HL incident on 2021-05-11 — MT

Operator
Cenex Pipeline Llc
Cause
Incorrect Operation
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2021-05-11 10:17
Report number
Location
MT
Narrative
During the field portion of a PHMSA integrated inspection on may 11, 2021, block valve 232 was found by cenex pipeline staff and the PHMSA inspector to be dripping a small volume of product from the body bleed valve. Controllers opened a downstream valve to bleed pressure/volume away from the site and oq qualified field staff tightened the bleed within minutes of arriving on-site to stop the leak. No repair was needed beyond tightening the bleed. Release estimate was based on volume of soil cleanup associated with the release. No leak alarms were received because the leak alarm thresholds were not met. Release was result of maintenance. Staff opened body bleed to drain valve. Upon completing maintenance, staff closed the body bleed but did not get it fully tightened, resulting in a small drip type of release.
Detailed record list
Report Received Date
2021-06-14 00:00:00
Iyear
2021
Report Number
20210172
Supplemental Number
35529
Report Type
Supplemental Final
Operator Id
Name
Cenex Pipeline Llc
Operator Street Address
803 Hwy 212 S (Po Box 909)
Operator City Name
Laurel
Operator State Abbreviation
MT
Operator Postal Code
59044
Local Datetime
2021-05-11 10:17:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
0.7
Recovered Bbls
0.7
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2021-05-11 10:17:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Pipeline Segment Was Not Operating At The Time Of The Release.
On Site Datetime
2021-05-11 10:17:00
Nrc Rpt Num
Nrc Notification Not Required
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Remotely Controlled
Downstream Valve Type Ind
Remotely Controlled
Num Pub Evacuated
0
Pipe Fac Name
Bv 232
Segment Name
New Rockford To Fargo
Onshore State Abbreviation
Nd
Onshore Postal Code
58004
Onshore City Name
Not Within A Municipality
Onshore County Name
Cass
Designated Location
Milepost/valve Station
Designated Name
Bv 232
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Mainline
Valve Mainline Type
Ball
Valve Manufacturer
Balon
Installation Year
2018
Manufactured Year
2018
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Other
Leak Type Other
Bv Body Bleed Valve
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
500
Est Cost Gas Released
100
Est Cost Prop Damage
0
Est Cost Emergency
15000
Est Cost Environmental
0
Est Cost Other
500
Est Cost Other Details
Phmsa Reporting And Data Collection Efforts.
Prpty
16100
Accident Psig
725
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
Unknown
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Small volume of product dripping from bleeder on valve body that was corrected by field staff within minutes of arriving on-site, as witnessed by a PHMSA inspector that was performing the field portion of an integrated inspection. Segment was shutdown at the time of the release and kept shutdown until the bleeder was tightened and stopped dripping product. Controller and field staff took appropriate actions when responding to the incident.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Other Incorrect Operation
Operation Type
Other Incorrect Operation
Operation Details
Valve Body Bleed Not Fully Tightened After Semi-Annual Routine Maintenance.
Related Failure Follow Ind
Yes
Category Type
Routine Maintenance
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
M******* S*****
Preparer Title
Manager Dot Compliacne
Preparer Email
M**************@c*****.com
Preparer Telephone
4066285293
Prepared Date
2021-07-21 00:00:00
Authorizer Name
G*** B****
Authorizer Telephone
4066285200
Authorizer Title
Vp Pipelines And Terminals
Authorizer Email
G*********@c*****.com
Narrative
During the field portion of a PHMSA integrated inspection on may 11, 2021, block valve 232 was found by cenex pipeline staff and the PHMSA inspector to be dripping a small volume of product from the body bleed valve. Controllers opened a downstream valve to bleed pressure/volume away from the site and oq qualified field staff tightened the bleed within minutes of arriving on-site to stop the leak. No repair was needed beyond tightening the bleed. Release estimate was based on volume of soil cleanup associated with the release. No leak alarms were received because the leak alarm thresholds were not met. Release was result of maintenance. Staff opened body bleed to drain valve. Upon completing maintenance, staff closed the body bleed but did not get it fully tightened, resulting in a small drip type of release.
Report Received Date 2021-06-14 00:00:00
Iyear 2021
Report Number 20210172
Supplemental Number 35529
Report Type Supplemental Final
Operator Id 2170 PHMSA Enforcement
Name Cenex Pipeline Llc
Operator Street Address 803 Hwy 212 S (Po Box 909)
Operator City Name Laurel
Operator State Abbreviation MT
Operator Postal Code 59044
Local Datetime 2021-05-11 10:17:00
Location Latitude 47.014696 Google Maps OpenStreetMap
Location Longitude -97.196908 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 0.7
Recovered Bbls 0.7
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2021-05-11 10:17:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Pipeline Segment Was Not Operating At The Time Of The Release.
On Site Datetime 2021-05-11 10:17:00
Nrc Rpt Num Nrc Notification Not Required NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Remotely Controlled
Downstream Valve Type Ind Remotely Controlled
Num Pub Evacuated 0
Pipe Fac Name Bv 232
Segment Name New Rockford To Fargo
Onshore State Abbreviation Nd
Onshore Postal Code 58004
Onshore City Name Not Within A Municipality
Onshore County Name Cass
Designated Location Milepost/valve Station
Designated Name Bv 232
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Mainline
Valve Mainline Type Ball
Valve Manufacturer Balon
Installation Year 2018
Manufactured Year 2018
Material Involved Carbon Steel
Release Type Leak
Leak Type Other
Leak Type Other Bv Body Bleed Valve
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 500
Est Cost Gas Released 100
Est Cost Prop Damage 0
Est Cost Emergency 15000
Est Cost Environmental 0
Est Cost Other 500
Est Cost Other Details Phmsa Reporting And Data Collection Efforts.
Prpty 16100
Accident Psig 725
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated Unknown
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Small volume of product dripping from bleeder on valve body that was corrected by field staff within minutes of arriving on-site, as witnessed by a PHMSA inspector that was performing the field portion of an integrated inspection. Segment was shutdown at the time of the release and kept shutdown until the bleeder was tightened and stopped dripping product. Controller and field staff took appropriate actions when responding to the incident.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Other Incorrect Operation
Operation Type Other Incorrect Operation
Operation Details Valve Body Bleed Not Fully Tightened After Semi-Annual Routine Maintenance.
Related Failure Follow Ind Yes
Category Type Routine Maintenance
Operator Qualification Ind Yes
Qualified Individuals Yes, They Were Qualified For The Task(S)
Preparer Name M******* S*****
Preparer Title Manager Dot Compliacne
Preparer Email M**************@c*****.com
Preparer Telephone 4066285293
Prepared Date 2021-07-21 00:00:00
Authorizer Name G*** B****
Authorizer Telephone 4066285200
Authorizer Title Vp Pipelines And Terminals
Authorizer Email G*********@c*****.com
Narrative During the field portion of a PHMSA integrated inspection on may 11, 2021, block valve 232 was found by cenex pipeline staff and the PHMSA inspector to be dripping a small volume of product from the body bleed valve. Controllers opened a downstream valve to bleed pressure/volume away from the site and oq qualified field staff tightened the bleed within minutes of arriving on-site to stop the leak. No repair was needed beyond tightening the bleed. Release estimate was based on volume of soil cleanup associated with the release. No leak alarms were received because the leak alarm thresholds were not met. Release was result of maintenance. Staff opened body bleed to drain valve. Upon completing maintenance, staff closed the body bleed but did not get it fully tightened, resulting in a small drip type of release.

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