HL incident on 2019-08-15 — TX

Operator
Panther Operating Company, Llc
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$130,000
Incident datetime
2019-08-15 15:45
Report number
Location
TX
Narrative
A pinhole leak was discovered on the high island pipeline system operated by panther operating company after the producer shut in both their inlet and outlet of their system into our line. When the line began pressuring up (still within maop), the leak was discovered. The leak is on a riser coming onto platform hi a563b. The leak was immediately clamped as a temporary repair, and then a permanent repair was made with the affected section of pipe replaced. All repair work completed on 9/3/2019. This report submission is intended to correct the report type submitted in 2019 in error. The original report # 20200032 - 33604 described the leak as a pinhole leak on a natural gas pipeline. The 2019 leak was on a liquid pipeline and the volume lost was <gallon.
Detailed record list
Report Received Date
2021-05-05 00:00:00
Iyear
2019
Report Number
20210141
Supplemental Number
36183
Report Type
Supplemental Final
Operator Id
Name
Panther Operating Company, Llc
Operator Street Address
Third Coast Midstream, Llc Po Box 1227
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77251
Local Datetime
2019-08-15 15:45:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.1
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2019-08-15 15:45:00
System Part Involved
Offshore Platform/deepwater Port, Including Platform-Mounted Equipment And Piping
On Off Shore
Offshore
Shutdown Due Accident Ind
No
Shutdown Explain
The Leak Was Minor And Allowed A Plidco Full Encirclement Clamp To Be Applied.
On Site Datetime
2019-08-15 17:00:00
Nrc Rpt Datetime
2019-08-15 15:45:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Off Water Depth
210
Off Accident Origin
On The Outer Continental Shelf (Ocs)
Off Ocs Area
Hi
Off Ocs Block
563
Off Area Accident Type
Below Water, Pipe Buried Or Jetted Below Seabed
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
24
Pipe Wall Thickness
0.5
Pipe Smys
52000
Pipe Specification
X 52
Pipe Seam Type
Erw - High Frequency
Pipe Manufacturer
Researching Original Pipeline Docs.
Pipe Coating Type
Other
Pipe Coating Details
Epoxy
Installation Year
Unknown
Manufactured Year
Unknown
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
Yes
Ocean Seawater Ind
Yes
Amount Released
0.1
Rel Water Name
Gulf Of Mexico
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
3
Est Cost Prop Damage
130000
Est Cost Emergency
50000
Est Cost Environmental
0
Est Cost Other
4025
Est Cost Other Details
Consulting Fees And Taxes
Prpty
184028
Accident Psig
2
Mop Psig
700
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
=< 20% Smys Regulated Gathering
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The controller was not involved in the incident cause, nor identification.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
External Corrosion
Internal External
External Corrosion
Visual Exam Results
Localized Pitting
Atmosphere Corrosion Ind
Yes
Field Exam Basis Ind
Yes
Underground Location
No
Externally Coated
Yes
Prior Damage
Yes
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
T*** R*****
Preparer Title
Sr. Manager Ehsr
Preparer Email
T******@3**********.com
Preparer Telephone
(346) 241-3663
Prepared Date
2021-12-20 00:00:00
Authorizer Name
T*** R*****
Authorizer Telephone
(346) 241-3663
Authorizer Title
Sr. Manager Ehsr
Authorizer Email
T******@3**********.com
Narrative
A pinhole leak was discovered on the high island pipeline system operated by panther operating company after the producer shut in both their inlet and outlet of their system into our line. When the line began pressuring up (still within maop), the leak was discovered. The leak is on a riser coming onto platform hi a563b. The leak was immediately clamped as a temporary repair, and then a permanent repair was made with the affected section of pipe replaced. All repair work completed on 9/3/2019. This report submission is intended to correct the report type submitted in 2019 in error. The original report # 20200032 - 33604 described the leak as a pinhole leak on a natural gas pipeline. The 2019 leak was on a liquid pipeline and the volume lost was <gallon.
Report Received Date 2021-05-05 00:00:00
Iyear 2019
Report Number 20210141
Supplemental Number 36183
Report Type Supplemental Final
Operator Id 31994 PHMSA Enforcement
Name Panther Operating Company, Llc
Operator Street Address Third Coast Midstream, Llc Po Box 1227
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77251
Local Datetime 2019-08-15 15:45:00
Location Latitude 27.964052 Google Maps OpenStreetMap
Location Longitude -94.388912 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.1
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2019-08-15 15:45:00
System Part Involved Offshore Platform/deepwater Port, Including Platform-Mounted Equipment And Piping
On Off Shore Offshore
Shutdown Due Accident Ind No
Shutdown Explain The Leak Was Minor And Allowed A Plidco Full Encirclement Clamp To Be Applied.
On Site Datetime 2019-08-15 17:00:00
Nrc Rpt Datetime 2019-08-15 15:45:00
Nrc Rpt Num 1255308 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Off Water Depth 210
Off Accident Origin On The Outer Continental Shelf (Ocs)
Off Ocs Area Hi
Off Ocs Block 563
Off Area Accident Type Below Water, Pipe Buried Or Jetted Below Seabed
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 24
Pipe Wall Thickness 0.5
Pipe Smys 52000
Pipe Specification X 52
Pipe Seam Type Erw - High Frequency
Pipe Manufacturer Researching Original Pipeline Docs.
Pipe Coating Type Other
Pipe Coating Details Epoxy
Installation Year Unknown
Manufactured Year Unknown
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind Yes
Ocean Seawater Ind Yes
Amount Released 0.1
Rel Water Name Gulf Of Mexico
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 3
Est Cost Prop Damage 130000
Est Cost Emergency 50000
Est Cost Environmental 0
Est Cost Other 4025
Est Cost Other Details Consulting Fees And Taxes
Prpty 184028
Accident Psig 2
Mop Psig 700
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function =< 20% Smys Regulated Gathering
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The controller was not involved in the incident cause, nor identification.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details External Corrosion
Internal External External Corrosion
Visual Exam Results Localized Pitting
Atmosphere Corrosion Ind Yes
Field Exam Basis Ind Yes
Underground Location No
Externally Coated Yes
Prior Damage Yes
Collected Data Ind No
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name T*** R*****
Preparer Title Sr. Manager Ehsr
Preparer Email T******@3**********.com
Preparer Telephone (346) 241-3663
Prepared Date 2021-12-20 00:00:00
Authorizer Name T*** R*****
Authorizer Telephone (346) 241-3663
Authorizer Title Sr. Manager Ehsr
Authorizer Email T******@3**********.com
Narrative A pinhole leak was discovered on the high island pipeline system operated by panther operating company after the producer shut in both their inlet and outlet of their system into our line. When the line began pressuring up (still within maop), the leak was discovered. The leak is on a riser coming onto platform hi a563b. The leak was immediately clamped as a temporary repair, and then a permanent repair was made with the affected section of pipe replaced. All repair work completed on 9/3/2019. This report submission is intended to correct the report type submitted in 2019 in error. The original report # 20200032 - 33604 described the leak as a pinhole leak on a natural gas pipeline. The 2019 leak was on a liquid pipeline and the volume lost was <gallon.

All rights reserved. Copyright © by ClearPHMSA