HL incident on 2021-04-19 — PA

Operator
Buckeye Partners, Lp
Cause
Incorrect Operation
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2021-04-19 18:30
Report number
Location
PA
Narrative
On 4/19/2021 at approximately 1830 edt buckeye local operations was conducting a routine tank to tank transfer for rvp turnover. After the completion of the transfer, the temporary hose was disconnected prematurely prior to properly depressurizing it. This resulted in a 3 barrel release. The task was immediately shut down and all internal and external notifications were made. There were no injuries, no fires, and no evacuations. All product released was recovered and terminal returned to normal operations. The 48 hour PHMSA update was made through the nrc at 1343 est on 4/21/2021, report # 1301377.
Detailed record list
Report Received Date
2021-05-10 00:00:00
Iyear
2021
Report Number
20210144
Supplemental Number
35313
Report Type
Supplemental Final
Operator Id
Name
Buckeye Partners, Lp
Operator Street Address
The Buckeye Building 6161 Hamilton Boulevar
Operator City Name
Allentown
Operator State Abbreviation
PA
Operator Postal Code
18106
Local Datetime
2021-04-19 18:30:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
3
Recovered Bbls
3
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2021-04-19 18:30:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
This Was During A Tank To Tank Transfer
On Site Datetime
2021-04-19 18:30:00
Nrc Rpt Datetime
2021-04-19 20:26:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Raritan Bay Terminal
Segment Name
Raritan Bay Terminal Tank Farm
Onshore State Abbreviation
Nj
Onshore Postal Code
08861
Onshore City Name
Perth Amboy
Onshore County Name
Middlesex County
Designated Location
Milepost/valve Station
Designated Name
Brf Raritan B
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Auxiliary Piping (E.g. Drain Lines)
Installation Year
2021
Material Involved
Carbon Steel
Release Type
Other
Release Type Details
Temporary Pumping Operation To Strip Gasoline Tank Bottom To Another Tank.
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
0
Est Cost Emergency
12700
Est Cost Environmental
0
Est Cost Other
0
Prpty
12700
Accident Psig
100
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The temporary pumping equipment was connected to pump out tank bottom and transfer to other tank. This equipment does not have electronic monitoring available.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Other Incorrect Operation
Operation Type
Other Incorrect Operation
Operation Details
Tank Line Was Not Properly Depressurized Before Disconnected
Related Inadequate Proc Ind
Yes
Category Type
Routine Maintenance
Operator Qualification Ind
No
Preparer Name
D*** C*****
Preparer Title
Sr Regional Compliance Specialist
Preparer Email
D******@b******.com
Preparer Telephone
484-707-1426
Prepared Date
2021-05-21 00:00:00
Authorizer Name
C****** P********
Authorizer Telephone
610-904-4113
Authorizer Title
Director Regulatory Compliance
Authorizer Email
C*********@b******.com
Narrative
On 4/19/2021 at approximately 1830 edt buckeye local operations was conducting a routine tank to tank transfer for rvp turnover. After the completion of the transfer, the temporary hose was disconnected prematurely prior to properly depressurizing it. This resulted in a 3 barrel release. The task was immediately shut down and all internal and external notifications were made. There were no injuries, no fires, and no evacuations. All product released was recovered and terminal returned to normal operations. The 48 hour PHMSA update was made through the nrc at 1343 est on 4/21/2021, report # 1301377.
Report Received Date 2021-05-10 00:00:00
Iyear 2021
Report Number 20210144
Supplemental Number 35313
Report Type Supplemental Final
Operator Id 1845 PHMSA Enforcement
Name Buckeye Partners, Lp
Operator Street Address The Buckeye Building 6161 Hamilton Boulevar
Operator City Name Allentown
Operator State Abbreviation PA
Operator Postal Code 18106
Local Datetime 2021-04-19 18:30:00
Location Latitude 40.5121785 Google Maps OpenStreetMap
Location Longitude -74.2919789 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 3
Recovered Bbls 3
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2021-04-19 18:30:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain This Was During A Tank To Tank Transfer
On Site Datetime 2021-04-19 18:30:00
Nrc Rpt Datetime 2021-04-19 20:26:00
Nrc Rpt Num 1303062 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Raritan Bay Terminal
Segment Name Raritan Bay Terminal Tank Farm
Onshore State Abbreviation Nj
Onshore Postal Code 08861
Onshore City Name Perth Amboy
Onshore County Name Middlesex County
Designated Location Milepost/valve Station
Designated Name Brf Raritan B
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Auxiliary Piping (E.g. Drain Lines)
Installation Year 2021
Material Involved Carbon Steel
Release Type Other
Release Type Details Temporary Pumping Operation To Strip Gasoline Tank Bottom To Another Tank.
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Usa Drinking Ind Yes
Usa Drinking Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 0
Est Cost Emergency 12700
Est Cost Environmental 0
Est Cost Other 0
Prpty 12700
Accident Psig 100
Mop Psig 275
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The temporary pumping equipment was connected to pump out tank bottom and transfer to other tank. This equipment does not have electronic monitoring available.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Other Incorrect Operation
Operation Type Other Incorrect Operation
Operation Details Tank Line Was Not Properly Depressurized Before Disconnected
Related Inadequate Proc Ind Yes
Category Type Routine Maintenance
Operator Qualification Ind No
Preparer Name D*** C*****
Preparer Title Sr Regional Compliance Specialist
Preparer Email D******@b******.com
Preparer Telephone 484-707-1426
Prepared Date 2021-05-21 00:00:00
Authorizer Name C****** P********
Authorizer Telephone 610-904-4113
Authorizer Title Director Regulatory Compliance
Authorizer Email C*********@b******.com
Narrative On 4/19/2021 at approximately 1830 edt buckeye local operations was conducting a routine tank to tank transfer for rvp turnover. After the completion of the transfer, the temporary hose was disconnected prematurely prior to properly depressurizing it. This resulted in a 3 barrel release. The task was immediately shut down and all internal and external notifications were made. There were no injuries, no fires, and no evacuations. All product released was recovered and terminal returned to normal operations. The 48 hour PHMSA update was made through the nrc at 1343 est on 4/21/2021, report # 1301377.

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