nozzle) to tank 221. Tank 221 is an oily water tank inside of the tank farm of the marine terminal. The operator alerted company personnel and emergency activities were initiated immediately. Tank 221 was static at the time the leak was discovered, but operating systems (including pressure reliefs) tied to the tank were shutdown at approximately 7:30am. A temporary repair was implemented at approximately 8:00am on july 22, but the tank remained out of service to allow for a permanent repair to be coordinated and implemented. Impacted pipeline systems were restarted at 9:30am on july 22 once alternative operational plans were implemented. Tank 221 was then drained of liquid down to a level of 3.5 feet and a permanent repair was implemented on july 25, 2021 at 5pm. The tank was refilled and recommissioned the evening of july 26.
Report Received Date 2021-08-19 00:00:00
Iyear 2021
Report Number 20210241
Supplemental Number 35652
Report Type Original Final
Operator Id 32147 PHMSA Enforcement
Name Marathon Pipe Line Llc
Operator Street Address 539 South Main Street
Operator City Name Findlay
Operator State Abbreviation OH
Operator Postal Code 45840
Local Datetime 2021-07-22 07:15:00
Location Latitude 33.77664 Google Maps OpenStreetMap
Location Longitude -118.2128 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.2
Recovered Bbls 0.2
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2021-07-22 07:15:00
System Part Involved Onshore Breakout Tank Or Storage Vessel, Including Attached Appurtenances
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2021-07-22 07:30:00
Restart Datetime 2021-07-22 09:30:00
On Site Datetime 2021-07-22 07:20:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Long Beach Terminal 2
Segment Name Tank 221 Nozzle
Onshore State Abbreviation Ca
Onshore Postal Code 90813
Onshore City Name Long Beach
Onshore County Name Los Angeles
Designated Location Milepost/valve Station
Designated Name Facility
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Tank, Including Attached Appurtenances
Crossing No
Pipe Facility Type Intrastate
Item Involved Tank/vessel
Tank Vessel Subtype Appurtenance
Tank Type Atmospheric
Api Std Out Of Service Year 2007
Api Std In Service Year 2018
Installation Year 1955
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 40000
Est Cost Emergency 1000
Est Cost Environmental 0
Est Cost Other 0
Prpty 41000
Accident Psig 12
Mop Psig 275
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function < 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details There was no abnormal operation of the tank during the incident.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results Localized Pitting
Int Water Acid Ind Yes
Int Field Exam Basis Ind Yes
Int Low Point Pipe Loc Ind Yes
Corrosion Inhibitors No
Corrosion Lining No
Cleaning Dewatering Not Applicable - Not Mainline Pipe
Corrosion Coupons Not Applicable - Not Mainline Pipe
Preparer Name A***** R*********
Preparer Title Hes Professional
Preparer Email A***********@m****************.com
Preparer Telephone 7148801713
Prepared Date 2021-08-19 00:00:00
Authorizer Name A**** M*******
Authorizer Telephone 210-626-6343
Authorizer Title Environmental Safety And Security Manager
Authorizer Email A*********@m****************.com
Narrative On july 22, 2021 at approximately 7:15 am pt, a marathon terminal 2 operator performing a routine facility inspection identified an active leak on an 8" appurtenance (nozzle) to tank 221. Tank 221 is an oily water tank inside of the tank farm of the marine terminal. The operator alerted company personnel and emergency activities were initiated immediately. Tank 221 was static at the time the leak was discovered, but operating systems (including pressure reliefs) tied to the tank were shutdown at approximately 7:30am. A temporary repair was implemented at approximately 8:00am on july 22, but the tank remained out of service to allow for a permanent repair to be coordinated and implemented. Impacted pipeline systems were restarted at 9:30am on july 22 once alternative operational plans were implemented. Tank 221 was then drained of liquid down to a level of 3.5 feet and a permanent repair was implemented on july 25, 2021 at 5pm. The tank was refilled and recommissioned the evening of july 26.

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