HL incident on 2021-06-09 — PA

Operator
Buckeye Partners, Lp
Cause
Natural Force Damage
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$4,529
Incident datetime
2021-06-09 18:32
Report number
Location
PA
Narrative
On the evening of june 9, 2021 the employee at buckeye's east chicago west terminal discovered a flange misting ulsd on the eg999kg line shortly after a routine transfer. There was an insulating gasket recently installed next to a flange where the release occurred. Shortly after the gasket was installed, this location started having significant increases in temperatures with thermal growth which is suspected as the cause of this release. An estimate of 10 gallons of product was released, the transfer was shutdown, and product was cleaned up immediately by buckeye and assistance from osro. Internal notifications were made and this release did not meet the criteria of nrc immediate notification requirements .
Detailed record list
Report Received Date
2021-07-09 00:00:00
Iyear
2021
Report Number
20210198
Supplemental Number
35669
Report Type
Supplemental Final
Operator Id
Name
Buckeye Partners, Lp
Operator Street Address
The Buckeye Building 6161 Hamilton Boulevar
Operator City Name
Allentown
Operator State Abbreviation
PA
Operator Postal Code
18106
Local Datetime
2021-06-10 12:43:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
0.25
Recovered Bbls
0.25
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2021-06-09 18:32:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2021-06-09 20:00:00
Restart Datetime
2021-06-10 12:00:00
On Site Datetime
2021-06-09 18:32:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Automatic
Downstream Valve Type Ind
Automatic
Num Pub Evacuated
0
Pipe Fac Name
East Chicago Terminal
Segment Name
Eg999kg
Onshore State Abbreviation
In
Onshore Postal Code
46312
Onshore City Name
East Chicago
Onshore County Name
Lake
Designated Location
Milepost/valve Station
Designated Name
3+70
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Other
Item Involved Details
Gasket
Installation Year
2021
Material Involved
Material Other Than Carbon Steel
Material Details
Gasket
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
4529
Est Cost Emergency
11005
Est Cost Environmental
0
Est Cost Other
0
Prpty
15534
Accident Psig
220
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
1350
Internal Inspection Ind
No
Tight Mitered Ind
Yes
Operation Complications Ind
Yes
Low Op Pressure Ind
Yes
Pipeline Function
< 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The controller had no involvement in this release
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Natural Force Damage
Cause Details
Temperature
Natural Force Type
Temperature
Temperature Subtype
Thermal Stress
Nf Extreme Weather Ind
No
Preparer Name
J**** P*****
Preparer Title
Regional Compliance Specialist Ii
Preparer Email
J*******@b******.com
Preparer Telephone
219-796-8225
Prepared Date
2021-08-26 00:00:00
Authorizer Name
C****** P********
Authorizer Telephone
610-904-4113
Authorizer Title
Director Of Regulatory Compliance
Authorizer Email
C*********@b******.com
Narrative
On the evening of june 9, 2021 the employee at buckeye's east chicago west terminal discovered a flange misting ulsd on the eg999kg line shortly after a routine transfer. There was an insulating gasket recently installed next to a flange where the release occurred. Shortly after the gasket was installed, this location started having significant increases in temperatures with thermal growth which is suspected as the cause of this release. An estimate of 10 gallons of product was released, the transfer was shutdown, and product was cleaned up immediately by buckeye and assistance from osro. Internal notifications were made and this release did not meet the criteria of nrc immediate notification requirements .
Report Received Date 2021-07-09 00:00:00
Iyear 2021
Report Number 20210198
Supplemental Number 35669
Report Type Supplemental Final
Operator Id 1845 PHMSA Enforcement
Name Buckeye Partners, Lp
Operator Street Address The Buckeye Building 6161 Hamilton Boulevar
Operator City Name Allentown
Operator State Abbreviation PA
Operator Postal Code 18106
Local Datetime 2021-06-10 12:43:00
Location Latitude 41.64338 Google Maps OpenStreetMap
Location Longitude -87.477898 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls 0.25
Recovered Bbls 0.25
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2021-06-09 18:32:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2021-06-09 20:00:00
Restart Datetime 2021-06-10 12:00:00
On Site Datetime 2021-06-09 18:32:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Automatic
Downstream Valve Type Ind Automatic
Num Pub Evacuated 0
Pipe Fac Name East Chicago Terminal
Segment Name Eg999kg
Onshore State Abbreviation In
Onshore Postal Code 46312
Onshore City Name East Chicago
Onshore County Name Lake
Designated Location Milepost/valve Station
Designated Name 3+70
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Other
Item Involved Details Gasket
Installation Year 2021
Material Involved Material Other Than Carbon Steel
Material Details Gasket
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 4529
Est Cost Emergency 11005
Est Cost Environmental 0
Est Cost Other 0
Prpty 15534
Accident Psig 220
Mop Psig 275
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 1350
Internal Inspection Ind No
Tight Mitered Ind Yes
Operation Complications Ind Yes
Low Op Pressure Ind Yes
Pipeline Function < 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The controller had no involvement in this release
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Natural Force Damage
Cause Details Temperature
Natural Force Type Temperature
Temperature Subtype Thermal Stress
Nf Extreme Weather Ind No
Preparer Name J**** P*****
Preparer Title Regional Compliance Specialist Ii
Preparer Email J*******@b******.com
Preparer Telephone 219-796-8225
Prepared Date 2021-08-26 00:00:00
Authorizer Name C****** P********
Authorizer Telephone 610-904-4113
Authorizer Title Director Of Regulatory Compliance
Authorizer Email C*********@b******.com
Narrative On the evening of june 9, 2021 the employee at buckeye's east chicago west terminal discovered a flange misting ulsd on the eg999kg line shortly after a routine transfer. There was an insulating gasket recently installed next to a flange where the release occurred. Shortly after the gasket was installed, this location started having significant increases in temperatures with thermal growth which is suspected as the cause of this release. An estimate of 10 gallons of product was released, the transfer was shutdown, and product was cleaned up immediately by buckeye and assistance from osro. Internal notifications were made and this release did not meet the criteria of nrc immediate notification requirements .

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