Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2021-07-07 — OK
Operator
Magellan Terminals Holdings, Lp
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$500
Incident datetime
2021-07-07 10:45
Report number
Location
OK
Narrative
At 10:45 on 7/7/2021, magellan operations personnel identified transmix near the a-yard manifold sample sink. The line was isolated and cleanup activities were initiated. Upon further investigation it was determined the sample sink check valve failed to close due to debris and allowed product to release through the sink. The line was flushed and the check valve was replaced before placing the sample sink back in service.
Detailed record list
Report Received Date
2021-08-06 00:00:00
Iyear
2021
Report Number
20210224
Supplemental Number
35586
Report Type
Original Final
Operator Id
31580
Name
Magellan Terminals Holdings, Lp
Operator Street Address
100 West 5th Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2021-07-07 10:45:00
Location Latitude
29.743857
Location Longitude
-95.200509
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Mixture Of Refined Products (Transmix Or Other Mixture)
Unintentional Release Bbls
2
Recovered Bbls
2
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2021-07-07 10:45:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
The Release Was Isolated From All Mainline Movements.
On Site Datetime
2021-07-07 10:45:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Galena Park
Segment Name
Fac Id 474
Onshore State Abbreviation
Tx
Onshore Postal Code
77547
Onshore City Name
Galena Park
Onshore County Name
Harris
Designated Location
Milepost/valve Station
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Installation Year
2008
Material Involved
Carbon Steel
Release Type
Other
Release Type Details
Check Valve Hung Open
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
500
Est Cost Emergency
500
Est Cost Environmental
0
Est Cost Other
0
Prpty
1000
Accident Psig
100
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The release volume was below detectable thresholds.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Malfunction Of Control/relief Equipment
Eq Failure Type
Malfunction Of Control/relief Equipment
Check Valve Ind
Yes
Eq Additional Other Ind
Yes
Eq Additional Other Details
Valve Hung Open Due To Debris
Preparer Name
S****** L******
Preparer Title
Ai Analyst
Preparer Email
S**************@m*********.com
Preparer Telephone
918-574-7327
Preparer Fax
918-574-7376
Prepared Date
2021-08-06 00:00:00
Authorizer Name
G**** R****
Authorizer Telephone
918-574-7165
Authorizer Title
Supervisor Integrity Management
Authorizer Email
G**********@m*********.com
Narrative
At 10:45 on 7/7/2021, magellan operations personnel identified transmix near the a-yard manifold sample sink. The line was isolated and cleanup activities were initiated. Upon further investigation it was determined the sample sink check valve failed to close due to debris and allowed product to release through the sink. The line was flushed and the check valve was replaced before placing the sample sink back in service.
| Report Received Date | 2021-08-06 00:00:00 |
|---|---|
| Iyear | 2021 |
| Report Number | 20210224 |
| Supplemental Number | 35586 |
| Report Type | Original Final |
| Operator Id | 31580 PHMSA Enforcement |
| Name | Magellan Terminals Holdings, Lp |
| Operator Street Address | 100 West 5th Street |
| Operator City Name | Tulsa |
| Operator State Abbreviation | OK |
| Operator Postal Code | 74103 |
| Local Datetime | 2021-07-07 10:45:00 |
| Location Latitude | 29.743857 Google Maps OpenStreetMap |
| Location Longitude | -95.200509 Google Maps OpenStreetMap |
| Commodity Released Type | Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions |
| Commodity Subtype | Mixture Of Refined Products (Transmix Or Other Mixture) |
| Unintentional Release Bbls | 2 |
| Recovered Bbls | 2 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Accident Identifier | Local Operating Personnel, Including Contractors |
| Operator Type | Operator Employee |
| Incident Identified Datetime | 2021-07-07 10:45:00 |
| System Part Involved | Onshore Terminal/tank Farm Equipment And Piping |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | No |
| Shutdown Explain | The Release Was Isolated From All Mainline Movements. |
| On Site Datetime | 2021-07-07 10:45:00 |
| Nrc Rpt Num | Nrc Notification Not Required NRC Report How to search |
| Ignite Ind | No |
| Explode Ind | No |
| Num Pub Evacuated | 0 |
| Pipe Fac Name | Galena Park |
| Segment Name | Fac Id 474 |
| Onshore State Abbreviation | Tx |
| Onshore Postal Code | 77547 |
| Onshore City Name | Galena Park |
| Onshore County Name | Harris |
| Designated Location | Milepost/valve Station |
| Designated Name | 0 |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Aboveground |
| Incident Area Subtype | Typical Aboveground Facility Piping Or Appurtenance |
| Crossing | No |
| Pipe Facility Type | Intrastate |
| Item Involved | Valve |
| Valve Type | Auxiliary Or Other Valve |
| Installation Year | 2008 |
| Material Involved | Carbon Steel |
| Release Type | Other |
| Release Type Details | Check Valve Hung Open |
| Wildlife Impact Ind | No |
| Soil Contamination | Yes |
| Long Term Assessment | No |
| Remediation Ind | No |
| Water Contam Ind | No |
| Could Be Hca | Yes |
| Commodity Reached Hca | Yes |
| High Pop Ind | Yes |
| High Pop Yes No | Yes |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 0 |
| Est Cost Prop Damage | 500 |
| Est Cost Emergency | 500 |
| Est Cost Environmental | 0 |
| Est Cost Other | 0 |
| Prpty | 1000 |
| Accident Psig | 100 |
| Mop Psig | 275 |
| Accident Pressure | Pressure Did Not Exceed Mop |
| Pressure Restriction Ind | No |
| Pipeline Function | > 20% Smys Regulated Transmission |
| Scada In Place Ind | No |
| Cpm In Place Ind | No |
| Investigation Status | No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate) |
| Investigation Status Details | The release volume was below detectable thresholds. |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Equipment Failure |
| Cause Details | Malfunction Of Control/relief Equipment |
| Eq Failure Type | Malfunction Of Control/relief Equipment |
| Check Valve Ind | Yes |
| Eq Additional Other Ind | Yes |
| Eq Additional Other Details | Valve Hung Open Due To Debris |
| Preparer Name | S****** L****** |
| Preparer Title | Ai Analyst |
| Preparer Email | S**************@m*********.com |
| Preparer Telephone | 918-574-7327 |
| Preparer Fax | 918-574-7376 |
| Prepared Date | 2021-08-06 00:00:00 |
| Authorizer Name | G**** R**** |
| Authorizer Telephone | 918-574-7165 |
| Authorizer Title | Supervisor Integrity Management |
| Authorizer Email | G**********@m*********.com |
| Narrative | At 10:45 on 7/7/2021, magellan operations personnel identified transmix near the a-yard manifold sample sink. The line was isolated and cleanup activities were initiated. Upon further investigation it was determined the sample sink check valve failed to close due to debris and allowed product to release through the sink. The line was flushed and the check valve was replaced before placing the sample sink back in service. |
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