HL incident on 2021-05-18 — NJ

Operator
Torrance Pipeline Company Llc
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$29,537
Incident datetime
2021-05-18 10:16
Report number
Location
NJ
Narrative
On may 18, 2021, at approximately 1016 hrs. Pdt, a torrance pipeline company (tpc) operator conducting facility rounds arrived at eptc meter station. Upon arrival, the operator discovered crude oil product on the ground inside the facility. The operator immediately contacted his supervisor; tpc supervisor arrived on site at approximately 1033 hrs. Pdt. Cleanup and recovery crew were dispatched to the facility to commence response efforts. Initial estimates approximately 1 barrel of crude oil to soil. Internal and external notifications were promptly made. On may 18, 2021, at 1042 hrs. Pdt, cal oes was notified - control number #21-2652. At approximately 1052 hrs. Pdt, nrc was notified - report #1305340. On may 20, 2021, a 48-hour report to nrc was made - report #1305563; no changes to report at that time. The source of the release, a two-inch thermal relief line with a through wall pinhole at the 6 oclock position was located and secured as ongoing cleanup was performed. The thermal relief line was replaced and permanently repaired. An investigation is underway to determine the cause of the release; a supplemental report will be submitted. ________________________________________________________________________________________________________________________ supplemental / final report updates: updated part d, items 8a-8g updated part g1, ic, items 6-13 updated part h, narrative description of the accident: torrance pipeline company has concluded its investigation and has identified the cause of the release. As initially reported at the 6 oclock position, a through wall pinhole was identified. Based on visual field examination and non-destructive flexoform phased array and conventional ultrasonic evaluation, it has been confirmed to be an isolated internal corrosion pit. Initial mitigative action was to replace the failed two-inch thermal relief line with a new two-inch thermal relief line. Additional mitigative actions include implementation of weekly operator/line rider facility visits and inspections inside all remote meter station sites. Future potential implementations include development of a facility integrity inspection standard in addition to evaluating remote meter/pump stations and prioritizing future facility integrity inspections of deadleg, no flow or low flow piping. This concludes the investigation and actions taken for this incident.
Detailed record list
Report Received Date
2021-06-17 00:00:00
Iyear
2021
Report Number
20210177
Supplemental Number
35811
Report Type
Supplemental Final
Operator Id
Name
Torrance Pipeline Company Llc
Operator Street Address
One Sylvan Way Second Floor
Operator City Name
Parsippany
Operator State Abbreviation
NJ
Operator Postal Code
07054
Local Datetime
2021-05-18 10:33:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
1
Recovered Bbls
1
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Ground Patrol By Operator Or Its Contractor
Operator Type
Operator Employee
Incident Identified Datetime
2021-05-18 10:16:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
This Lateral Segment Was Not In Operation At The Time Of Discovery
On Site Datetime
2021-05-18 10:16:00
Nrc Rpt Datetime
2021-05-18 10:52:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Eptc Meter
Segment Name
M-146b Lateral
Onshore State Abbreviation
Ca
Onshore Postal Code
90745
Onshore City Name
Carson
Onshore County Name
Los Angeles
Designated Location
Survey Station No.
Designated Name
0+68
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Relief Line And Relief Equipment
Installation Year
2000
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
68
Est Cost Prop Damage
29537
Est Cost Emergency
49606
Est Cost Environmental
0
Est Cost Other
0
Est Cost Other Details
Corrected $68 From 8a To 8b.
Prpty
79211
Accident Psig
137
Mop Psig
393
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The pipeline was down and not shipping when discovery of the release was made.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Other
Int Visual Exam Details
Isolated Internal Corrosion Pit
Int Other Corrosion Ind
Yes
Int Corrosion Type Details
Isolated Internal Corrosion Pit
Int Field Exam Basis Ind
Yes
Int Low Point Pipe Loc Ind
Yes
Corrosion Inhibitors
No
Corrosion Lining
No
Cleaning Dewatering
No
Corrosion Coupons
No
Preparer Name
A****** G*****
Preparer Title
Regulatory Compliance Specialist
Preparer Email
A*************@p********.com
Preparer Telephone
310-212-1764
Prepared Date
2021-09-23 00:00:00
Authorizer Name
T***** M*****
Authorizer Telephone
281-602-4424
Authorizer Title
Director Regulatory Compliance
Authorizer Email
T************@p********.com
Narrative
On may 18, 2021, at approximately 1016 hrs. Pdt, a torrance pipeline company (tpc) operator conducting facility rounds arrived at eptc meter station. Upon arrival, the operator discovered crude oil product on the ground inside the facility. The operator immediately contacted his supervisor; tpc supervisor arrived on site at approximately 1033 hrs. Pdt. Cleanup and recovery crew were dispatched to the facility to commence response efforts. Initial estimates approximately 1 barrel of crude oil to soil. Internal and external notifications were promptly made. On may 18, 2021, at 1042 hrs. Pdt, cal oes was notified - control number #21-2652. At approximately 1052 hrs. Pdt, nrc was notified - report #1305340. On may 20, 2021, a 48-hour report to nrc was made - report #1305563; no changes to report at that time. The source of the release, a two-inch thermal relief line with a through wall pinhole at the 6 oclock position was located and secured as ongoing cleanup was performed. The thermal relief line was replaced and permanently repaired. An investigation is underway to determine the cause of the release; a supplemental report will be submitted. ________________________________________________________________________________________________________________________ supplemental / final report updates: updated part d, items 8a-8g updated part g1, ic, items 6-13 updated part h, narrative description of the accident: torrance pipeline company has concluded its investigation and has identified the cause of the release. As initially reported at the 6 oclock position, a through wall pinhole was identified. Based on visual field examination and non-destructive flexoform phased array and conventional ultrasonic evaluation, it has been confirmed to be an isolated internal corrosion pit. Initial mitigative action was to replace the failed two-inch thermal relief line with a new two-inch thermal relief line. Additional mitigative actions include implementation of weekly operator/line rider facility visits and inspections inside all remote meter station sites. Future potential implementations include development of a facility integrity inspection standard in addition to evaluating remote meter/pump stations and prioritizing future facility integrity inspections of deadleg, no flow or low flow piping. This concludes the investigation and actions taken for this incident.
Report Received Date 2021-06-17 00:00:00
Iyear 2021
Report Number 20210177
Supplemental Number 35811
Report Type Supplemental Final
Operator Id 39535 PHMSA Enforcement
Name Torrance Pipeline Company Llc
Operator Street Address One Sylvan Way Second Floor
Operator City Name Parsippany
Operator State Abbreviation NJ
Operator Postal Code 07054
Local Datetime 2021-05-18 10:33:00
Location Latitude 33.804229 Google Maps OpenStreetMap
Location Longitude -118.28371 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 1
Recovered Bbls 1
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Ground Patrol By Operator Or Its Contractor
Operator Type Operator Employee
Incident Identified Datetime 2021-05-18 10:16:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain This Lateral Segment Was Not In Operation At The Time Of Discovery
On Site Datetime 2021-05-18 10:16:00
Nrc Rpt Datetime 2021-05-18 10:52:00
Nrc Rpt Num 1305340 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Eptc Meter
Segment Name M-146b Lateral
Onshore State Abbreviation Ca
Onshore Postal Code 90745
Onshore City Name Carson
Onshore County Name Los Angeles
Designated Location Survey Station No.
Designated Name 0+68
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
Item Involved Relief Line And Relief Equipment
Installation Year 2000
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Usa Drinking Ind Yes
Usa Drinking Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 68
Est Cost Prop Damage 29537
Est Cost Emergency 49606
Est Cost Environmental 0
Est Cost Other 0
Est Cost Other Details Corrected $68 From 8a To 8b.
Prpty 79211
Accident Psig 137
Mop Psig 393
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The pipeline was down and not shipping when discovery of the release was made.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results Other
Int Visual Exam Details Isolated Internal Corrosion Pit
Int Other Corrosion Ind Yes
Int Corrosion Type Details Isolated Internal Corrosion Pit
Int Field Exam Basis Ind Yes
Int Low Point Pipe Loc Ind Yes
Corrosion Inhibitors No
Corrosion Lining No
Cleaning Dewatering No
Corrosion Coupons No
Preparer Name A****** G*****
Preparer Title Regulatory Compliance Specialist
Preparer Email A*************@p********.com
Preparer Telephone 310-212-1764
Prepared Date 2021-09-23 00:00:00
Authorizer Name T***** M*****
Authorizer Telephone 281-602-4424
Authorizer Title Director Regulatory Compliance
Authorizer Email T************@p********.com
Narrative On may 18, 2021, at approximately 1016 hrs. Pdt, a torrance pipeline company (tpc) operator conducting facility rounds arrived at eptc meter station. Upon arrival, the operator discovered crude oil product on the ground inside the facility. The operator immediately contacted his supervisor; tpc supervisor arrived on site at approximately 1033 hrs. Pdt. Cleanup and recovery crew were dispatched to the facility to commence response efforts. Initial estimates approximately 1 barrel of crude oil to soil. Internal and external notifications were promptly made. On may 18, 2021, at 1042 hrs. Pdt, cal oes was notified - control number #21-2652. At approximately 1052 hrs. Pdt, nrc was notified - report #1305340. On may 20, 2021, a 48-hour report to nrc was made - report #1305563; no changes to report at that time. The source of the release, a two-inch thermal relief line with a through wall pinhole at the 6 oclock position was located and secured as ongoing cleanup was performed. The thermal relief line was replaced and permanently repaired. An investigation is underway to determine the cause of the release; a supplemental report will be submitted. ________________________________________________________________________________________________________________________ supplemental / final report updates: updated part d, items 8a-8g updated part g1, ic, items 6-13 updated part h, narrative description of the accident: torrance pipeline company has concluded its investigation and has identified the cause of the release. As initially reported at the 6 oclock position, a through wall pinhole was identified. Based on visual field examination and non-destructive flexoform phased array and conventional ultrasonic evaluation, it has been confirmed to be an isolated internal corrosion pit. Initial mitigative action was to replace the failed two-inch thermal relief line with a new two-inch thermal relief line. Additional mitigative actions include implementation of weekly operator/line rider facility visits and inspections inside all remote meter station sites. Future potential implementations include development of a facility integrity inspection standard in addition to evaluating remote meter/pump stations and prioritizing future facility integrity inspections of deadleg, no flow or low flow piping. This concludes the investigation and actions taken for this incident.

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