HL incident on 2021-05-20 — OK

Operator
Magellan Crude Oil Pipeline Company, L.p.
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$25,000
Incident datetime
2021-05-20 07:25
Report number
Location
OK
Narrative
At 7:25 on 5/20/21 magellan operations personnel were conducting a daily facility inspection when product was noticed in the tank 3512 containment area. The area was isolated and cleanup activities were initiated. Upon further investigation it was determined that the packing on the booster pump bypass valve had failed due to normal wear and was allowing product to leak by. The valve will be repacked and the stem replaced before it is placed back in service.
Detailed record list
Report Received Date
2021-06-18 00:00:00
Iyear
2021
Report Number
20210178
Supplemental Number
35409
Report Type
Original Final
Operator Id
Name
Magellan Crude Oil Pipeline Company, L.p.
Operator Street Address
100 West 5th Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2021-05-20 07:25:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.95
Recovered Bbls
0.95
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2021-05-20 07:25:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
The Tank Was Isolated From The System.
On Site Datetime
2021-05-20 07:25:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
East Houston Terminal
Segment Name
Fac Id 728
Onshore State Abbreviation
Tx
Onshore Postal Code
77029
Onshore City Name
Houston
Onshore County Name
Harris
Designated Location
Milepost/valve Station
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Mainline
Valve Mainline Type
Gate
Valve Manufacturer
Spx
Installation Year
2014
Manufactured Year
2014
Material Involved
Material Other Than Carbon Steel
Material Details
Valve Packing
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
60
Est Cost Prop Damage
25000
Est Cost Emergency
1000
Est Cost Environmental
0
Est Cost Other
0
Prpty
26060
Accident Psig
100
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The release was contained within the facility on piping not monitored by ops control.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
Seal (Not Pump Seal) Or Packing
Eq Additional Other Ind
Yes
Eq Additional Other Details
Normal Wear
Preparer Name
S****** L******
Preparer Title
Ai Analyst
Preparer Email
S**************@m*********.com
Preparer Telephone
918-574-7327
Preparer Fax
918-5747376
Prepared Date
2021-06-18 00:00:00
Authorizer Name
G**** R****
Authorizer Telephone
918- 574-7165
Authorizer Title
Supervisor Integrity Management
Authorizer Email
G**********@m*********.com
Narrative
At 7:25 on 5/20/21 magellan operations personnel were conducting a daily facility inspection when product was noticed in the tank 3512 containment area. The area was isolated and cleanup activities were initiated. Upon further investigation it was determined that the packing on the booster pump bypass valve had failed due to normal wear and was allowing product to leak by. The valve will be repacked and the stem replaced before it is placed back in service.
Report Received Date 2021-06-18 00:00:00
Iyear 2021
Report Number 20210178
Supplemental Number 35409
Report Type Original Final
Operator Id 39504 PHMSA Enforcement
Name Magellan Crude Oil Pipeline Company, L.p.
Operator Street Address 100 West 5th Street
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74103
Local Datetime 2021-05-20 07:25:00
Location Latitude 29.797146 Google Maps OpenStreetMap
Location Longitude -95.279005 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.95
Recovered Bbls 0.95
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2021-05-20 07:25:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain The Tank Was Isolated From The System.
On Site Datetime 2021-05-20 07:25:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name East Houston Terminal
Segment Name Fac Id 728
Onshore State Abbreviation Tx
Onshore Postal Code 77029
Onshore City Name Houston
Onshore County Name Harris
Designated Location Milepost/valve Station
Designated Name 0
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Mainline
Valve Mainline Type Gate
Valve Manufacturer Spx
Installation Year 2014
Manufactured Year 2014
Material Involved Material Other Than Carbon Steel
Material Details Valve Packing
Release Type Leak
Leak Type Seal Or Packing
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 60
Est Cost Prop Damage 25000
Est Cost Emergency 1000
Est Cost Environmental 0
Est Cost Other 0
Prpty 26060
Accident Psig 100
Mop Psig 275
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The release was contained within the facility on piping not monitored by ops control.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Non-Threaded Connection Failure
Eq Failure Type Non-Threaded Connection Failure
Other Non Threaded Ind Seal (Not Pump Seal) Or Packing
Eq Additional Other Ind Yes
Eq Additional Other Details Normal Wear
Preparer Name S****** L******
Preparer Title Ai Analyst
Preparer Email S**************@m*********.com
Preparer Telephone 918-574-7327
Preparer Fax 918-5747376
Prepared Date 2021-06-18 00:00:00
Authorizer Name G**** R****
Authorizer Telephone 918- 574-7165
Authorizer Title Supervisor Integrity Management
Authorizer Email G**********@m*********.com
Narrative At 7:25 on 5/20/21 magellan operations personnel were conducting a daily facility inspection when product was noticed in the tank 3512 containment area. The area was isolated and cleanup activities were initiated. Upon further investigation it was determined that the packing on the booster pump bypass valve had failed due to normal wear and was allowing product to leak by. The valve will be repacked and the stem replaced before it is placed back in service.

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