HL incident on 2021-06-21 — OK

Operator
Williams Field Services
Cause
Natural Force Damage
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$5,000
Incident datetime
2021-06-21 21:30
Report number
Location
OK
Narrative
Operations technician received a notification from pipeline control that mlv 8 had closed. As tech approached valve set he noticed a fire around the actuator. Operations technician then returned to entrance of access road to make notification. Once a supervisor was on scene they proceeded to walk back in to mlv and discovered at time the fire had self extinguished. They then proceed to investigate and identified the leak was coming from a 3/8 tubing sensing line. They isolated the tubing and stopped the leak. The 3/8" tubing line was replaced. Asset integrity and engineering services reviewed the incident. Among other analysis and considerations, a hardness test was performed on the valve to indicate whether the valve had sustained damage. It was determined the valve was fit for service and was returned to normal operation.
Detailed record list
Report Received Date
2021-07-22 00:00:00
Iyear
2021
Report Number
20210213
Supplemental Number
36047
Report Type
Supplemental Final
Operator Id
Name
Williams Field Services
Operator Street Address
One Williams Center Wrc-3
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74172
Local Datetime
2021-06-21 21:30:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Other Hvl
Commodity Details
Ethane
Unintentional Release Bbls
10.8
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime
2021-06-21 21:30:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2021-06-21 22:02:00
Restart Datetime
2021-06-22 15:52:00
On Site Datetime
2021-06-21 21:30:00
Nrc Rpt Datetime
2021-06-22 09:47:00
Nrc Rpt Num
Ignite Ind
Yes
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Oak Grove To Houston Pa
Segment Name
92000
Onshore State Abbreviation
Pa
Onshore Postal Code
15232
Onshore City Name
Claysville
Onshore County Name
Washington
Designated Location
Milepost/valve Station
Designated Name
37
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Tubing
Installation Year
2013
Material Involved
Material Other Than Carbon Steel
Material Details
Stainless Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
206
Est Cost Prop Damage
5000
Est Cost Emergency
74000
Est Cost Environmental
0
Est Cost Other
0
Prpty
79206
Accident Psig
1100
Mop Psig
2160
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
8
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
No indications controllers actions contributed to the incident.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Natural Force Damage
Cause Details
Lightning
Natural Force Type
Lightning
Lightning Subtype
Secondary Impact Such As Resulting Nearby Fires
Nf Extreme Weather Ind
No
Preparer Name
T*** S*****
Preparer Title
Pipeline Safety Engineer
Preparer Email
T**********@w*******.com
Preparer Telephone
9183446359
Prepared Date
2021-11-29 00:00:00
Authorizer Name
C**** R****
Authorizer Telephone
4056261785
Authorizer Title
Manager Pipeline Safety
Authorizer Email
C**********@w*******.com
Narrative
Operations technician received a notification from pipeline control that mlv 8 had closed. As tech approached valve set he noticed a fire around the actuator. Operations technician then returned to entrance of access road to make notification. Once a supervisor was on scene they proceeded to walk back in to mlv and discovered at time the fire had self extinguished. They then proceed to investigate and identified the leak was coming from a 3/8 tubing sensing line. They isolated the tubing and stopped the leak. The 3/8" tubing line was replaced. Asset integrity and engineering services reviewed the incident. Among other analysis and considerations, a hardness test was performed on the valve to indicate whether the valve had sustained damage. It was determined the valve was fit for service and was returned to normal operation.
Report Received Date 2021-07-22 00:00:00
Iyear 2021
Report Number 20210213
Supplemental Number 36047
Report Type Supplemental Final
Operator Id 30826 PHMSA Enforcement
Name Williams Field Services
Operator Street Address One Williams Center Wrc-3
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74172
Local Datetime 2021-06-21 21:30:00
Location Latitude 40.154797 Google Maps OpenStreetMap
Location Longitude -80.3574 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Other Hvl
Commodity Details Ethane
Unintentional Release Bbls 10.8
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Cpm Leak Detection System Or Scada-Based Information (Such As Alarm(S), Alert(S), Event(S), And/or Volume Calculations)
Incident Identified Datetime 2021-06-21 21:30:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2021-06-21 22:02:00
Restart Datetime 2021-06-22 15:52:00
On Site Datetime 2021-06-21 21:30:00
Nrc Rpt Datetime 2021-06-22 09:47:00
Nrc Rpt Num 1308429 NRC Report How to search
Ignite Ind Yes
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Oak Grove To Houston Pa
Segment Name 92000
Onshore State Abbreviation Pa
Onshore Postal Code 15232
Onshore City Name Claysville
Onshore County Name Washington
Designated Location Milepost/valve Station
Designated Name 37
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Tubing
Installation Year 2013
Material Involved Material Other Than Carbon Steel
Material Details Stainless Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 206
Est Cost Prop Damage 5000
Est Cost Emergency 74000
Est Cost Environmental 0
Est Cost Other 0
Prpty 79206
Accident Psig 1100
Mop Psig 2160
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 8
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details No indications controllers actions contributed to the incident.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Natural Force Damage
Cause Details Lightning
Natural Force Type Lightning
Lightning Subtype Secondary Impact Such As Resulting Nearby Fires
Nf Extreme Weather Ind No
Preparer Name T*** S*****
Preparer Title Pipeline Safety Engineer
Preparer Email T**********@w*******.com
Preparer Telephone 9183446359
Prepared Date 2021-11-29 00:00:00
Authorizer Name C**** R****
Authorizer Telephone 4056261785
Authorizer Title Manager Pipeline Safety
Authorizer Email C**********@w*******.com
Narrative Operations technician received a notification from pipeline control that mlv 8 had closed. As tech approached valve set he noticed a fire around the actuator. Operations technician then returned to entrance of access road to make notification. Once a supervisor was on scene they proceeded to walk back in to mlv and discovered at time the fire had self extinguished. They then proceed to investigate and identified the leak was coming from a 3/8 tubing sensing line. They isolated the tubing and stopped the leak. The 3/8" tubing line was replaced. Asset integrity and engineering services reviewed the incident. Among other analysis and considerations, a hardness test was performed on the valve to indicate whether the valve had sustained damage. It was determined the valve was fit for service and was returned to normal operation.

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