HL incident on 2021-07-07 — OK

Operator
Magellan Terminals Holdings, Lp
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$500
Incident datetime
2021-07-07 10:45
Report number
Location
OK
Narrative
At 10:45 on 7/7/2021, magellan operations personnel identified transmix near the a-yard manifold sample sink. The line was isolated and cleanup activities were initiated. Upon further investigation it was determined the sample sink check valve failed to close due to debris and allowed product to release through the sink. The line was flushed and the check valve was replaced before placing the sample sink back in service.
Detailed record list
Report Received Date
2021-08-06 00:00:00
Iyear
2021
Report Number
20210224
Supplemental Number
35586
Report Type
Original Final
Operator Id
Name
Magellan Terminals Holdings, Lp
Operator Street Address
100 West 5th Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2021-07-07 10:45:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Mixture Of Refined Products (Transmix Or Other Mixture)
Unintentional Release Bbls
2
Recovered Bbls
2
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2021-07-07 10:45:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
The Release Was Isolated From All Mainline Movements.
On Site Datetime
2021-07-07 10:45:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Galena Park
Segment Name
Fac Id 474
Onshore State Abbreviation
Tx
Onshore Postal Code
77547
Onshore City Name
Galena Park
Onshore County Name
Harris
Designated Location
Milepost/valve Station
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Installation Year
2008
Material Involved
Carbon Steel
Release Type
Other
Release Type Details
Check Valve Hung Open
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
500
Est Cost Emergency
500
Est Cost Environmental
0
Est Cost Other
0
Prpty
1000
Accident Psig
100
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The release volume was below detectable thresholds.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Malfunction Of Control/relief Equipment
Eq Failure Type
Malfunction Of Control/relief Equipment
Check Valve Ind
Yes
Eq Additional Other Ind
Yes
Eq Additional Other Details
Valve Hung Open Due To Debris
Preparer Name
S****** L******
Preparer Title
Ai Analyst
Preparer Email
S**************@m*********.com
Preparer Telephone
918-574-7327
Preparer Fax
918-574-7376
Prepared Date
2021-08-06 00:00:00
Authorizer Name
G**** R****
Authorizer Telephone
918-574-7165
Authorizer Title
Supervisor Integrity Management
Authorizer Email
G**********@m*********.com
Narrative
At 10:45 on 7/7/2021, magellan operations personnel identified transmix near the a-yard manifold sample sink. The line was isolated and cleanup activities were initiated. Upon further investigation it was determined the sample sink check valve failed to close due to debris and allowed product to release through the sink. The line was flushed and the check valve was replaced before placing the sample sink back in service.
Report Received Date 2021-08-06 00:00:00
Iyear 2021
Report Number 20210224
Supplemental Number 35586
Report Type Original Final
Operator Id 31580 PHMSA Enforcement
Name Magellan Terminals Holdings, Lp
Operator Street Address 100 West 5th Street
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74103
Local Datetime 2021-07-07 10:45:00
Location Latitude 29.743857 Google Maps OpenStreetMap
Location Longitude -95.200509 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Mixture Of Refined Products (Transmix Or Other Mixture)
Unintentional Release Bbls 2
Recovered Bbls 2
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2021-07-07 10:45:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain The Release Was Isolated From All Mainline Movements.
On Site Datetime 2021-07-07 10:45:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Galena Park
Segment Name Fac Id 474
Onshore State Abbreviation Tx
Onshore Postal Code 77547
Onshore City Name Galena Park
Onshore County Name Harris
Designated Location Milepost/valve Station
Designated Name 0
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Installation Year 2008
Material Involved Carbon Steel
Release Type Other
Release Type Details Check Valve Hung Open
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 500
Est Cost Emergency 500
Est Cost Environmental 0
Est Cost Other 0
Prpty 1000
Accident Psig 100
Mop Psig 275
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The release volume was below detectable thresholds.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Malfunction Of Control/relief Equipment
Eq Failure Type Malfunction Of Control/relief Equipment
Check Valve Ind Yes
Eq Additional Other Ind Yes
Eq Additional Other Details Valve Hung Open Due To Debris
Preparer Name S****** L******
Preparer Title Ai Analyst
Preparer Email S**************@m*********.com
Preparer Telephone 918-574-7327
Preparer Fax 918-574-7376
Prepared Date 2021-08-06 00:00:00
Authorizer Name G**** R****
Authorizer Telephone 918-574-7165
Authorizer Title Supervisor Integrity Management
Authorizer Email G**********@m*********.com
Narrative At 10:45 on 7/7/2021, magellan operations personnel identified transmix near the a-yard manifold sample sink. The line was isolated and cleanup activities were initiated. Upon further investigation it was determined the sample sink check valve failed to close due to debris and allowed product to release through the sink. The line was flushed and the check valve was replaced before placing the sample sink back in service.

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